SAV5710AWW Maytag Washer - Instructions
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- Customer:
- Mike from Lithonia, GA
- Parts Used:
- WP40053901
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
Hole in Drain Hose
I disconnected the water supply line to washer and moved washer into open area. I removed the front panel of washer to gain access to drain hose. I removed hose and reinstalled new hose. I did turn the hose holder inside the washer as it allowed the old hose to rub against the housing support of the washer causing the hose to leak. I was glad that I read the article that someone mentioned in their repair. The new hose was somewhat difficult to maneuver through the back of the washer and through the part that held the hose; otherwise, it was rather easy. Thanks for the feed back on your web page.
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- Customer:
- Jacob from Clarkston, MI
- Parts Used:
- 205217P
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Socket set
Wouldn't pump out water
I found about 2-3 baby socks stuck in the pump and couldnt remove them so I had to replace the part. Unfortunately I found this website AFTER I took the bad pump off. So I ended up removing the lower front panel and then flipping the washer upside down and removing the bottom of the washer and taking the pump off because I couldnt see any other way to get it off. The new pump arrived very quickly and I put it back on and put the bottom panel back on and flipped the washer back right side up. I certainly made it more difficult then it had to be but it was still fairly easy. Now I see all I needed to do was remove the motor to get the pump off. Oh well.
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- Customer:
- Michael from Lyndhurst, OH
- Parts Used:
- WP22004042
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Socket set
Finn broke on the agitator/auger
Pop the cap off the agitator/auger no tools needed. Once removed select a socket and a socket exstension. remove the screw amd pull off the part. Make sure to save the washer that may be still attached to the inside of the agitator. install the new agitator using the existing screw and washer. Takes about 15 minutes.
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- Customer:
- Gary from North Aurora, IL
- Parts Used:
- W10116791
- Difficulty Level:
- Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers, Socket set, Wrench (Adjustable)
Loud Noise at Spin Cycle
I read what the others had done and thought it was the lower bearing so I originally tore it down and replaced just the lower bearing.
Unfortunately, after 2 + hours of doing that and putting it back together, it still didn't fix the problem. So I read more reviews and others claimed to use this kit and that it fixed the problem. So I ordered the kit.
BTW, Parts Select rocks!!!! They get me the part within about 2 days every time.. Great Service! Thanks guys!
Anyhow, part came in, knowing how to tear this thing down now, I was able to get to where I needed to be within about 45 minutes.
2 things that were difficult.
The first was removing the plate at the bottom of the tub. This is the aluminum plate that looks somewhat like a spoked wheel. Maytag has a tool for this. Without it, you must go at it with a small punch on one of the spokes and carefully tap the seal until it turns. You may have to try it from different angles to loosen it up but it will eventually give way..
Once you get that off, the second little piece of joy is actually removing the seal from the bottom of the tub. Here again, Maytag offers a tool to remove this. Without it, and with years of this rubberized fitting mounted in this plastic tub and corrded with water and crap... you will need to create a bearing puller.
I did so with a 2X4 board straddled across the bottom of the tub. I used an 8 inch lag bolt, drilled a hole through the 2X4 and placed the lag bolt throuigh the board and through the center of the bearing. I attached a large washer and nut to the bottom side of the bearing and then began to tighten the bolt on the other side of the board. By tightening the bolt, the board created alot of tension but not enough still to seperate it from the tub. With the tension on the bearing, I turned the tub over and tapped it with piece of wood the size of the bearing and a rubber mallet. It popped right off. The rest was just reassembly.
Don't forget to remove the sticker backing on the felt gasket to hold the gasket in place while you screw the tub back together...
The good news... Super quiet! So, about 3 hours.... (I had to come up with the idea to remove the bearing and build it) and it's all done..
Yeah.... Fun Saturday.
Unfortunately, after 2 + hours of doing that and putting it back together, it still didn't fix the problem. So I read more reviews and others claimed to use this kit and that it fixed the problem. So I ordered the kit.
BTW, Parts Select rocks!!!! They get me the part within about 2 days every time.. Great Service! Thanks guys!
Anyhow, part came in, knowing how to tear this thing down now, I was able to get to where I needed to be within about 45 minutes.
2 things that were difficult.
The first was removing the plate at the bottom of the tub. This is the aluminum plate that looks somewhat like a spoked wheel. Maytag has a tool for this. Without it, you must go at it with a small punch on one of the spokes and carefully tap the seal until it turns. You may have to try it from different angles to loosen it up but it will eventually give way..
Once you get that off, the second little piece of joy is actually removing the seal from the bottom of the tub. Here again, Maytag offers a tool to remove this. Without it, and with years of this rubberized fitting mounted in this plastic tub and corrded with water and crap... you will need to create a bearing puller.
I did so with a 2X4 board straddled across the bottom of the tub. I used an 8 inch lag bolt, drilled a hole through the 2X4 and placed the lag bolt throuigh the board and through the center of the bearing. I attached a large washer and nut to the bottom side of the bearing and then began to tighten the bolt on the other side of the board. By tightening the bolt, the board created alot of tension but not enough still to seperate it from the tub. With the tension on the bearing, I turned the tub over and tapped it with piece of wood the size of the bearing and a rubber mallet. It popped right off. The rest was just reassembly.
Don't forget to remove the sticker backing on the felt gasket to hold the gasket in place while you screw the tub back together...
The good news... Super quiet! So, about 3 hours.... (I had to come up with the idea to remove the bearing and build it) and it's all done..
Yeah.... Fun Saturday.
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- Customer:
- Henry from Bradenton, FL
- Parts Used:
- WP27001006
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Wrench set
Belt degraded with failure
After turning on the machine set to the spin cycle and acertaining that the problem was not a switch or the motor the lower cover was removed (Two sheet metal hex head screws)with appropriate socket. The failure of the belt was self-evident, having sprayed itself in granuals, the belt itself having parted with easy removal.
A search of the internet produced the order for drive belt, which arrived in a timely manner trough Fedex.
Replacing the belt was the most labor intensive part of the process. No mirror being available a CD was placed in the base of the machine in order to view what fasteners (Three torx head) fasened the pump to the motor assembly. Removal of the pump was necessary in order to replace the belt.
The removal of the fasteners required that three holes (120* angular spacing, 1/2" diameter, located on the pump fastener bosses) be drilled in the machine base in order to
remove and replace. This required setting the machine on its side. (Tell the engineers to put an inspection plate there in order to negate having to drill the holes. Thankx.) Pump assembly was lowered off driveshaft and belt replaced. Tensioner set on belt after pump assembly fit to driveshaft and torx fasteners replaced and tightened. Machine powered up, checked for function. In use. Lower cover replaced. I'll be using your buisness for parts again, no doubt.
A search of the internet produced the order for drive belt, which arrived in a timely manner trough Fedex.
Replacing the belt was the most labor intensive part of the process. No mirror being available a CD was placed in the base of the machine in order to view what fasteners (Three torx head) fasened the pump to the motor assembly. Removal of the pump was necessary in order to replace the belt.
The removal of the fasteners required that three holes (120* angular spacing, 1/2" diameter, located on the pump fastener bosses) be drilled in the machine base in order to
remove and replace. This required setting the machine on its side. (Tell the engineers to put an inspection plate there in order to negate having to drill the holes. Thankx.) Pump assembly was lowered off driveshaft and belt replaced. Tensioner set on belt after pump assembly fit to driveshaft and torx fasteners replaced and tightened. Machine powered up, checked for function. In use. Lower cover replaced. I'll be using your buisness for parts again, no doubt.
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- Customer:
- Wayne from Ankeny, IA
- Parts Used:
- WP27001113
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Screw drivers
Washing machine would not consistenty run through the cycles.
Removed 6 screws from the metal plate on the back of the washing machine. Removed the dial from the front of the timer. You have to pop the center peice of the dial out which then frees the rest of the dial to be removed. Removed one screw from the timer back of the timer. Slid the timer out and unplugged it. Installed new timer.
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- Customer:
- George W. from Thomasville, GA
- Parts Used:
- WP27001006, 40061401, WP40045001
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers, Socket set
The pully seprated, and wore the belt out.
I takened the 4 bolts out of the motor assimbley, and droped the whole thing out where I could see the screws that held the water pump on, and I took them out, and lifted the water pump, and put the belt in place, and the new pully on , and the new spring in place. Then I reversed the proseger.
It works like a new one.
It works like a new one.
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- Customer:
- Douglas from Eden, UT
- Parts Used:
- W10116791
- Difficulty Level:
- Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Socket set
loud noise on spin cycle
I had previously done a partial tear down on the machine to see if I thought I could do the repair. The dealer try's to scare you with warnings about special tools etc. Looked OK and after reading other comments on this site, I thought I would try. The only comment that I would add to what has already said is that you should have the recommended sealer or an equivalent sealer. I used weatherstrip adhesive that I had on hand. Hope that it holds up! Like it says in the directions, the seal will lift up if there is too much sealer under the lip of the seal. Just hold down the seal with a weight until the adhesive sets up and then it will stay. I've fixed cars for 30 years and this was an easy repair comparable to replacing wheel bearings.
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I had to replace the tub,because it cracked when replacing the bearing and seal
I had no problem replacing the triple lip seal and bearing. I cracked the plastic tub, which after 10 years was very britle and cracked in two places ON THE SIDE. To remove the bearing I had to improvise a bearing removal tool using a puller I had on hand and a 1 lb metal coffee can. It worked great! You need to use some type of pulling device to remove the bearing without damaging the tub.
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- Customer:
- Mary Lou from NEW ULM, MN
- Parts Used:
- WP40053901
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Wrench (Adjustable)
The hose on the washer been leaking and needed to be replaced.
After receiving the new hose we replaced the hose and tested the washer by running a rinse cycle. The new hose fixed the problem.
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- Customer:
- John from BAINBRIDGE IS, WA
- Parts Used:
- WP40053901
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver
Cracked hose leaking
Hardest thing was moving washing machine away from wall. Two screws on panel. One screw for hose.
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- Customer:
- William from NEW DURHAM, NH
- Parts Used:
- R0131578
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Cold water flow very slow.
Removed and replaced mixing valve. Shut off hot & cold water supply to machine. Pull machine electric plug. Access back of machine. Remove water supply to machine. (Pliers) Be sure to keep some paper towels handy to pick up residual water. Remove screw that holds mixing valve mounting plate to machine. Pull plate away from machine. Undo hot and cold elect. connectors to valve. Remove water supply to valve. (Black hose-screwdriver.) Remove screw holding valve to mount plate. (Nut driver.) Install new valve onto mount plate. Reverse process used to remove valve. Test by turning on machine.
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- Customer:
- Bruce from Harrison, OH
- Parts Used:
- WP40004001
- Difficulty Level:
- Very Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set, Wrench (Adjustable)
noise while spinning
had to completely disasemble whole washer drum and mechanical components to remove upper bearing on transmission,the drum hub was corroded on the shaft. I had to use a gear puller and a propane torch to get the hub off upper shaft of the transmission. then press the bearings in the respective sheet metal supports. reassembly was alot easier than taking it apart. Not a job for an average homeowner. It would not have been repaired without the wheel puller. all the seals were reusable A week and a half of use later no leaks and works great
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- Customer:
- Tracy from martinez, GA
- Parts Used:
- W10116791, WP27001006
- Difficulty Level:
- Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
Upper Bearing sounded like jet taking off during spin cycle, burnt belt in half
Unplug and disconnect Power, Drain and h20 connections. Removed front panel, disconnected internal electricrical connections and capicitor from washer. Remove 11 (I think) screws connecting outer cover to base. Remove pull drain hose through the outer cover and hold the end lower that the washer to drain the excess h20. Remove the hoses from the pump and outer tub. Remove outer cover from base exposing the guts. Grab the bottom of the agitator and pull up pretty hard. Agitator will pop off, watch your head. Remove the 4 bolts attaching the Inner tub to the hub. Remove seal from top of transmission spline. You will need a 38mm deep well socket to remove the nut from the top of the transmission. I used a socket and a impact wrench to remove the nut. Remove the teflon seal that is below the nut. You will need a puller and/or grinder to remove the hub from the transmission spline. My puller broke, so I ended up using an air grinder to cut a couple of pizza slices out of the hub. Then I used an air hammer to break the slices off of the hub. Once it is cut the cast aluminum is quite brittle. Pull what remains of the hub off of the transmission spline. Remove the bolts that connect the transmission housing to the outer tub. Remove the 3 bolts from the underside of the outer tub that connect the outer tub to the upper bearing. using a set of vice grips, grab the top of the springs that connect the outer tub to the base and carefully remove them one by one.
The outer tub should slide right off. Remove the bearing from the transmission. Supplies that you will most likely need are the 3m800 sealant, when you get this you will only need a little around the bottom of the lip where the new seal attaches to the bottom of the outer tub. You will also want to get the Seal tool which will ensure that the seal that goes around the top of the transmission spline is seated properly. Assemble in reverse order but keep in mind to attach tub bolts prior to attaching the springs. Also keep in mind that both maytag and amana make a washer with the same model number LWA80AW. Check to see which one you are ordering for. The kits are different. Don't ask me how I know. Just make sure you get the correct kit the first time, it will save you a whole lot of head scratching.
The outer tub should slide right off. Remove the bearing from the transmission. Supplies that you will most likely need are the 3m800 sealant, when you get this you will only need a little around the bottom of the lip where the new seal attaches to the bottom of the outer tub. You will also want to get the Seal tool which will ensure that the seal that goes around the top of the transmission spline is seated properly. Assemble in reverse order but keep in mind to attach tub bolts prior to attaching the springs. Also keep in mind that both maytag and amana make a washer with the same model number LWA80AW. Check to see which one you are ordering for. The kits are different. Don't ask me how I know. Just make sure you get the correct kit the first time, it will save you a whole lot of head scratching.
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- Customer:
- DAVID from ORLAND PARK, IL
- Parts Used:
- R0131578
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
Water Inlet valve wouldn't work for cold water
Water inlet valve was different than the one shown on web photo. The hose supplied was the wrong size so I had to use the original old hose. Wire harness had to be modified since the electrodes were on opposite sides of the valve. Overall I was disappointed with the part and the service.
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