MLE20PDBGW2 Maytag Washer Dryer Combo - Instructions
Jump to:
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
- Customer:
- PHILLIP from AUSTIN, MN
- Parts Used:
- 279827
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable), Wrench set
Start and then kick out.
Two Phillips screws, and 2 5/16 bolts and the dryer is open for this repair. Remove the drum and note the placement of the drive belt. Then using a pipe wrench grab the rear plastic fan housing, at the rear of the motor shaft, and turn the front of the motor shaft CLOCKWISE. If the Fan is ceased (as it was in my case) you will need to use locking vice grips (at least 3 or 4 between the fan blades to stop the fan blades from turning on the rear shaft.) while your turning the front of the motor's shaft. If done properly, you should have about 25-30 turns before the motor is free for replacement.
Once this is accomplished, mounting the new motor back into the dryer is a simple matter of reversing your steps. But keep note of the belt placement and the motor wiring placement before starting.
Once this is accomplished, mounting the new motor back into the dryer is a simple matter of reversing your steps. But keep note of the belt placement and the motor wiring placement before starting.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Carl from MARION, KY
- Parts Used:
- WPW10314173
- Difficulty Level:
- Really Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
Making a racket.
Took the top off and then front off and drum out . Replaced Drum roller and shaft support bolts.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Lawrence from ARITON, AL
- Parts Used:
- 280114
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Screw drivers, Socket set
Old. Original heat seal was deteriorated and peeling off. Streaks were getting on the clothes.
Removed the front panel, removed the tub and removed the old seal. Tub seal area was scraped, sanded and wiped with acetone to ensure a clean. Bonding surface. Applied adhesive with and acid brush to get a consistent adhesive layer without getting too much in any one place. Seal was a bit smaller than the tub circumference so it had to be stretch to fit. While the adhesive was curing , I took the time to clean the contact surfaces and vacuum the lint from inside the cabinet. Reinstalled the tub, drive belt and front panel.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Madeline from PANA, IL
- Parts Used:
- WP8577274
- Difficulty Level:
- Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set, Wrench (Adjustable), Wrench set
YouTube video dated 9/28/2015
How to repair E1 error/fault on Whirlpool Duet dryer model GEW9200LW0 please watch that video very helpful.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- David from HUNTINGDON VY, PA
- Parts Used:
- 4392067
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Bad screaming noise
Replaced 4 wheels and new belt
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Dwayne from Bainbridge, PA
- Parts Used:
- WP8577274
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Socket set
Dryer would shut off mid way through cycle and give an E1 error code
After turning off the power to the dryer I removed two screws to the bottom front panel and droped it out of the way. I remved three screws hloding the lint screen in place just for better axcess to the element. I then removed the two wires attached to the element and then the two screws holding the element in place. I put everything back together in reverse. I also took the time to clean any dust and lint out.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Victor from ORANGE, CA
- Parts Used:
- 4392067
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
Dryer was not running as fast as normal, belt was squeaking loudly
The repair went well, using the whirlpool repair manual and looking at the video from PartSelect. The machine was a bit different than the one in both the video and the manual but that did not cause any problems. The only tricky part was to reinstall the belt "blind" behind the motor, easy to pinch your fingers and also get scratched by the sheet metal edges. To make it easier for that part I supported the drum with the old belt and a bungee cord to the garage frame so I did not have to hold it up and work under it at the same time. When the drum and new belt were in place I just cut the old belt, it was going to the trash anyway.. I replaced the belt and the tension pulley, witch was not turning easy and worn by the belt. I also put some grease ( SUPER-LUBE, www.super-lube.com) on all pulleys. It took about 2 hours because I am 78 years old and have heart problems.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- James from Randsburg, CA
- Parts Used:
- 279311
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
No heat
I had two dryers, one was gas and the other was electric. The electric stopped heating. So I rolled out the gas dryer, but it was setup for natural gas and at this location, I only have propane. So I changed the jets to work with propane, in the process I broke the igniter, so I replaced that and that made the propane one work. Armed with the knowledge from that job, I took the electric dryer apart located the thermostat and replaced that and low and behold I have two working dryers. One for now and one for an emergency. I only have four screws left over!!!! Jim Cooke
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Raymond from Washington, DC
- Parts Used:
- 279570
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers
Door latch catch broke
I squeezed the latch catch with a pair of pliers and pushed it in the catch hole. But that was the final repair. There were two "repairs" before that. First, we used two commercial grade rolls of wide plastic tape to tape the dryer door shut each time we used it, for a year, until we ran out of tape. Second, we positioned a chest of drawers in front of the dryer and wedged a 1" x 4" against the door. Very effective. Then I broke down and ordered the $3 catch.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Cynthia M from Westfield, MA
- Parts Used:
- WP660658
- Difficulty Level:
- Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Screw drivers
Dryer drum wouldn't turn and motor would shut off
First I was told by the maytag repair man that the motor was shot and it would be 467 dollars to repair. Since I didn't have that kind of money I decided to take it apart to see if I could replace the motor myself. Once I had it apart I saw the part that held the motor in place was broken off and the motor was out of place causing it too shut itself off. Once I figured it all out it took about 2 minutes to replace the less than 6 dollar part! Thanks partSelect!!!
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Candido from GREENVILLE, TX
- Parts Used:
- WP8577274
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers, Socket set
Dryer won't start.Only make a click noise.
Remove top,front and panels.change thermal fuse and outlet thermistor.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Steven from WICHITA, KS
- Parts Used:
- WPW10314173
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers
Loud squeaking noise
Replaced the most worn drum wheel any lubed the belt tension arm pulley. The noise didn't go completely away. There are 4 drum wheels. I need to order 3 more wheels and the tension arm now.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- WILFRED from NORTH HIGHLANDS, CA
- Parts Used:
- 279570
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
I recieved the kit the next day after ordering. It took about two seconds to do the repair
all that was required was to push the catch into the slot notools needed.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Scott from WOODBURY, MN
- Parts Used:
- W10120998
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
lint screen was not catching lint and sending out the dryer vent
replaced dryer lint screen with new.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- william from VIRGINIA BCH, VA
- Parts Used:
- WPW10467289
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers
Replacing the heat sensor following an F-24 Error Notice.
I followed your repair video explicitly, simple fix. However, one should
be careful when disconnecting the two prong electrical connector from
the heat sensor. the two black wires can pull free easily. In that case, the
rear of the female plastic wired connector must be extracted to allow the two black wires to be "pushed" into the narrow slot which displaces the
wire insulation and allows for a good electrical connection. If a punch tool is not available a pair of needle nose pliers works. Also, observe
the orientation slots on both the male andfemale connectors - they
connect one way only! I set the washer on it's face while effecting this
repair to better see what I was doing (eyesight not as good as it used to be). Thanks for the timely support!
be careful when disconnecting the two prong electrical connector from
the heat sensor. the two black wires can pull free easily. In that case, the
rear of the female plastic wired connector must be extracted to allow the two black wires to be "pushed" into the narrow slot which displaces the
wire insulation and allows for a good electrical connection. If a punch tool is not available a pair of needle nose pliers works. Also, observe
the orientation slots on both the male andfemale connectors - they
connect one way only! I set the washer on it's face while effecting this
repair to better see what I was doing (eyesight not as good as it used to be). Thanks for the timely support!
Was this instruction helpful to you?
Thank you for voting!