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MLE19PNAYW Maytag Washer Dryer Combo - Instructions

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All Instructions for the MLE19PNAYW
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Customer:
Lisa from Trenton, NJ
Parts Used:
WP6-3705180, WP6-3700340, WPY312527, WP354987
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Pliers, Screw drivers, Socket set
Dryer made very loud squealing, screeching noise. (Sometimes Intermittent, sometimes constant)
Note: You may want to consider replacing the 2 Drum Support rollers at this time (while your in there)

1. UNPLUG YOUR DRYER FIRST.

2. Using a phillips head screw driver - Remove 2 screws that secure the dryer door hinges to the frame, Lift door very slightly to unhook hinges and pull out door with hinges attached as straight as possible, set aside. Remove the 2 plastic tabs from the opposing side of the door hinge also secured by screws.

3. Remove the front panel (panel is shaped like a football goal post) by tilting out the top ends of the front panel toward you, then lift up to remove panel from the bottom metal retaining tabs.

4. Remove the 2 hexhead screws from the 2 retaining clips (security hooks) that secure the top
of the dryer closed.

5. Systematically remove the hexhead screws from the rest of the front of "shroud" (it holds (suspends) the drum in place between the front and back of the dryer).

*** I didn't disconnect any wires, I carefully swung out each piece that had wires attached, propped up those parts vertically ensuring no strain on the attached wires. Others may want to disconnect wires to avoid breaking or damaging them.

6. Vacuum out any dust/lint that may be present.

7. Draw a quick diagram of how the underside of the belt is threaded on the idler pulley and motor pully first. Release the tension of the belt from the underside of the drum. The easiest way is to push the idler pulley arm away from the belt and slide off the belt from the idler pulley and motor pulley. Slide the drum out.

8. Remove the hexhead screw from the bottom of the idler arm. Disconnect from retaining spring.

9. You may only need to replace just the Idler Pulley Wheel. I recommend replacing as a "unit" the Idler Pulley Wheel, Idler Arm, Ring-E and Idler Shaft Washer(s) - then you can just swap out the old one for the new one.

10. Reassemble

(When reassembling the belt - place around drum first and slide drum in place. Now from the underside-place (drape) belt around the motor pulley (it will be very loose) Now push the idler pulley arm toward the motor pulley, engage the left side of the belt around the idler pulley and slowly allow idler pulley to increase its tension on the belt) You can test manually by rotating the drum by hand to ensure proper movement.)
18 of 20 people found this instruction helpful.
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Customer:
Robert from Buffalo, NY
Parts Used:
WP694674
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers
Temperature setting not working
Took off back cover, thermostat was easily identified because of photos I've seen on website. Took 2 connectors off, removed 2 screws and removed old thermostat. That was pretty much it!

NOTE: Replacement thermostat 694674 has an adjustable temperature range setting that MUST be manually set prior to installing! You need to use the enclosed chart to find your original part# and make sure the setting is matched. My original part# 341146 had a "D" setting so I had to change but very easy to do.
19 of 23 people found this instruction helpful.
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Customer:
Glenn from New Paltz, NY
Parts Used:
12002533
Difficulty Level:
A Bit Difficult
Total Repair Time:
15 - 30 mins
Tools:
Pliers, Screw drivers
Daughters destroyed door seal with comforter caught in the door...
*** MY REPAIR STORY ***

*** Rule #1: READ THE OTHER STORIES FIRST! ***

The best tip was supplied by the guy that used a piece of good twine/string to help him reconnect the inner seal cable and spring assembly; the whole business of using a buddy to do so is a lot of hooey. Save yourself the aggravation of using your wife, kid or other mechanically-declined individual, and use the string trick. It is still a royal pain, but it is far superior with only one person, using the unbeatable mechanical advantage that the string gives you. I used a piece of good waxed poly twine; I tied it to a convenient hole near the front right side corner of the machine, and then threaded it throught the spring and pulled it with some good pliers in order to stretch the spring enough to re-engage the other loop of the inner seal cable, using needle nose pliers. Of course, it took about four shots to get it right, but I was particularly anal about getting the cable ends in their originally-installed orientation. In retrospect, it ought not make too much of a difference, as long as you keep the spring near the top of the drum and respect the placement of the cable: make sure it is fully in its recess in the seal, all the way 'round. Additionally, pay close attention to the drain hose attachment and outer seal installation; you don't want any more leaks. I have strong fingers so it was a snap, and there are both molded recesses, arrows and "tits" along the seal edges that correspond to the outline of the machine's mating surfaces. Please take the time to push in all the lugs all the way all around in all positions; your floor's dryness is depending on you. As far as the inner seal cable/spring situation goes, be aware that any slight failure to get it right will likely cause a "domino effect" that will necessitate that you to reinstall the seal along its entire periphery, on both inner and outer sides... hold onto that cable, and watch as you tension the spring... it will cause the inner seal to walk off the drum if you aren't paying attention, and you will not be able to recover the perfect position you had at first. In honesty, that is the only "difficult" part of the job. Ensure you've had ample food & drink before you undertake seal replacement ( and not alcoholic drink, either... ) !

As with all jobs of this type, the end was far better than the beginning... the machine doesn't spew water out onto the floor anymore, and helped reinforce my claim to the "most useful" Family Member status! lol My wife was nice to me for almost a week afterwards... your mileage may vary.

PartSelect.com, thank you so much for not only the right part at the right price delivered fast, but also the forum where others could report their repair experiences in order to give a good heads up to those contemplating this repair job. Super site, super business, would definitely use again. A+

Regards,

Glenn Buononato
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Customer:
Matthew from Lombard, IL
Parts Used:
WP33001807
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Screw drivers
Rear Felt seal came out, squealing sound when drying
Turned off gas and unplugged dryer
1) Removed bottom front panel
2) lifted top panel up like a car hood
3) Removed door springs
4) disconnected electrial connections to door unit, removed door unit
5) removed drum, scraped old felt from drum
6) glued new felt with a very strong glue (nanoglue or gorilla glue, same thing), let it dry overnight
7) secured back inside panel, replaced drum and put dryer back together.
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Customer:
Paul from Tallahassee, FL
Parts Used:
22003728
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Pliers, Screw drivers
Bad pressure switch on front loading washer allowed water level to exceed proper height leading to water leaking from door seal.
First I sent the local repair man away. I recieved much better advice from this forum. Partselect saved me literally hundreds of dollars. The local repair man was headed in the totally wrong direction.

After identifying the problem with the online partselect repair forum I ordered the part. It was in stock and delivered the next day.(local dealer needed 2 weeks to get the same part) The repair was fairly easy. The pressure switch sits on top of the water manifold for the pump. Removing the old pressure switch required disconnecting the connector and then pulling it free from the snap clip on the backside of the switch. After taking out the old switch I took off the pipe boot that the pressure swich inlet tube seats into. This pipe connects directly to the drain hose that runs into the manifold. I would recommend this to make sure this pipe is not clogged. The pipe needed to be cleaned as a plug of old detergent was totally blocking the pipe.( In fact this was probably the cause of the problem as no water could make it to the actual pressure switch. I had already ordered the new swith so I installed it anyway.) After cleaning out the pipe I put the boot and retaining clip back over the top of the pipe. This was the most difficult part of the repair. It took some time as the clip is very difficult to replace. From there it was just snaping the new switch into place, plugging in the connector and it was done. After putting the front washer cover back in place it was ready to go.
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Customer:
Stacie from Las Vegas, NV
Parts Used:
W10181639
Difficulty Level:
A Bit Difficult
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
The spinner support had sheared off
First, I removed the drum. Removed the spinner support. Removed old seals. Reinstalled new spinner support. Reinstalled pulley and belt. Reinstalled drum. Reinstalled machine covers.
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Customer:
Scott from Sedalia, MO
Parts Used:
WP25001052
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers, Screw drivers
Washer would not drain
Starting out I found the code that the washer was showing,ND, Meaning no drain so I read up on and people where saying that the pump had a blockage in it, so I took the back of the washer to gain acess to the pump, I took the drain hose off to look in side to see if there was a problem there was nothing in the pump itself so I started to remove the pump I undid the wiring harness to find the problem, the red wire to the pump had burned in the harness order the part from part select and 30 minutes later my wife was doing laundry again..........Thanks partselect for the fast shipping and quality parts very easy repair.
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Customer:
Inocencio from Edinburg, TX
Parts Used:
LA-1003
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Door Catch was broken
I just inserted the door catch, which by the way fit in perfectly. Thanks. Took 5 seconds to repair.
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Customer:
SALLY from ANAHEIM, CA
Parts Used:
WP33001762
Difficulty Level:
Easy
Total Repair Time:
Less than 15 mins
Tools:
Pliers, Screw drivers
Dryer wouldn't start
We tried replacing the door switch first, still didn't start. Next we tried the thermal fuse and it turned on and has worked ever since.
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Customer:
Terry from Caruthersville, MO
Parts Used:
33001790, WP33001789
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Pliers
loud noise inside dryer
After changing all the rollers in the dryer (which didn't fix the problem) I decided to take apart the blower. Sure enough, that was the problem. As the dryer heated up, the damaged wheel would swell and start rubbing the housing. I replaced both and fixed the problem. The repair was pretty easy, since I had taken the dryer apart several times replacing the rollers.
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Customer:
Gregory from El Dorado, AR
Parts Used:
12002022
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Screw drivers, Socket set, Wrench (Adjustable)
Bearings making loud rough noise
Thanks to all the others who gave detailed information I was able to replace the front & rear bearings and front seal. I must say it was a time comsuming job but at least I am alot clearer on the quality of clothes washing machines. I do believe I could give a manufacturer / designer some design points after working on this Maytag Neptune. I was able to knock out the bearing shaft that held the stainless perforated tumbler inside the plastic tub/drum by using a #3 LB hammer I reinstalled the old screw in the shaft which held the plastic pully on because this would keep the end of the shaft from being damaged. After several blows it started moving I was afraid I might damage the plastic drum but fortunately no damage was done to it. After removing the stainless steel perforated tumbler here is where it really got interesting. The Hub that held the old seal was shot! pretty much deteorated from corosion it seems. Here is where I could significantly help a manufactured/designer out The bearing/seal hub should have been made out of stainless instead of Pot metal/ aluminum or whatever they made it from. After much cleaning with a small wire brush and vacuming all the debree out of the Tub I didn't have much hub left to install the new seal. Also the three armed Spinner was very coroaded it attaches to the back of the stainless tumbler I removed it from the stainless tumbler and wire brushed it the back side was full of crud, it looked like left over washing powder or soap and Corosion debree it was a job just cleaning it up. I pressed on and on though replacing both bearings front and rear. Thanks to another person who explained the easy way to remove the bearings and race I was able to do so without removing the Drum/Tub as others stated they had to do. The Dremmel and a few Cutter blades did the trick I cut a wide V notch in the bearings and the bearings fell out I then cut through the bearing race being careful not to cut too deeply although if you did slightly cut beyond the race it really wouldn't matter because the front seal will keep it from leaking anyway. Anyway when I cut through the race it made a ping sound and the race pulled away and fell right out of the HuB. The front & rear bearings a definately serviceable and it doesn't have to be a beat/bang ordeal. after cleaning up the hub I tapped the new bearings in place and discarded the metal spacer that went inside the middle of hub. I then brainstormed on how I could install the new Lip Seal upgrade and then it dawned on me that since the inner Hub that holds the seal was so far gone and only enough left to barely hold the new seal in I remembered the ole saying Don't Discard just use JB Stick or JB Quick I used JB Stick to fill in around the new seal because it is supposed to bond to metal and it did just that I pressed the putty in quickly before it hardened bringing it out even with the plastic drum where the origional hub should have been and made the repair to the deteriorated Hub so that the Seal would stay in place it Worked! This Maytag Neptune was given to me by my mother in-law she did not want to wait on the repair after I tried to previously repair the problem with it I just did not delv deeply enough into the problem with this washingmachine at first. I previously removed both Pumps thinking they were not pumping all the water out because the Towels especially were staying soaked. Both the pumps were nasty with alot of debree inside of them now I know that because of the deteriorated Seal Hub on the inside had done the dirty work. The Pumps can be easily taken apart only a few screws and the plastic impeller can be gently pried off also that is where I found alot of particles from the deteoriated Seal Hub I then reinstalled the pumps and they worked fine pumped out the water. Then that is when I noticed it wasn't cycling properly also Ha Ha I thought to myself what else could possibly be wrong with this washing machine? Thanks to Parts Select site I wa
17 of 22 people found this instruction helpful.
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Customer:
john from richland, MI
Parts Used:
12002022
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Pliers, Screw drivers, Socket set, Wrench set
Front bearings totally destroyed rear bearings rusted out
I found your site where other people worked on their washers . I removed the front & rear panels. at the front I found that removing the rubber tub seal was easy, then I removed the 3 agitaters that cover the nuts that hold the tub to the support drive shaft ,I saved the plastic shims nuts & washers then removed the tub,I removed the drive wheel, I put the bolt & washers back in the shaft end & knocked it out with a 1lb hammer.I removed the motor and all the hoses also the front & rear WeightsI left the switches connected to the wires, for everything I removed including screws I taped them all to the parts that they camefrom .Then I knocked out the rear bearing with a 8" long 1/2'dia.piece of steel rod taking care to drive evenly around the circomference of the bearing. the front bearing was in 2 pieces with the bearings in a pile inside the hub because of the spacer between the bearings there was not a lot of bearing to hit but eventually it came out I saved the spacer & the rear bearing clip & cleaned them up for reuse.The face of the crap metal insert was badly corroded ,I cleaned it and all surfaces inside the hub with a wire brush in my drillmotor I found bearings at an industrial store and found NO problem matching the old bearings I ordered the lipseal kit from Part select It came with 2 seals & dubious instrutions I found the revised seal did not fit my support shaft but the other one did ,it comes in 2 parts that are stuck together with grease pry them apart with e small screw driver. I then tapped the new bearings in rear first then the spacer. then the front bearing I tapped it in enough to get it started then I inserted a cardboard toilet roll center folded enough to go in through the spacer & the rear bearing this lined up the parts so the shaft will go throughafter the bearings & new seal were in I used a marine silicon to put over the corroded face & made shure that it snugged up to the seal ,sealing it good I let it set for 24 hrs Then I putthe shaft back onto the tub put the agataters back on, then put the outer shell with the new bearings back in place connected the hoses, the weights, the switches, the wire clips,the motor,hooked up the springs ,inserted the tub, put the drive wheel back on the shaft then the belt , then put all the front panels back and IT ALL WORKED. total cost $36.00 for bearings $53.00 for the seal kit so about $90.00 total & two weeks at about a couple of hours a day .shure beats $650.00 + $300.00 at a repair facility . GOOD LUCK .IAN
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Customer:
paul from madison, CT
Parts Used:
W10169313
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Switch did not turn off dryer when door opened
Switch can be removed from outside of dryer and your video described the repair as having to work from inside dryer. But since wires were still attached to old switch, it could be popped out and wires switched. Since there were three wires on new switch to allow it to turn on and off a circuit, it was useful to check the resistance of the switch compressed or released to be certain I was attaching the two wires to the right two poles of the new switch. But that all required only a couple of minutes. Thank you.
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Customer:
gary from tecumseh, MI
Parts Used:
12002533
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Pliers, Screw drivers
door boot seal was all milldew
Unpluged washer. Removed screws from front and removed door. Removed one more screw on each side and was able to remove front panel, and also lift the top. The boot seal was held in place with a wire and a spring. I unhooked the spring and removed the wire and then removed the old boot seal. I then proceeded to reverse the steps to put it all back together. It took me almost 4 hours. I also used the picture on your web sight to see how things were put together. It really helped a lot.
15 of 21 people found this instruction helpful.
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Customer:
Kevin from San Diego, CA
Parts Used:
WP6-3129480, WP9703438, WP33001443, WP312535, 12001541
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers, Socket set
drum support roller was squeaking
My 11 year old grandson and I did the repair together. He had a blast and I did too. First we removed a bunch of screws that got us no closer to getting the machine apart than when we started. Then I remembered from the last time I had the machine apart that there are two screws just below the door, angled as not to be visable unless you know where to look. Once we removed those the from came off. We removed the wires for the door light and heat sensor, remembering the order of the wires for later reinstallation. Then we undid the bolts holding down the top. Once the top was removed we took off the belt and removed the drum. We used the retainer pliers to remove the retainer ring from the first roller. We removed the roller and also the shaft as this roller was the noise maker and the shaft was not in reusable condition. We installed a new shaft, roller washer, roller, another roller washer and then the retainer ring. We repeated the same process on the other roller, although we did not replace the shaft as it was in good condition. It turned out I did not need to order the shaft washers as the rollers came with washers. Oh well, its not a good job unless you have parts left over when you are done. Once we replaced the rollers we commenced reinstallation. But first we had to google for diagram of the proper belt installation, which we found and that got the drum and belt installed properly. Thankd god for the internet. Once we had the drum installed we put the machine back together in the opposite order we took it apart. An operational test showed we did the job right, no more squeaking. The only injury was my grandson cut his thumb right after I gave him the speech about watching where your hand is going to end up when that bolt breaks free. It broke loose and into the metal bracket went his thumb. Oh well it was a good lesson and it was not a bad cut. All in all a good repair.
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All Instructions for the MLE19PNAYW
31 - 45 of 727