MDE13PDBDW Maytag Dryer - Instructions
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- Customer:
- Alan from BETHESDA, MD
- Parts Used:
- WPY312527, WP6-3037050, WP6-3033630
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
After a period of the dryer not being used, the idler pulley wheel froze up on the shaft of the idler pulley arm.
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
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- Customer:
- David from Calvert City, KY
- Parts Used:
- WP6-3129480, 12001541
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Wrench set
drum support roller had come apst from bearing and was making a squealing noise when dryer was running
first i removed the screws holding back cover. Then I remeved nut from tumbler roller shaft. Then I slid shaft from roller .I removed roller then replaced with new one. Installed new shaft then replaced back cover. recieved parts from parts direct very promptly & they were the right parts the first time thanks very much
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- Customer:
- Robert from Somers Point, NJ
- Parts Used:
- WPY312959
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Dryer tumbler did not turn, dryer still turned on, dryer still produced heat : diagnosis broken tumbler belt..
I looked for dryer repair videos on my computer. I found several and they all showed me that what was most likely broken was the tumbler belt. I didn't even know dryers had a belt. My dryer still turned on,and still produced heat. It just wouldn't rotate. One of the videos even used the exact Maytag dryer in their video that I had. After watching it a few times, I knew I could make this repair. I am pretty good at fixing things if I can first see it done. I had never taken a dryer apart before though. I pulled the dryer away from the wall and unplugged it. I unscrewed the small access panel on the back of the dryer. This let me see the two belt pulleys back there. Then I went to the front and removed the two screws(my particular model) that held the front panel on and removed it. I then unscrewed the four screws holding on the front face plate in front of the tumbler. Next, I pulled the tumbler out, it is not screwed in. There was the broken belt. It took two days with regular shipping for the belt to come in. I put the tumbler back in, resting it on its two supports, placed the belt on, flat side down, and routed the belt through the pulleys in the back of the dryer exactly as it had been shown in the videos. I turned the tumbler clockwise two full rotations by hand to make sure the belt was seated correctly on the pulleys, and it was. I then screwed the face plate back on in front of the tumbler, put the front panel back on and screwed it in. I then reattached the back access panel. I plugged the dryer back in and turned it on. It worked. Though it may take a bit longer, this type of repair is about as easy as replacing a broken belt on a vacuum cleaner even for someone who has never done a dryer repair before. Watch a Repair Clinic video and if you enjoy fixing things, replacing a belt on a clothes dryer will be your next successful repair. It really is pretty easy.
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- Customer:
- David from Lower Burrell, PA
- Parts Used:
- 306207
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
electric dryer had no heat
I removed the cover from the control panel, took out the schematic, removed the rear cover by the motor, followed the schematic, powered the heater by taking the blue hot leg wire off the right side of the switch and touching it to the black lead for the heater on the left side, and I could hear the heater power on. Since bypassing the motor start switch powered the heater, I ordered the part. When it came, I installed it in about 5 minutes and the dryer worked perfectly.
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- Customer:
- Robert from Sacramento, CA
- Parts Used:
- WP33002970
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
I relaced our worn out lint filter
My part was not amazing. What was genuinely cool: I ordered it one day and it was here the next, took out the old and put in the new. Thanks for getting it here so quickly.
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When the dryer grumbles check the blower wheel too.
If your dryer is making a rumbling noise, change the blower wheel. It's plastic and the heating and cooling cycles causes the keyway in the plastic to give out and the wheel just spins causing the noise and the slower dry time. The other parts I replaced see below. Like many other repairs, remove screws below dryer door. Mark all wires and locations for re-assembly. Next remove front tumbler/lint screen assembly (4 sheet metal screws 2/L 2/R. Work belt off back of tumbler and remove. Use flathead screw driver to release tabs that hold felts on both front and back tumble supports. Make sure you know rotation of tumbler and install new felts so the overlap goes in direction of spin. Use a drum stick or 3/8 ratchet extension, something dull and flat to press tabs back down on felts. A screwdriver could slip off and tear cloth. Next drill out heads of the rivets on the glides and remove teflon glide and cork backer. Make sure all rivet material is removed front and back. Install new cork and glide. Rivet one side back in, then the other. Repeat on 2nd glide. Re-assemble dryer. Super smooth, super quiet.
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- Customer:
- William from Springfield, OH
- Parts Used:
- WP6-3129480, WP312535, 12001541, WP9703438
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
One of the roller shafts was worn
Replaced both rollers,shafts, bearings and snap rings.
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Squeaking noise
I had replaced belt, but the noise continued. Ordered new rollers and washer. Removed the front panel by tipping the dryer back against the wall and removing two screws at the bottom of the panel. Tipping the dryer makes it easy to remove the front panel. Removed the front drum support by removing four (4) screws. I was then able to just move the drum enough to have access to the rollers. Didn't even have to remove the belt. Replaced the rollers. Needed special pliers to remove and replace the retaining rings. Put the drum back into position and mounted the front drum support. Tightened four screws and then put the front panel back on. Plugged it in and tested it. Problem solved. Took about 35 minutes. Thanks
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Clunking noise when first turned on
I took the access panel off the back, realized that belt was in very bad shape. Ordered a belt when I got that changed I put it back together and it still had a clunking noise. Found out that the blower wheel was rounded off where it goes over the shaft. So to change that I took the two front screws off, then the four hex screws off of the tumbler guide. There were eight or so screws over the blower wheel, took those out and the clamp on the blower wheel then used the snap ring pliers for the snap ring, then changed the wheel. Problem solved. This website is very helpful I would not have attempted to fix my dryer without this website.
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- Customer:
- Robert from WESTCHESTER, IL
- Parts Used:
- WP33002970
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
hole in filter
took out old and placed in new
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- Customer:
- William from New Bern, NC
- Parts Used:
- WP6-3037050
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Dryer making strange thumping noise
Removed back panel of machine which exposed badly worn idler pulley. Have had problem before on another dryer so I was sure what problem was before I started. Removed snap washer and cloth washer and then bad pulley.(It was very worn and wobbly).Cleaned shaft with small piece of emery paper and put two drops of oil on shaft and replaced old pulley with new one.Put back washer and snap washer.Drive belt had slipped away from its proper position so I had to remove the front panel of the dryer to place the belt back and realign it on the drum and around the new pulley and the motor drive shaft. Not really that difficult.....Machine now runs like it's brand new.....
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- Customer:
- Chris from Truckee, CA
- Parts Used:
- WP6-3129480, 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Wrench set
worn out bearing
Unplug the dryer and pull it away from the wall so front and back can be accessed. Remove front panel. Remove front drum support. Remove rear access panel. Disengage drive belt from idler wheel. Make careful note of course of belt and which side is "outward". Remove drum through front. Remove Rollers using circlip pliers. Remove nuts behind shafts. Remove shafts. Clean-up area and parts before re-install.
Install new Shafts and nuts. Grease shafts. Install new Rollers, washers and clips. Drape drive belt over drum while reinstalling from front. Remount drive belt over drive and idler pullies from the rear access. During this step it helps to have a helper to position the belt around the drum in correct fore/aft position, lying flat and without twists, smooth side against drum. Install front drom support. Rotate drum to seat belt before closing up. Install rear panel cover. Install Front panel. Plug it in and turn it on for a test.
Install new Shafts and nuts. Grease shafts. Install new Rollers, washers and clips. Drape drive belt over drum while reinstalling from front. Remount drive belt over drive and idler pullies from the rear access. During this step it helps to have a helper to position the belt around the drum in correct fore/aft position, lying flat and without twists, smooth side against drum. Install front drom support. Rotate drum to seat belt before closing up. Install rear panel cover. Install Front panel. Plug it in and turn it on for a test.
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- Customer:
- Stephen from Crawfordsville, IN
- Parts Used:
- WPY312959, Y303836, WP6-3037050, WP6-3033630, WP315772, 12001541
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
Broken belt
There were two screws to remove the front of the dryer. Then 4 screws to remove the front drum support. Remove the drum. Then one nut each on changing the back drum support rollers. Assemble the drum and front support in reverse, and door front, don't forget to put the new drive belt ovre the drum. Then from the rear panel opening, one screw to change the idler assembly. Easy
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A lot of screeching noise while tumbling
It took me a lot longer to plan the repair and decide to do it than to do the actual work, knowing what I know now, and having the parts, it would take less than half an hour. As there are no repair manuals available, it took one of these reports to give me the confidence I needed to proceed.
I first found out how to open the front (only two screews on the underneath part of the front cover) and opened it to hear the noise, (just put the cover to one side while still connected to the door switch),,,,, sprayed some WD40 all over the place and the noise went away temporarily (DO NOT DO THIS as the oil will burn off on top of heater unit and smell and smoke). I replaced the roller that the drum sits on (above the heating unit) to the right of the drum and the belt. You need a special tool that fits into the little holes in the ring retainer, I got it at Lowe's ($20 +/-). It is a Channellock plier that opens when you squeeze, you have to change the points (comes with it).
So, here is the squence: remove the front panel, disconnect the swhitch (it took some pulling), set aside; remove front drum assembly (only four screws looking at you) and it comes right out; the Drum is light and comes right out as well, it just sits in a dry channel. The belt will fall off.... take the retainer ring off the roller with the special tool... remove roller and replace with new washers (one on either side) replace the ring retainer (recommend getting new one) with same tool. If you remove the small panel in the back of the washer it is very eassy to replace the belt.... I did replace it although the old one looked almost new .. instructions and a diagram come with the parts you buy here by the way... which they should say... place belt on drum per instructions (solid side down), put belt inside the chanell on drum (it will climb to the correct position by itself) put on drum front cover to hold drum in place, and then sting belt on pulley from the back of the dryer. (diagram comes with belt otherwise look at it before taking off the drum) Replace front panel (after reconnecting switch) and you are off (if you want to test without the front panel you have to touch the switch wires to each other (use tape) and do not do plugged in...
After much anxiety but not that much work the dryer runs great and is as quiet as new.... I took the parts off before ordering by the way.... the order came within three days... I am happy to have PartSelect.com .. Maytag had not clue this model even existed.... Thanks
I first found out how to open the front (only two screews on the underneath part of the front cover) and opened it to hear the noise, (just put the cover to one side while still connected to the door switch),,,,, sprayed some WD40 all over the place and the noise went away temporarily (DO NOT DO THIS as the oil will burn off on top of heater unit and smell and smoke). I replaced the roller that the drum sits on (above the heating unit) to the right of the drum and the belt. You need a special tool that fits into the little holes in the ring retainer, I got it at Lowe's ($20 +/-). It is a Channellock plier that opens when you squeeze, you have to change the points (comes with it).
So, here is the squence: remove the front panel, disconnect the swhitch (it took some pulling), set aside; remove front drum assembly (only four screws looking at you) and it comes right out; the Drum is light and comes right out as well, it just sits in a dry channel. The belt will fall off.... take the retainer ring off the roller with the special tool... remove roller and replace with new washers (one on either side) replace the ring retainer (recommend getting new one) with same tool. If you remove the small panel in the back of the washer it is very eassy to replace the belt.... I did replace it although the old one looked almost new .. instructions and a diagram come with the parts you buy here by the way... which they should say... place belt on drum per instructions (solid side down), put belt inside the chanell on drum (it will climb to the correct position by itself) put on drum front cover to hold drum in place, and then sting belt on pulley from the back of the dryer. (diagram comes with belt otherwise look at it before taking off the drum) Replace front panel (after reconnecting switch) and you are off (if you want to test without the front panel you have to touch the switch wires to each other (use tape) and do not do plugged in...
After much anxiety but not that much work the dryer runs great and is as quiet as new.... I took the parts off before ordering by the way.... the order came within three days... I am happy to have PartSelect.com .. Maytag had not clue this model even existed.... Thanks
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- Customer:
- Steve from MENDOCINO, CA
- Parts Used:
- WP307178
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Socket set
No heat
I watched Steve the repairman on u tube then opened up the front of the dryer and noticed the part in my dryer was a little different than the one on the video. So I called in and I was reassured it was what I wanted. When I got the replacement part and before I removed the old part I took pictures of the wiring noticing the wires where changed from left to right I had to make up one of the 12 gauge wires and connectors with parts from the hardware store and the new part was shorter than the old part, but the machine all ready had screw holes where I needed them. I looked at my photos and wired the new part the same way I took the wires off the old part and put it back together and it works like new! saved money! the local guy is $150 to show up and start the clock. I also fixed the blower,EASY!
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