MDE16CSAGW Maytag Dryer - Instructions
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- Customer:
- Dave from CRANBERRY TWP, PA
- Parts Used:
- WPY014874, WP33002535, 306508, 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
Noisy
This is the dryer of a 28 year old Maytag laundry pair. I had replaced the glide kit 8-10 years before. Did them again because they were worn in half again but this time I added the 2 roller kits and the belt, really just guessing. I was surprised how full of dust and lint the inside was, especially the blower fan blades. I ordered the screw because the belt idler pulley assembly was very wobbly and I hoped that was the screw anchoring it to the motor housing was the problem but it wasn't. Turns out the threaded hole in the housing was stripped, due I guess to years of vibration. It was too tight to get a tap and dye in there so I drilled the hole out and replaced the screw with a bolt and nut and lock washer. Before drilling it out I tried a few strands of wire and JB Weld, like the trick with stripped wood holes where you break off toothpicks in the hole and fill with wood glue. But that stripped out too so I drilled and used the bolt. Turned out I didn't need that $7 screw. Probably should have known comparing it to the old one which looked the same after I cleaned it. Anyway, it sounds fine again.
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Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
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- Customer:
- William from Springfield, OH
- Parts Used:
- WP6-3129480, WP312535, 12001541, WP9703438
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
One of the roller shafts was worn
Replaced both rollers,shafts, bearings and snap rings.
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- Customer:
- Tyler from Decatur, AL
- Parts Used:
- WP6-3705180, WP6-3700340
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers, Socket set, Wrench set
Horribly Squeaky Dryer
I looked up my problem online and everything I saw said to change the roller wheels that hold the barrel of the dryer. After doing that (twice, once on each side) I was still having a horrible squeaking sound so bad that we were waiting to do laundry until we were leaving for a while. Finally I determined that the problem was actually the idler wheel. All I had to do was remove the bolt holding the idler arm on (it's the arm that has a spring connected to it that moves to allow the belt on or off) and put the new arm with the new wheel on. The dryer is now whisper quiet and works perfectly.
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- Customer:
- Joe from Nashville, TN
- Parts Used:
- WP33002535, W10410997
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Socket set
Dryer made a buzzing sound when start button pushed. Would not start.
Took off front. Removed door. Removed drum support. Removed drum and belt. Made sure motor was correct size and fit. Removed blower wheel. Disconnected wire plug from motor and slid motor out of blower wheel. Replaced everything in reverse order. Figuring out belt tensioning position was a trip, but finally got it. Vacuumed out all the lint. Amazingly it worked!
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- Customer:
- Donald from Bridgewater, MA
- Parts Used:
- WP6-3705180, WPY312527, WP9703438, WP6-3700340, 12001541
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Loudly squealing dryer
Piece of cake. Use the available manual to ascertain dismantling procedure. Only thing that might be tough for average DIY'er is the internal snap rings. Snap ring pliers are mandatory for quick easy repair.
Total time was probably about 15 minutes and this was the first time I had taken it apart. Quiet as a mouse now!
Very helpful site.
Total time was probably about 15 minutes and this was the first time I had taken it apart. Quiet as a mouse now!
Very helpful site.
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- Customer:
- Chad from West Fargo, ND
- Parts Used:
- WP33001755
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Screw drivers
Dryer baffle broke when drying sneakers
I was able to quickly make this repair with the help of some instructions that I found on this site on how to remove the front panel of my dryer. 4 screws on the front around the door (and removal of the door) and then it was simply a matter of rolling the top portion out to pop it out of some clips and then the front panel opened toward me and I was able to lift it off of the metal fingers that secure it on the bottom. Removing the old baffle was a matter of removing two screws with a nutdriver and installation of the new baffle was a breeze. All in all I was done start to finish in under 10 minutes.
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- Customer:
- Tom from Crystal City, MO
- Parts Used:
- WP33001755
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
baffle broke
i removed the 2 screws holding the door hindges on. then i removed the 2 adjasent screws to remove the front door panel. i rotated the drum to aceses the screws holding the baffle and installed the baffle .
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- Customer:
- Tulio from ASHLAND, MA
- Parts Used:
- WP9703438, WP6-3700340, WP6-3129480, WP354987, WP33002535, WP33001807, 12001541
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Noisy & Drum stop working
Replaced damaged parts and recommended parts normally causing the problem. Dryer is working again like new. I expended $112 rather than $600 for a new equipment. Good deal!
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- Customer:
- Loretta E. from Miamisburg, OH
- Parts Used:
- W10169313
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Button to start dryer
Per instructions I printed off online: took off door, then the front panel. Pulled out the old switch/button, connected the new switch/button, made sure the new button was working; put the panel back on then the door and DONE!
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Squeaking noise
I had replaced belt, but the noise continued. Ordered new rollers and washer. Removed the front panel by tipping the dryer back against the wall and removing two screws at the bottom of the panel. Tipping the dryer makes it easy to remove the front panel. Removed the front drum support by removing four (4) screws. I was then able to just move the drum enough to have access to the rollers. Didn't even have to remove the belt. Replaced the rollers. Needed special pliers to remove and replace the retaining rings. Put the drum back into position and mounted the front drum support. Tightened four screws and then put the front panel back on. Plugged it in and tested it. Problem solved. Took about 35 minutes. Thanks
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- Customer:
- William from ORANGE, CA
- Parts Used:
- 306508
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Socket set
Loud squeaking noise
I removed the front of the dryer and the drum support plate. I drilled out the old rivets and installed the Glides with the enclose rivets. The Glides came loose in a few days! The holes in the glides are larger than in the old Glides. I disassembled the dryer again and reassembled with my rivets. This time I held the rivet gun inside the perimeter of the dryer so that the head of the rivet is opposite the initial installation. So far, so good, except the dryer still squeaks. The idler pulley is now the culprit. White grease burned up. I reassembled with high temperature grease. If that does not work, I will need another idler pulley. The journal looks very worn. the dryer is 30+ years old.
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- Customer:
- Chris from Truckee, CA
- Parts Used:
- WP6-3129480, 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Wrench set
worn out bearing
Unplug the dryer and pull it away from the wall so front and back can be accessed. Remove front panel. Remove front drum support. Remove rear access panel. Disengage drive belt from idler wheel. Make careful note of course of belt and which side is "outward". Remove drum through front. Remove Rollers using circlip pliers. Remove nuts behind shafts. Remove shafts. Clean-up area and parts before re-install.
Install new Shafts and nuts. Grease shafts. Install new Rollers, washers and clips. Drape drive belt over drum while reinstalling from front. Remount drive belt over drive and idler pullies from the rear access. During this step it helps to have a helper to position the belt around the drum in correct fore/aft position, lying flat and without twists, smooth side against drum. Install front drom support. Rotate drum to seat belt before closing up. Install rear panel cover. Install Front panel. Plug it in and turn it on for a test.
Install new Shafts and nuts. Grease shafts. Install new Rollers, washers and clips. Drape drive belt over drum while reinstalling from front. Remount drive belt over drive and idler pullies from the rear access. During this step it helps to have a helper to position the belt around the drum in correct fore/aft position, lying flat and without twists, smooth side against drum. Install front drom support. Rotate drum to seat belt before closing up. Install rear panel cover. Install Front panel. Plug it in and turn it on for a test.
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- Customer:
- Mitch from Ripin, CA
- Parts Used:
- WP33002535, WP6-3700340, 12001541
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
Dryer Was Making A Very Loud Screching Sound
I looked on line and found a scematic from your web site to determine how to dismantel the dryer. Once I was inside I was able to determine that the drum roller was making the noise. I decided to replace the other moving part while I was inside just in case. . . Pretty easy job
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- Customer:
- Yvonna from Mulberry Grove, IL
- Parts Used:
- W10410997
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Wrench set
motor hummed but wouldn't turn drum
Unplugged dryer and removed screws that hold door in place. removed screws that hold front panel. removed front panel. took drum belt off idler pulley. pulled drum out of dryer cabinet. unhooked wiring harness and removed motor. replaced motor and reversed steps to put back together. Thanks to partselect for getting me the parts so quickly. I ordered the motor on line on Friday and it was at my house on Saturday.
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