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MDE14PDAGW Maytag Dryer - Instructions

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All Instructions for the MDE14PDAGW
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Customer:
James from Canyon Lake, TX
Parts Used:
WP33002032
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Socket set
Baffels in Dryer came off
The YouTube video on how to replace the baffels was excellent. After watching the video, it was a piece of cake.
4 of 5 people found this instruction helpful.
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Customer:
Beverly from Oakland, MD
Parts Used:
W10410997
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers, Screw drivers
dryer would not run
Removed door and front and drum. Removed fan assembly. Be careful when working fan off of motor shaft. Unhooked wiring from motor. Removed clips. Replaced motor. Reverse procedure to put dryer back together. Now works like new. Very, very, happy. Part came in 2 days using standard shipping. Way better than buying a new dryer.
4 of 5 people found this instruction helpful.
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Customer:
Mark from Napa, CA
Parts Used:
WP303396
Difficulty Level:
Very Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Screw drivers
No Heat
Insure the double pole breaker in the breaker box is functioning properly.
5 of 8 people found this instruction helpful.
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Customer:
William from ENTERPRISE, AL
Parts Used:
WP6-3700340, WP303396, 306508, 12001541
Difficulty Level:
Really Easy
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Screw drivers
A few weeks ago our dryer stated making metal to metal sounds and about the same time stopped drying the clothes.
I looked at this website and found the symptoms, noisy, and no heat or not enough heat. I ordered the recommended parts. They were the drum support roller kit, idler pulley wheel and bearing, high limit thermostat, and lastly the front glide kit. I had anticipated having to use all of these parts. Upon following the instructions in the videos (couldn't ask for better instructions) I disassembled the dryer to see how bad everything was before replacing the parts. The left drum support roller spun easily, but had a little roughness and slight noise, the right one spun easily but not like I thought a new one would have spun, the idler pulley was stiff and very noisy. The thermostats all seemed to be in good shape (had continuity). I cleaned the bearings and shafts of all of the rollers with alcohol, paper towels and cotton swabs. The bearings and shafts all looked like new, so I lubed them with a slight amount of high temperature grease and reassembled the rollers. They moved smoothly and quietly. The fan was quite full of lint, even cleaning the filter after every load does not stop all of the lint. It has been in use probably over 10 years. After everything was back together, it runs like a well oiled sewing machine and has been drying well. I did return the parts unopened. This would not have been so successful without the videos. Thanks to all of you.
5 of 9 people found this instruction helpful.
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Customer:
Janel from BOWDLE, SD
Parts Used:
WP6-3700340, WP6-3129480, WP33002535, WP33001807, 306508, 12001541
Difficulty Level:
A Bit Difficult
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers, Socket set, Wrench set
Dryer started to sound like someone was beating a dog in the laundry room.
The dryer model was on a sticker inside the door which had long ago rubbed off. The most difficult part was figuring our how to dismantle the dryer. I finally looked up the matching washer by model number watched a youtube video and the dismantle was the same....take off the door, remove front cover then remove screws that held the hook brackets that held the top down. After we figured that out the rest was pretty easy. The main issue was the Idler Pulley Wheel and Bearing. We decided to replace the rest of the parts because we already had the thing all apart. It is amazing all the lint that gets into the dryer cabinet and passed the lint filter. Dryer works like new again. I love this set and will keep repairing as long as we can get parts.
3 of 3 people found this instruction helpful.
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Customer:
Alan from BETHESDA, MD
Parts Used:
WPY014874, WP315772
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
3 of 3 people found this instruction helpful.
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Customer:
Dave from CRANBERRY TWP, PA
Parts Used:
WPY014874, WP33002535, 306508, 12001541
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Pliers, Screw drivers, Socket set
Noisy
This is the dryer of a 28 year old Maytag laundry pair. I had replaced the glide kit 8-10 years before. Did them again because they were worn in half again but this time I added the 2 roller kits and the belt, really just guessing. I was surprised how full of dust and lint the inside was, especially the blower fan blades. I ordered the screw because the belt idler pulley assembly was very wobbly and I hoped that was the screw anchoring it to the motor housing was the problem but it wasn't. Turns out the threaded hole in the housing was stripped, due I guess to years of vibration. It was too tight to get a tap and dye in there so I drilled the hole out and replaced the screw with a bolt and nut and lock washer. Before drilling it out I tried a few strands of wire and JB Weld, like the trick with stripped wood holes where you break off toothpicks in the hole and fill with wood glue. But that stripped out too so I drilled and used the bolt. Turned out I didn't need that $7 screw. Probably should have known comparing it to the old one which looked the same after I cleaned it. Anyway, it sounds fine again.
3 of 3 people found this instruction helpful.
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Customer:
Kim from Jacksonville, FL
Parts Used:
WP33002032
Difficulty Level:
A Bit Difficult
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Socket set
End of one baffle pulled away from drum
Following the instructions I pulled off the door and front panel. After rotating drum so the broken baffle was at the bottom I used a socket to remove the two screws on either end. I removed the broken baffle and inserted the new baffle in its place. Reinserted the screws, front panel, and door. I do strongly suggest having the manual handy to view the steps. It's available in PDF format.
3 of 3 people found this instruction helpful.
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Customer:
Warner from Troy, OH
Parts Used:
WP6-3705180, WP6-3700340, WP33002535
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Wrench (Adjustable)
Dryer was making a loud sueaking sound.
On my maytag dryer I took the door off with two screws, took the front panel off with four srcews, lifted the top panel up a little bit and removed the belt from the "tub" and pulled the tub out. I could easily then access the idler arm and pulley wheel. Due to the age of the dryer, I also replaced the tub belt while it was apart. Reversed the process to put it back together, alot easier than I thought.

Warner
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Customer:
David from Calvert City, KY
Parts Used:
WP6-3129480, 12001541
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers, Wrench set
drum support roller had come apst from bearing and was making a squealing noise when dryer was running
first i removed the screws holding back cover. Then I remeved nut from tumbler roller shaft. Then I slid shaft from roller .I removed roller then replaced with new one. Installed new shaft then replaced back cover. recieved parts from parts direct very promptly & they were the right parts the first time thanks very much
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Customer:
KARL from NAMPA, ID
Parts Used:
WP6-3700340, WP6-3129480, 12001541
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Pliers, Screw drivers, Wrench set
Squeeking drum
Went smoothly. Took the opportunity to vacuum out entire cabinet. Also removed tumbler vanes inside dryer as coins had made their way into them. The only other suggestion I have is that I didn't notice cabinet screws were different lengths till I started reassembly. Might be smart to label and separate them
5 of 9 people found this instruction helpful.
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Customer:
Shane from Heber City, UT
Parts Used:
WP6-3700340
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers, Wrench set
belt tensioner pulley seized to shaft
At first I thought I could just replace the pulley, but on closer inspection I found that the pulley had become seized on the shaft. I ended up removing the entire bracket (which I should have purchased also) and cutting the shaft off. I manufactured a new shaft from a bolt of the appropriate size and tack welded it to the bracket. It took a little more time than I anticipated. My advice to anyone doing this would be to spend a little extra money and buy the entire bracket and pulley. That would make this about a 15 minute job.
3 of 3 people found this instruction helpful.
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Customer:
BRIAN from FAIRVIEW PARK, OH
Parts Used:
33001750
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers
Seal torn on inner door panel
Took out old inner door panel, replaced it with the new. Had to take out 6 screws, remove old panel, put in new panel and replaced the screws..............pretty easy.
4 of 6 people found this instruction helpful.
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Customer:
Doyce from PENSACOLA, FL
Parts Used:
WP6-3700340, WP6-3129480, WP33002535, 12001541
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers, Socket set
Loud squealing noise
Disassembled dryer and replaced drum support roller and shaft. That took care of the noise but I still replaced the belt and idler pulley while I had it apart.
5 of 9 people found this instruction helpful.
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Customer:
Brian from CASCADE, CO
Parts Used:
WP33001755
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers
Broken short baffle
Removed door, then brackets holding top panel to side exposed after removing door. Lifted top panel to expose dryer chamber. Rotated chamber to access outside screws holding broken baffle. Removed and replaced baffle. Closed top lid, reattached to side. Replaced door. When reattaching top lid, do not tighten H/W just yet. You'll have to maneuver the hooks into place for the door to reattach. Then tighten when in place.
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All Instructions for the MDE14PDAGW
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