LSE7804ADM Maytag Washer Dryer Combo - Instructions
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- Customer:
- Charles from Raymond, NH
- Parts Used:
- W10411000
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Tub would not turn Dryer would heat up but did not spin.
First I shut off the power at the breaker. I removed the two screws on top holding the front panel in place I removed the wires carfully marking so they would go back in the correct places. I removed the tub and then removed the old motor and switching the wires to the new one. Mounted the new motor, replaced the tub with the belt, attached the belt to the motor. connected the marked wires and put the front cover back in place with the two screws on top of machine. Turned the power back on and started it up it works perfect The motor only cost $119.00 and a little of my time much better than getting a new machine as it is a stack washer dryer.
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- Customer:
- John from Warsaw, IL
- Parts Used:
- W10169313
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Door safety switch would not close keeping dryer from running
Shut off or unplugged dryer for safety.
Slipped thin blade putty knife up under bezel of switch to unlatch from the panel and pulled forward to remove the swwitch from the dryer. Unplugged the quick connect terminals (3) from the old switch and plugged them onto the new switch. one of the terminals had gotten quite hot and darkened the insulation so it was replaced with one that was supplied with the switch. that was a cut, strip, crimp process. Placed the new switch into the panel and snapped into place.
Slipped thin blade putty knife up under bezel of switch to unlatch from the panel and pulled forward to remove the swwitch from the dryer. Unplugged the quick connect terminals (3) from the old switch and plugged them onto the new switch. one of the terminals had gotten quite hot and darkened the insulation so it was replaced with one that was supplied with the switch. that was a cut, strip, crimp process. Placed the new switch into the panel and snapped into place.
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- Customer:
- richard from pleasant valley, NY
- Parts Used:
- W10169313
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
door switch broke
remove bottom section under door 2 screws remove door 2 screws remove switch by squeezing tabs install 2 new female ends on wires supplied with switch . put switch back in plug in wires .
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lid closing to far bumpers missing and fuse block cracked
unhooked power plug removed 2 top screws tilted topfront panel back removed cracked fuse holder replaced with new fuse holder put top cover back on installed 2 top screws plugged in power cord done!
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- Customer:
- Donnie from Spring, TX
- Parts Used:
- WP22001274
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Pliers
The water to the washing machine continued to run into the unit when it was supposed cut off. It continue to fill overflowing the tub of the washing machine and onto the floor. The water had to be cut off at the wall in order to stop the inflow of water.
I disconnected both water hoses from the back of the machine. I then unscrewed the panel that holds the water inlet valve. After disconnecting the two electrical connections from the valve and replacing it with the new unit, the job was done.
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- Customer:
- Efrain from Fontana, CA
- Parts Used:
- 206638
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers, Wrench (Adjustable)
water leak during spin cycle
First removed the two lower screws from the front panel. I then unscrewed two screws holding the top(lid) of washing machine. I then lifted the lid and let it rest on its rear hinges. The syphon is removed by unscrewing four screws from the rear of the washer. I then cut the original clamp holding the syphon to the hose. New syphon was installed. Enclosed hose clamp was used to tighten around hose. Syphon was then then screwed back to the rear wall of the machine. Easy fix. Water leak solved.
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- Customer:
- RAFAEL from CENTERVILLE, GA
- Parts Used:
- WP207166
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Burned out part
Good.
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- Customer:
- Henry from Southside, AL
- Parts Used:
- WP22001187, WP22001186
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
Upper and lower filler injectors broken
Power cord out, of course.Popped off the front panel, swinging bottom outward. Wedge shaped protrusions on top of front panel work as a hinge until the bottom is swung out and the entire front lowered. Unscrewed the top--one screw in each front corner accessed from the front opening (removed panel). Panel behind control panel must be removed (5 hex head screws). Tilted front of top up revealing broken injector. Retaining screw for injector accessible from behind control panel loosened and broken injector assembly removed. New (easily assembled--snap together) injector slid into holding slot on one side and screwed down with previously removed hex screw. Reassemble in reverse.
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- Customer:
- ROBERT from MORGAN CITY, LA
- Parts Used:
- WPY312959, WPY312901, WP33001003, WP314820, 306508
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Socket set, Wrench set
black marks on whites and dark
The repair went better then I thought it would go.
the seals went on just fine
the seals went on just fine
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- Customer:
- tina from north bennington, VT
- Parts Used:
- WP213045
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Water was leaking from under washer
Frist remover the two screws from washer front. The ones that are about 5 inches from the floor. Pulled front cover toward me and removed. The hose was right in the front that was cracked. It was held on by two hose clamps. I just removed the old and put in the new. No more water on the floor. Shipping was fast for the hose too. They said that if they recieved the order by 3pm it would be shipped the same day. I order at 3:01pm Sat. recieved Tuesday.
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- Customer:
- Robert from Finland, MN
- Parts Used:
- WPY312959
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Broken drum belt
I pulled the face of the dry off by removing the two screws on the lower face below the door. I pulled the drum out by removing the two bolts holding the drum mounts to the frame. I put the new belt around the drum and remounted it. The access hole on the lower right corner on the back of the appliance allowed me to turn the drum to align the belt (and turn it right side up) with the pulley. It took a moment to figure out how to re-thread the pulley but was able to do it after only a couple of tries. All in all it was quite easy!
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- Customer:
- Hazel from CONNERSVILLE, IN
- Parts Used:
- 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
noisy
I watched the video
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Very old washer was leaking oil and grease drops into the wash water.
Followed the procedures recommended for replacement of all the parts included in the Tub Bearing Kit and the Mounting Stem/Tub Seal kit as illustrated in a detailed, 32 minute repair video for the Maytag A606 washer which is available on YouTube. Many difficulties were experienced in the disassembly procedures due to extensive corrosion of tub bearing and tub stem parts (the washer is 47 years old).
I was not successful in using a special tub wrench that was purchased to break loose the old tub mounting stem and its threaded lock nut. The old tub mounting stem, lock nut, and the tub bearing race had to be cut off the threaded support shaft using a saws-all electric tool. Finally, corrosion on the edge of the tub caused problems with water leaks once the tub top and its rubber tub seal ring were reinstalled and the washer was put back into operation. The bottom line is that it may be questionable to attempt major repairs on washers that are 40+ years old and have any extensive corrosion in internal, mechanical parts.
I was not successful in using a special tub wrench that was purchased to break loose the old tub mounting stem and its threaded lock nut. The old tub mounting stem, lock nut, and the tub bearing race had to be cut off the threaded support shaft using a saws-all electric tool. Finally, corrosion on the edge of the tub caused problems with water leaks once the tub top and its rubber tub seal ring were reinstalled and the washer was put back into operation. The bottom line is that it may be questionable to attempt major repairs on washers that are 40+ years old and have any extensive corrosion in internal, mechanical parts.
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- Customer:
- Howard from ALBRIGHT, WV
- Parts Used:
- WP6-2022030
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver
The old pump was beginning to drag due to the age of the washer.
Removed the front panel. Then blocked up the front of the machine. Removed the pump belt. Removed the 3 5/16" screws from the bottom of the old one and tilted it slightly to remove. Put the new one in and reinstalled the 3 screws. Put the belt back on and slid new pump all the way to the right and tightened 1 screw. Loosened the screw until there was about 1/4" of gap when squeezed the belt together. Tightened the one screw, then the other 2. Put the front panel back on and lowered the machine. New pump works great.
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- Customer:
- Russell from ELK GROVE, CA
- Parts Used:
- Y303836
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
Noisy Dryer operation and eventually no air movement through dryer
Every two to three years, the blower wheel gets chewed out in the center where it attaches to the motor shaft. I have learned the sound of it starting to rattle so I know to order a new blower before the air stops moving altogether. Replacing it is very easy if you have tiny sockets or nut drivers and a pair of snap ring pliers.
When working on this dryer, be aware that the heater wires are always "hot", even when the dryer is not running. You are only likely to touch one at a time so the worst you will feel is 120 volts. The shock probably won't hurt you but you may cut yourself jerking your arm out of the dryer. Best to unplug the dryer or open the circuit breaker before sticking your arm in there!
When working on this dryer, be aware that the heater wires are always "hot", even when the dryer is not running. You are only likely to touch one at a time so the worst you will feel is 120 volts. The shock probably won't hurt you but you may cut yourself jerking your arm out of the dryer. Best to unplug the dryer or open the circuit breaker before sticking your arm in there!
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