LSE9900ACL Maytag Washer Dryer Combo - Instructions
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- Customer:
- Larry from Chippewa Lake, OH
- Parts Used:
- WPW10116738
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver
broken siphon elbow
I thought it was going to be next to impossible to find a replacement part for an older washer. So my first attempt was to try to epoxy the original part, but the epoxy didn't hold up to the stress. I began thinking about what I might need to make a replacement part which was possible but not very practical. Although I dreaded trying to find this part online, I was very surprised and elated to happen upon PartSelect! Oh, by the way, this washer belongs to my daughter and I nave tossed the paper I wrote the model number on, so the model number was entered as the part number, sorry. At any rate, the the part was reasonable priced, and shipping about standard, but I still saved a lot by doing it myself rather than having a repair person for something this simple. Partselect online lookup made it easy to find the model and drawings to help me find the correct part nomenclature. AND, the part was in stock! So I am pleased with how this venture worked out.
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- Customer:
- Wesley from Tulsa, OK
- Parts Used:
- WP6-3037050, WPY312959, Y303836, 306508, 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Trying to install the drum belt by reaching in from the front over the top of the blower & motor.
I observed that the top of the dryer was affixed by two screws at each front corner. With these removed the top of the dryer could be easily lifted and with the front support panel removed the drum, drive motor and idler pulley could be accessed. This allowed the installation of a new drum belt in a short period of time. Installing the belt from the front lower left hand side proved very difficult for me but with the top raised and coming in from the top it was accomplished in short order. Thank you, Wesley Harmon
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- Customer:
- William from Placerville, CA
- Parts Used:
- WP306199
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers, Wrench set
Dryer stopped heating up.
Dryer stopped heating after a few days of it being an intermintant problem. I ohmed the heating coil and it was fine @ 12-15 ohms and the 2 sensors were open so I knew they were not the problem. The only item left was the Heater Relay. As soon as it was changed, dryer operated as it should.
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- Customer:
- Charles from Raymond, NH
- Parts Used:
- W10411000
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Tub would not turn Dryer would heat up but did not spin.
First I shut off the power at the breaker. I removed the two screws on top holding the front panel in place I removed the wires carfully marking so they would go back in the correct places. I removed the tub and then removed the old motor and switching the wires to the new one. Mounted the new motor, replaced the tub with the belt, attached the belt to the motor. connected the marked wires and put the front cover back in place with the two screws on top of machine. Turned the power back on and started it up it works perfect The motor only cost $119.00 and a little of my time much better than getting a new machine as it is a stack washer dryer.
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- Customer:
- JACLYN from RICE LAKE, WI
- Parts Used:
- 6-2095720
- Difficulty Level:
- Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers, Socket set, Wrench set
Washer Leaked Water From Bottom Seal
Removed washer tubs inner and outer nut (part # 10 ) on inner was hard to remove and is a reverse thread used hammer to loosen once off removed 1st tub - then removed set screw #17 and then unscrewed mounting s item #29 this again required some hammer tapping to loosen - once off used flat head screwdriver to pry & remove the rubber piece on bottom of outer or 2nd tub -but keep going as the leak will probably be from part #20 tub bearing ( this will save you the time to test and find out it still leaks and have to take apart again after only replacing #29 removed 3 bolts holding tub - disconnected hoses and removed 2nd tub - used rubber hammer to knock out and install #20 tub bearing - reasembled and wow no leaks to cost about $120 - time worked on 3 hrs - only because took apart 2 times - down time on washer 10 days as we didn't order all parts to start with no beer needed but did enjoy a nice red wine - good luck
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- Customer:
- richard from pleasant valley, NY
- Parts Used:
- W10169313
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
door switch broke
remove bottom section under door 2 screws remove door 2 screws remove switch by squeezing tabs install 2 new female ends on wires supplied with switch . put switch back in plug in wires .
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- Customer:
- John from Warsaw, IL
- Parts Used:
- W10169313
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Door safety switch would not close keeping dryer from running
Shut off or unplugged dryer for safety.
Slipped thin blade putty knife up under bezel of switch to unlatch from the panel and pulled forward to remove the swwitch from the dryer. Unplugged the quick connect terminals (3) from the old switch and plugged them onto the new switch. one of the terminals had gotten quite hot and darkened the insulation so it was replaced with one that was supplied with the switch. that was a cut, strip, crimp process. Placed the new switch into the panel and snapped into place.
Slipped thin blade putty knife up under bezel of switch to unlatch from the panel and pulled forward to remove the swwitch from the dryer. Unplugged the quick connect terminals (3) from the old switch and plugged them onto the new switch. one of the terminals had gotten quite hot and darkened the insulation so it was replaced with one that was supplied with the switch. that was a cut, strip, crimp process. Placed the new switch into the panel and snapped into place.
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Dryer wouldn't start - 7E code on display
Found error code list on internet. stated that the 7E code was a faulty Thermistor or a few other possibilities. also found instructions to test Thermistor and clear error code. unplugged dryer plug to reset error. removed panel to access thermistor on blower duct, started dryer and ran until 7E error reappeared. removed one wire from thermister and using a volt/ohm meter. checked the resistence through the two post of thermister.
should read between 100-50 ohm. 100ohm=room temp and 50ohm=180 degree F (approx) replaced with new Thermister and problem solved.
should read between 100-50 ohm. 100ohm=room temp and 50ohm=180 degree F (approx) replaced with new Thermister and problem solved.
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Washer was leaking a lot of water
This repair started because I wanted to clean the lint build up out the exhaust vent. But when I moved the washer out, the tile floor was buckled from water damage. So I removed the old tiles and coated the cement with waterproof paint and sealed the seams of the baseboards. Then before reinstalling the washer I had to locate the water leak. I looked at the water inlets and the faucets and saw (and felt) nothing wet. Then I started the wash cycle and looked for the drips. I found them on the left side coming from under the unit. I removed the water inlet plumbing (two screws hold it in place) from the back of the washer but there was no leak. Finally I removed the front panel and could see water running down the side and coming from near the top of the machine. This was right behind the water inlet unit and I thought that one of the hoses was leaking. To get to that area I then removed the top casing and found the injector port was leaking, not the hoses. To remove the front panel I had to take out two screws at the bottom of the panel. To remove the top I had to remove 4 screws...the two rear screws were easily accessible but the two front screws were inside the unit and the one on the left had restricted access because of the electrical unit installed there. After the replacement parts arrived it was relatively easy to remove the front and top again to gain access to the injector port. I removed the old nozzle and valve and installed the new parts. Then I started a wash cycle to check that the leak was fixed. The water did not leak so the repair was successful.
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Broken belt
It was as simple as leaning the machine back far enough so I could get to the belts - which were on the bottom. The diagrams that came with the ordered parts were right on. This is the first time I have attempted this myself - my repairman has retired - I'm sure I will do it again.
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- Customer:
- karl from monroe, GA
- Parts Used:
- 306436
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Dryer would not stay closed.
I used a flat screw driver to pop out the old female portion and snapped in the new one. Dryer stays shut. That's it!
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- Customer:
- Hazel from CONNERSVILLE, IN
- Parts Used:
- 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
noisy
I watched the video
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Very old washer was leaking oil and grease drops into the wash water.
Followed the procedures recommended for replacement of all the parts included in the Tub Bearing Kit and the Mounting Stem/Tub Seal kit as illustrated in a detailed, 32 minute repair video for the Maytag A606 washer which is available on YouTube. Many difficulties were experienced in the disassembly procedures due to extensive corrosion of tub bearing and tub stem parts (the washer is 47 years old).
I was not successful in using a special tub wrench that was purchased to break loose the old tub mounting stem and its threaded lock nut. The old tub mounting stem, lock nut, and the tub bearing race had to be cut off the threaded support shaft using a saws-all electric tool. Finally, corrosion on the edge of the tub caused problems with water leaks once the tub top and its rubber tub seal ring were reinstalled and the washer was put back into operation. The bottom line is that it may be questionable to attempt major repairs on washers that are 40+ years old and have any extensive corrosion in internal, mechanical parts.
I was not successful in using a special tub wrench that was purchased to break loose the old tub mounting stem and its threaded lock nut. The old tub mounting stem, lock nut, and the tub bearing race had to be cut off the threaded support shaft using a saws-all electric tool. Finally, corrosion on the edge of the tub caused problems with water leaks once the tub top and its rubber tub seal ring were reinstalled and the washer was put back into operation. The bottom line is that it may be questionable to attempt major repairs on washers that are 40+ years old and have any extensive corrosion in internal, mechanical parts.
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Water leak coming from rear, left side of washing machine.
Removed front access panel--very easy, two screws at bottom of panel, near the floor. Removed two more hex-headed screws that secure the top panel/lid to the top of the washing machine frame.
Most difficult problem was identifying the source of the leak. I saw water running out of a white, rectangular (about 1" x 3/4" x 3/4") box-like device that was installed in the water line that leads from the mixing valve (blue box, mounted at the back of washer) to the top of the tub. Discovered this device is called the injector assembly, have not yet been able to figure out what function it serves.
Disconnected one of the hose clamps that secure the injector assembly to the water hose. Removed the rubber injector valve and injector nozzle, the two parts that fit inside the above-described "box." Soaked the assembly "box" in vinegar to eliminate hard-water deposits. Replaced the two internal parts (injector nozzle & injector valve) with new (about $15, including shipping). This almost resolved the problem, still saw a small amount of water leaking from the whole assembly, but only about 5% of what was leaking. Haven't yet figured out why it's not completely dry, or what function that injector assembly serves.
Most difficult problem was identifying the source of the leak. I saw water running out of a white, rectangular (about 1" x 3/4" x 3/4") box-like device that was installed in the water line that leads from the mixing valve (blue box, mounted at the back of washer) to the top of the tub. Discovered this device is called the injector assembly, have not yet been able to figure out what function it serves.
Disconnected one of the hose clamps that secure the injector assembly to the water hose. Removed the rubber injector valve and injector nozzle, the two parts that fit inside the above-described "box." Soaked the assembly "box" in vinegar to eliminate hard-water deposits. Replaced the two internal parts (injector nozzle & injector valve) with new (about $15, including shipping). This almost resolved the problem, still saw a small amount of water leaking from the whole assembly, but only about 5% of what was leaking. Haven't yet figured out why it's not completely dry, or what function that injector assembly serves.
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- Customer:
- Russell from ELK GROVE, CA
- Parts Used:
- Y303836
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
Noisy Dryer operation and eventually no air movement through dryer
Every two to three years, the blower wheel gets chewed out in the center where it attaches to the motor shaft. I have learned the sound of it starting to rattle so I know to order a new blower before the air stops moving altogether. Replacing it is very easy if you have tiny sockets or nut drivers and a pair of snap ring pliers.
When working on this dryer, be aware that the heater wires are always "hot", even when the dryer is not running. You are only likely to touch one at a time so the worst you will feel is 120 volts. The shock probably won't hurt you but you may cut yourself jerking your arm out of the dryer. Best to unplug the dryer or open the circuit breaker before sticking your arm in there!
When working on this dryer, be aware that the heater wires are always "hot", even when the dryer is not running. You are only likely to touch one at a time so the worst you will feel is 120 volts. The shock probably won't hurt you but you may cut yourself jerking your arm out of the dryer. Best to unplug the dryer or open the circuit breaker before sticking your arm in there!
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