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LDE9900 Maytag Dryer - Instructions

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All Instructions for the LDE9900
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Customer:
Gary from Liberty, MO
Parts Used:
Y303836
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Screw drivers, Socket set
Blower noisy no air flow.
I did it the hard way from the back by removing the motor. The easy way is from the front. From the front there are 2 screws about 5 inches above the floor. Also, remove the 4 screws in the tumbler behind the lent filter. Swing out the front panel from the bottom and it will release at the top. Remove 2 screws on left and right side of the front tumbler cover. It will come out now and you can get to the blower wheel which in my case was just spinning on the motor shaft.
5 of 6 people found this instruction helpful.
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Customer:
Eileen from Hillsborough, NJ
Parts Used:
WPY312959, 306508
Difficulty Level:
Really Easy
Total Repair Time:
1- 2 hours
Tools:
Screw drivers, Socket set
loud noise from dryer
Removed the front panel by removing two front screws. Removed screws from front panel holding tumbler drum. Cleaned interior with a vacuum cleaner. (dryer is at least 16 years old). Removed what was left of rivets on damaged glides with a drill, and cleaned area well. Attached new glides with rivet gun, and also applied glue to make glide and cork more secure. Replaced belts, and decided to reverse drum due to damage to drum from allowing glides to deteriorate to the point of putting scratches on the drum itself, allowing the new glides to rest on drum where there was no damage at all. This process was easy, and fast. We did make one error however, in not noticing that with our model, that there were TWO glides to be replaced. Luckily a local repair shop had one more glide so the job could be done the same day. The dryer sounds like it did when it was brand new. Very quiet! The comments from other home repairs helped very much in clairifying any possible errors. Fast delivery of parts, and the extra help was great. Thanks!
5 of 6 people found this instruction helpful.
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Customer:
anthony from alexandria, VA
Parts Used:
WPY312959
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Screw drivers, Socket set, Wrench (Adjustable)
Tumbler will not rotate...dryer is heating
If I had waited until I reviewed the pack-up date that came with the part, the disassembly would have gone much faster. The part arrived in record time, several days before anticipated. Outstanding website, parts and repair experience!
5 of 6 people found this instruction helpful.
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Customer:
William from ORANGEBURG, SC
Parts Used:
WPY312959, WPY312527, WP6-3037050, WP6-3033630, WP315772
Difficulty Level:
A Bit Difficult
Total Repair Time:
30 - 60 mins
Tools:
Screw drivers, Socket set
old was belt stretched and idler pulley gummed up, drum won't tumble a normal sized load
Replaced all the parts per the very good video provided on the website.
I recommend watching the video very closely several times. BE SURE THE BELT IS NOT IN THE DRUM'S GROOVE. The video mentions this very very briefly; I caught it on my third viewing. If your belt is not the correct location, it may still turn the drum for you - and eat the belt up in about an hour.
4 of 4 people found this instruction helpful.
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Customer:
Robert from Fort Worth, TX
Parts Used:
WPY312959, WPY312527, WP6-3037050, 12001541
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Pliers, Screw drivers
Dryer tumbler belt broke.
I followed the videos on your website, but had to clean 30 years of dust and lint out in the process. Cleaning took the longest time.
6 of 10 people found this instruction helpful.
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Customer:
Fred from Columbia Falls, MT
Parts Used:
WPY312959, WP6-3037050, WP314820, 306508, 12001541
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
very noisy, not working properly
Took it apart according to the videos, replaced about all moving parts (almost). Put it back together and still made noise. It turned out to be the blower wheel. Ordered a new blower wheel and installed it. Works great and has mostly all new parts. The website was great!!
4 of 4 people found this instruction helpful.
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Customer:
Mark from Noblesville, IN
Parts Used:
Y303778
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers, Screw drivers
No heat in the dryer
This is super easy:

Just take out two screws on the front panel and drop the front panel off the dryer.

Then pull the wires off the heater assembly and remove (1 screw).

Move the heat fuse and heat sensor to the new heater.

Put the new heater in, plug in wires, pop front back on and, wow, that was easy!

Less than 30 min and I am a business sales guy, not an appliance repairman.
4 of 4 people found this instruction helpful.
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Customer:
jim from sierra vista, AZ
Parts Used:
Y303836
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Screw drivers
Blower fan came loose and broke
No manual on this so had to remove about 12 screws to figger out disassembly,after locating the right ones[front]the job was easy.Remove front plate,remove drum bearing,remove blower front cover,remove snap ring,remove broken fan,clean fan shaft,slide new fan onto shaft[there is a flat in the bore of new fan]instal fan retainer on stub of fan,reinstal snap ring,reinstal the rest of the parts,test drive system[all sat]The part was exactly as ordered,thanks,Jim Thompson
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Customer:
Francis from Half Moon Bay, CA
Parts Used:
WPY312959, Y303945
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Screw drivers, Socket set
Loud, rumbling noise
1. Removed two screws from front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
5 of 8 people found this instruction helpful.
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Customer:
Mark from Napa, CA
Parts Used:
WP303396
Difficulty Level:
Very Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Screw drivers
No Heat
Insure the double pole breaker in the breaker box is functioning properly.
5 of 8 people found this instruction helpful.
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Customer:
William from Winter Park, FL
Parts Used:
WP6-3037050
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers, Screw drivers
Squealing noise on start up.
I opened the back acess panel and started the dryer. Looking at the motor and idler pulleys it was obvious by the frequency of the squealing noise that it was coming from the idler pulley.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
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Customer:
Anthony from New Port Richey, FL
Parts Used:
307208
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers, Screw drivers
Dryer would over heat,temp uncontrolable
The repair was very simple.I removed the door and the front cover.Right in front of the blower housing sat the temperature control thermistor.All that was needed to do the swap was a nut driver.Everything I read said the high limit thermostat may of been bad but it was fine.Ordering the parts was easy and fast all I needed was the model number and all the charts and numbers were easy to find.Thank you Parts select..
7 of 14 people found this instruction helpful.
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Customer:
Gale F. from Atlanta, GA
Parts Used:
33001167
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Needed a replacement lint filter.
I pulled out the old filter, the screen of which had ripped, and put in the new one...It took a few seconds! Mainly I was delighted that from the online photo guide I had chosed correctly!

Glad your site exists! It prolongs the life of older but functional equipment.
5 of 8 people found this instruction helpful.
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Customer:
Alan from BETHESDA, MD
Parts Used:
WPY312527, WP6-3037050, WP6-3033630
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
After a period of the dryer not being used, the idler pulley wheel froze up on the shaft of the idler pulley arm.
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
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Customer:
Alan from BETHESDA, MD
Parts Used:
WPY014874, WP315772
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
3 of 3 people found this instruction helpful.
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All Instructions for the LDE9900
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