Models > DG408 > Instructions

DG408 Maytag Dryer - Instructions

Jump to:

All Instructions for the DG408
106 - 120 of 1079
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
Customer:
Alan from BETHESDA, MD
Parts Used:
WPY312527, WP6-3037050, WP6-3033630
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
After a period of the dryer not being used, the idler pulley wheel froze up on the shaft of the idler pulley arm.
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
3 of 3 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Alan from BETHESDA, MD
Parts Used:
WPY014874, WP315772
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
3 of 3 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Bill from Frisco, TX
Parts Used:
WP33001003, 306508
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Nutdriver, Screw drivers
Slide Was Worn Down To Bare Metal
Took the front off , removed front drum support, drilled out existing rivets, & replaced slides,riveted them in place,and re-assembled.
4 of 6 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Stephen from Lilburn, GA
Parts Used:
WP338906, WP4392003
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Socket set
No heat in dryer. Gas would not come on.
Replaced the flame sensor and the igniter. Probably didn’t need the igniter but put in anyway. Saved old igniter for a later time just in case it burns out.
3 of 3 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Conrad from CHESAPEAKE, VA
Parts Used:
W10169313
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers
Dryer No longer shuts off When Door Opened
All you need for a Maytag is a snub nose Philips screw driver. The screws on the front panel are at the bottom angled down, so a regular length Phillip's won't work. Just unscrew the 2 screws, then lift the panel up and out. Careful not to pull out too far, there are 2 wires attached to the switch. The replacement switch is NOT an exact copy of the old one. My Maytag is over 30 years old and it only had 2 prongs on the switch. The new one has 3. Don't let that throw you. It is the same size. Just attach, 1 wire to the bronze connector & the other to the silver. Push the switch into the door opening, re-attach the door. Total time 20 minutes. Saved well over $100 in a service call. Anyone with an IQ above freezing can do it.
3 of 3 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Joseph from Colts Neck, NJ
Parts Used:
W10169313
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers
Replaced door switch
Door switch was very easy to replace as it simply snaps in for the outside and you just clip on the two control wires that already have clips on them.
5 of 9 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
William from Fullerton, CA
Parts Used:
WP33001003, 306436
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Dryer door would not stay closed
1. Popped out old latch from dryer with a screw driver and pressed in new latch with fingers. Did not need to replace the part that is in the door. Very simple repair.
2. Lint filter was worn out and needed replacing.
4 of 6 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Jeffrey from Glenshaw, PA
Parts Used:
4391996
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Wrench (Adjustable)
Dryer not heating....Had to be igniter or solonoid
Upon receipt of part, just loosened 1 fastener, slid igniter forward and out....unclipped wire connection and replaced... Could not have been easier. Be careful not to overtighten fastener when replacing. Description and pictures made for very easy selection.
3 of 4 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
David from Manhattan, IL
Parts Used:
MAL9000AXX
Difficulty Level:
A Bit Difficult
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Switch Samsung dryer (w/ Maytag gas valve) to LP
The directions provided to modify the gas valve were very clear. Getting to the gas valve I was on my own. Taking the top and the face off the dryer, once I figured out that there was no reaching the gas valve from any of the access ports on the back, was the only way to access to the gas valve. If you have worked on any other dryers, this modification was definitely doable.
4 of 7 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
William from Springfield, OH
Parts Used:
WP6-3129480, WP312535, 12001541, WP9703438
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Screw drivers
One of the roller shafts was worn
Replaced both rollers,shafts, bearings and snap rings.
3 of 4 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Dan from Downieville, CA
Parts Used:
WP338906, WP303395
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Screw drivers, Wrench set
Na
Graet
3 of 4 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
David from Lower Burrell, PA
Parts Used:
306207
Difficulty Level:
A Bit Difficult
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers
electric dryer had no heat
I removed the cover from the control panel, took out the schematic, removed the rear cover by the motor, followed the schematic, powered the heater by taking the blue hot leg wire off the right side of the switch and touching it to the black lead for the heater on the left side, and I could hear the heater power on. Since bypassing the motor start switch powered the heater, I ordered the part. When it came, I installed it in about 5 minutes and the dryer worked perfectly.
3 of 4 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Stephen from Port Jefferson, NY
Parts Used:
WPY312959, WP33001003, 306508
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Screw drivers, Socket set, Wrench set
Squealling clothes dryer.
Undid two screws in lower front of dryer and popped off front. Removed screws holding lint screen duct and brackets supporting tumbler and removed duct and tumbler quite easily. Pulled, cleaned and oiled rear rollers, replaced front glides, and thoroughly cleaned exhaust duct of lint. Put new belt into position on the roller before sliding tumbler back in, then pulled belt over tumbler as it went in. Be careful to follow belt path directions correctly.
Key to this repair was obtaining the parts so easily from Parts Select.com. Ordered at 2pm and had them 2pm the following day. Unbelievable! These machines are relatively simple to keep running when the parts are available so easily. Thanks for great service.
3 of 4 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Charles from Daphne, AL
Parts Used:
WP312535, 12001541, WP9703438
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Pliers, Screw drivers, Socket set
Squeaking noise
I had replaced belt, but the noise continued. Ordered new rollers and washer. Removed the front panel by tipping the dryer back against the wall and removing two screws at the bottom of the panel. Tipping the dryer makes it easy to remove the front panel. Removed the front drum support by removing four (4) screws. I was then able to just move the drum enough to have access to the rollers. Didn't even have to remove the belt. Replaced the rollers. Needed special pliers to remove and replace the retaining rings. Put the drum back into position and mounted the front drum support. Tightened four screws and then put the front panel back on. Plugged it in and tested it. Problem solved. Took about 35 minutes. Thanks
3 of 4 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Horacio from Houston, TX
Parts Used:
4391996
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Socket set, Wrench set
Not enough heating to dry clothes.
My Maytag gas dryer model MDG7600AWW is about 12 years old. Everything else works fine except it takes 4-5 drying cycles instead of 1 to completely dry my clothes properly. The flat igniter was simply cracked but not broken so it only worked some times. My gas dryer igniter and the 2 ignition coils work hand in hand so I replaced all 3 parts. The ignition coils provide a solid and consistent power supply to the igniter for proper burner tube function. Disconnect power cord from wall outlet. Shut off gas supply by turning the wall gas valve off. Remove 2 small philips screws to detach front panel door from dryer frame. Remove 2 additional philips screws on left front side panel inner door frame. Gently pull front dryer panel off beginning at top and put it aside. Igniter and the 2 ignition coils are plainly visible and easily accessible at bottom right corner of dryer. Igniter is attached to the burner tube and facing into the heater housing assembly. The 2 ignition coils are attached just above the gas valve on the rear of the burner tube. The ignition coils are simply attached to the rear of the heater tube with one bracket using 2 small philips screws. First, disconnect igniter plug wire harness. Next, I recommend using a small open end applicable size wrench (5/16 perhaps) to remove attaching igniter screw. A small 1/4 ratchet with applicable socket size may also be used. Handle the igniter only from the white ceramic part when installing. You don't have to completely remove the igniter screw from the burner tube. The igniter has a white ceramic horse shoe shape slot in which the attaching screw goes through for tightening to the burner tube. Just unscrew generously for removal and replacement of the igniter. Do NOT over tighten igniter screw as the white ceramic plate may break from over torqing. Reconnect igniter wire plug harness. The igniter part I used was PartSelect Number PS373025. Next, remove the ignition coil bracket by unscrewing the 2 small philips screws from rear of the heater tube frame. Remove only 1 ignition coil at a time by removing the wire plug harness and simply lifting upward. One coil will have 2 prongs while the other has 3 prongs so you can't go wrong when reconnecting the wire plug harnesses. I used the PartSelect 'M' Series New Style Coil Kit (2 coils included)which was PartSelect Number PS334310. Replace the front dryer panel back. Attach the front door to the panel and dryer frame using the 2 philips screws. Attach the 2 left side inner door front panel philips screws to dryer frame. Turn on the wall gas valve. Reconnect power cord to wall outlet.
3 of 4 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
All Instructions for the DG408
106 - 120 of 1079