MDG16CSAGW Maytag Dryer - Instructions
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- Customer:
- Cindy from Vincent, OH
- Parts Used:
- WP33002535
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers
dryer drum not turning well clothes were wrinkled
Took off the front, took thd drum off, removed old belt, placed on new belt ptu everything back together.
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- Customer:
- Charles from Treynor, IA
- Parts Used:
- WPY312527, WP6-3705180, WP6-3700340, WP354987
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
The Idler Pulley broke off the Idler shaft
I removed the 2 screws that hold the door and removed the door. I then removed all the screws that hold the front panel and removed the front panel. Then I was able to lift (on hinges) the top panel. I then removed the screws that hold the front drum housing, then removed the drum and belt. At that point you have plenty of room to access the idler pulley. I removed the Idler pulley spring. Then I removed the the screw holding the Idler arm and shaft. Reinstalled in reverse order.
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- Customer:
- John from Floyd, VA
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Too much drying time, not hot enough
I removed the Drier Door and removed the Front Drier Panel exposing the Gas Valve & associated parts. I removed two (2) screws holding the Gas Valve Coils in place & replaced the 2 terminal coil, then replaced the screws, Front Cover & Drier Door. I liked the results so much, I ordered the other Gas Valve Coil and will replace it also when it arrives.
Good trouble shooting information.
Good trouble shooting information.
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- Customer:
- Beverly from Oakland, MD
- Parts Used:
- W10410997
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
dryer would not run
Removed door and front and drum. Removed fan assembly. Be careful when working fan off of motor shaft. Unhooked wiring from motor. Removed clips. Replaced motor. Reverse procedure to put dryer back together. Now works like new. Very, very, happy. Part came in 2 days using standard shipping. Way better than buying a new dryer.
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- Customer:
- Joseph from Colts Neck, NJ
- Parts Used:
- W10169313
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Replaced door switch
Door switch was very easy to replace as it simply snaps in for the outside and you just clip on the two control wires that already have clips on them.
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- Customer:
- julia from WOODRIDGE, IL
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Gas Dryer Runs With Heat for Less Than 5 minutes, Timer Won't Advance in Autodry
My gas dryer would run with heat for 5 minutes in all settings, but kick off and not heat again. Timer would not advance in autodry. Thought it was the cycling thermostat, so replaced that, but did not solve the issue. Ordered the coils, and cleaned out heavily clogged lint from bottom of lint trap, especially right above the fan motor at the bottom of the trap. Received the coils, opened the top and front, took out drum, and replaced the coils. The replacement took less than 2 minutes. Be careful putting the drum back on to make sure the felt is not caught inside the drum. You can give it a spin to make sure. Wear gloves, as I cut myself up pretty good on the edges of the dryer body. The inside of my dryer looks like a crime scene! Anyway, I put it back together, and it runs great. Solved the timer advance issue in autodry, and the heat kicks on and off when it is supposed to. Good luck! Thanks Part Select!
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- Customer:
- Janel from BOWDLE, SD
- Parts Used:
- WP6-3700340, WP6-3129480, WP33002535, WP33001807, 306508, 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set, Wrench set
Dryer started to sound like someone was beating a dog in the laundry room.
The dryer model was on a sticker inside the door which had long ago rubbed off. The most difficult part was figuring our how to dismantle the dryer. I finally looked up the matching washer by model number watched a youtube video and the dismantle was the same....take off the door, remove front cover then remove screws that held the hook brackets that held the top down. After we figured that out the rest was pretty easy. The main issue was the Idler Pulley Wheel and Bearing. We decided to replace the rest of the parts because we already had the thing all apart. It is amazing all the lint that gets into the dryer cabinet and passed the lint filter. Dryer works like new again. I love this set and will keep repairing as long as we can get parts.
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- Customer:
- Paul S from Peoria, AZ
- Parts Used:
- WP6-3700340, WP33002535, 12001541
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Socket set
Dryer make scraping sound while running.
Followed the directions on the video. I recommend changing both tumbler wheels and idler pulley when you have unit apart as well as the drive belt. When I opened the dryer cabinet I immediately saw what my scraping noise was being caused by. A screw holding a baffle in the dryer tub had backed out and was scraping the cabinet wall on each rotated pass. Like I said, when you have the cabinet apart you might as well change parts that are going to fail. The repair was very easy and now I have many more years of service with my dryer. Had I opened the dryer before to see what parts I needed I would have seen the loose screw.
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- Customer:
- Jodel from SAN DIEGO, CA
- Parts Used:
- 279834
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Screw drivers
Heat up then gas flame shuts down after 5 or so minutes igniter glows again trying to reignite but no gas supply coming out of the tube.
I ordered the top 5 items that may cause this problem based on the troubleshooting guide presented by the technicians I found in youtube. I replaced the coils and that fixed the problem. The coils are the first to go out according to techs, but I have the other parts just in case I may need them later on. My Maytag dryer which is over 19 years old is alive and working again. The coils are accessible from the bottom access panel secured by 2 nut screws, unplug the dryer first, then the coils are secured by a bracket with 2 small philips head screw, I used a stubby philips screw driver to remove the bracket, undo the 2 electrical connectors on the coils one with 2 prongs and the other with 3 prongs. Put the new coils attached the electrical connectors and secured them with the bracket. Checked for any loose wiring ensuring connectors are secured in place, then test run the dryer with the panel off so you can see the if the flame stays on, if you run the dryer without wet clothes the flame may stop after 15 or so minutes. It is better to test run the dryer with wet clothes just like when your drying fresh washed and wringed clothes. It was really easy, good luck!
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- Customer:
- Conrad from CHESAPEAKE, VA
- Parts Used:
- W10169313
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Dryer No longer shuts off When Door Opened
All you need for a Maytag is a snub nose Philips screw driver. The screws on the front panel are at the bottom angled down, so a regular length Phillip's won't work. Just unscrew the 2 screws, then lift the panel up and out. Careful not to pull out too far, there are 2 wires attached to the switch. The replacement switch is NOT an exact copy of the old one. My Maytag is over 30 years old and it only had 2 prongs on the switch. The new one has 3. Don't let that throw you. It is the same size. Just attach, 1 wire to the bronze connector & the other to the silver. Push the switch into the door opening, re-attach the door. Total time 20 minutes. Saved well over $100 in a service call. Anyone with an IQ above freezing can do it.
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- Customer:
- Louis from CHARLES CITY, IA
- Parts Used:
- 279834
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
dryer would light up gas coil bad
took 2 screws out and replace new coils
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Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
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- Customer:
- Dave from CRANBERRY TWP, PA
- Parts Used:
- WPY014874, WP33002535, 306508, 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
Noisy
This is the dryer of a 28 year old Maytag laundry pair. I had replaced the glide kit 8-10 years before. Did them again because they were worn in half again but this time I added the 2 roller kits and the belt, really just guessing. I was surprised how full of dust and lint the inside was, especially the blower fan blades. I ordered the screw because the belt idler pulley assembly was very wobbly and I hoped that was the screw anchoring it to the motor housing was the problem but it wasn't. Turns out the threaded hole in the housing was stripped, due I guess to years of vibration. It was too tight to get a tap and dye in there so I drilled the hole out and replaced the screw with a bolt and nut and lock washer. Before drilling it out I tried a few strands of wire and JB Weld, like the trick with stripped wood holes where you break off toothpicks in the hole and fill with wood glue. But that stripped out too so I drilled and used the bolt. Turned out I didn't need that $7 screw. Probably should have known comparing it to the old one which looked the same after I cleaned it. Anyway, it sounds fine again.
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- Customer:
- CHUCK from HARDIN, KY
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
ignitor failed to ignite gas or would fail to after first ignition.
Watched youtube video to problem shoot. Cause determined to be coils bad. Searched web found Parts Select to be easiest site to deal with and had coils for best price. Followed instructions supplied with parts. Dryer works like new.
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- Customer:
- Warner from Troy, OH
- Parts Used:
- WP6-3705180, WP6-3700340, WP33002535
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Wrench (Adjustable)
Dryer was making a loud sueaking sound.
On my maytag dryer I took the door off with two screws, took the front panel off with four srcews, lifted the top panel up a little bit and removed the belt from the "tub" and pulled the tub out. I could easily then access the idler arm and pulley wheel. Due to the age of the dryer, I also replaced the tub belt while it was apart. Reversed the process to put it back together, alot easier than I thought.
Warner
Warner
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