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GDG23CD Maytag Dryer - Instructions

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All Instructions for the GDG23CD
106 - 120 of 1060
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Customer:
William from Fullerton, CA
Parts Used:
WP33001003, 306436
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Dryer door would not stay closed
1. Popped out old latch from dryer with a screw driver and pressed in new latch with fingers. Did not need to replace the part that is in the door. Very simple repair.
2. Lint filter was worn out and needed replacing.
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Customer:
Bill from Frisco, TX
Parts Used:
WP33001003, 306508
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Nutdriver, Screw drivers
Slide Was Worn Down To Bare Metal
Took the front off , removed front drum support, drilled out existing rivets, & replaced slides,riveted them in place,and re-assembled.
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Customer:
Thomas from Wasilla, AK
Parts Used:
WP306199
Difficulty Level:
A Bit Difficult
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Dryer would run and get hot but lose heat in about 4 minutes.
Replaced a bad 240 volt heat relay and the problem was solved.
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Customer:
Alan from BETHESDA, MD
Parts Used:
WPY014874, WP315772
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
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Customer:
William from Springfield, OH
Parts Used:
WP6-3129480, WP312535, 12001541, WP9703438
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Screw drivers
One of the roller shafts was worn
Replaced both rollers,shafts, bearings and snap rings.
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Customer:
Jeffrey from Glenshaw, PA
Parts Used:
4391996
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Wrench (Adjustable)
Dryer not heating....Had to be igniter or solonoid
Upon receipt of part, just loosened 1 fastener, slid igniter forward and out....unclipped wire connection and replaced... Could not have been easier. Be careful not to overtighten fastener when replacing. Description and pictures made for very easy selection.
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Customer:
Charles from Daphne, AL
Parts Used:
WP312535, 12001541, WP9703438
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Pliers, Screw drivers, Socket set
Squeaking noise
I had replaced belt, but the noise continued. Ordered new rollers and washer. Removed the front panel by tipping the dryer back against the wall and removing two screws at the bottom of the panel. Tipping the dryer makes it easy to remove the front panel. Removed the front drum support by removing four (4) screws. I was then able to just move the drum enough to have access to the rollers. Didn't even have to remove the belt. Replaced the rollers. Needed special pliers to remove and replace the retaining rings. Put the drum back into position and mounted the front drum support. Tightened four screws and then put the front panel back on. Plugged it in and tested it. Problem solved. Took about 35 minutes. Thanks
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Customer:
Loretta E. from Miamisburg, OH
Parts Used:
W10169313
Difficulty Level:
Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Button to start dryer
Per instructions I printed off online: took off door, then the front panel. Pulled out the old switch/button, connected the new switch/button, made sure the new button was working; put the panel back on then the door and DONE!
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Customer:
suzanne from Ottawa, IL
Parts Used:
WP33001003
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
dryer filter screen broken
I didn't think it would fit as it looked bigger then the old one, I called the service department and they were very helpful. They made note of the fact that I had called with questions in case I had to call again, but it worked, and no one laughed at me. It was very nice of them. Thank you for all the help
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Customer:
Horacio from Houston, TX
Parts Used:
4391996
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Socket set, Wrench set
Not enough heating to dry clothes.
My Maytag gas dryer model MDG7600AWW is about 12 years old. Everything else works fine except it takes 4-5 drying cycles instead of 1 to completely dry my clothes properly. The flat igniter was simply cracked but not broken so it only worked some times. My gas dryer igniter and the 2 ignition coils work hand in hand so I replaced all 3 parts. The ignition coils provide a solid and consistent power supply to the igniter for proper burner tube function. Disconnect power cord from wall outlet. Shut off gas supply by turning the wall gas valve off. Remove 2 small philips screws to detach front panel door from dryer frame. Remove 2 additional philips screws on left front side panel inner door frame. Gently pull front dryer panel off beginning at top and put it aside. Igniter and the 2 ignition coils are plainly visible and easily accessible at bottom right corner of dryer. Igniter is attached to the burner tube and facing into the heater housing assembly. The 2 ignition coils are attached just above the gas valve on the rear of the burner tube. The ignition coils are simply attached to the rear of the heater tube with one bracket using 2 small philips screws. First, disconnect igniter plug wire harness. Next, I recommend using a small open end applicable size wrench (5/16 perhaps) to remove attaching igniter screw. A small 1/4 ratchet with applicable socket size may also be used. Handle the igniter only from the white ceramic part when installing. You don't have to completely remove the igniter screw from the burner tube. The igniter has a white ceramic horse shoe shape slot in which the attaching screw goes through for tightening to the burner tube. Just unscrew generously for removal and replacement of the igniter. Do NOT over tighten igniter screw as the white ceramic plate may break from over torqing. Reconnect igniter wire plug harness. The igniter part I used was PartSelect Number PS373025. Next, remove the ignition coil bracket by unscrewing the 2 small philips screws from rear of the heater tube frame. Remove only 1 ignition coil at a time by removing the wire plug harness and simply lifting upward. One coil will have 2 prongs while the other has 3 prongs so you can't go wrong when reconnecting the wire plug harnesses. I used the PartSelect 'M' Series New Style Coil Kit (2 coils included)which was PartSelect Number PS334310. Replace the front dryer panel back. Attach the front door to the panel and dryer frame using the 2 philips screws. Attach the 2 left side inner door front panel philips screws to dryer frame. Turn on the wall gas valve. Reconnect power cord to wall outlet.
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Customer:
Stephen from Port Jefferson, NY
Parts Used:
WPY312959, WP33001003, 306508
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Screw drivers, Socket set, Wrench set
Squealling clothes dryer.
Undid two screws in lower front of dryer and popped off front. Removed screws holding lint screen duct and brackets supporting tumbler and removed duct and tumbler quite easily. Pulled, cleaned and oiled rear rollers, replaced front glides, and thoroughly cleaned exhaust duct of lint. Put new belt into position on the roller before sliding tumbler back in, then pulled belt over tumbler as it went in. Be careful to follow belt path directions correctly.
Key to this repair was obtaining the parts so easily from Parts Select.com. Ordered at 2pm and had them 2pm the following day. Unbelievable! These machines are relatively simple to keep running when the parts are available so easily. Thanks for great service.
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Customer:
Robert from Mentor, OH
Parts Used:
Y303836
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Pliers, Screw drivers
Dryer rattled in operation
Unplug the dryer. Remove two screws to remove the front drum housing. Remove 4 screws to remove the front drum housing. The front panel and front drum housing do not need to be unwired to work on the blower. Loosen wire harnesses and move panel and housing out of the way. Remove 2 spring clips holding the blower assembly to the motor shaft. Remove blower. Install new blower and re-assemble in the reverse order. The other stories written on the subject were spot on. This repair also made the clothes dry more quickly. I did not realize that long before the ryer made noise, there was a reduction in air flow. A simple vacuum switch to monitor air flow would tell you when there is a problem or that the filter/duct needs to be cleaned.
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Customer:
Glenn from Lewisport, KY
Parts Used:
WPY312959, WP6-3129480, WP9703438, WP312535, 12001541
Difficulty Level:
A Bit Difficult
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers
Dryer was sweaking and rumbling. Found tub support roller and shaft had failed bushing.
My wife had to help me due to a recent back surgery that I had.

1. Disconnet power. Then if you have room, slide dryer away from wall far enough to tilt it slightly back. We had to do this to remove the two lower front panle philips head scres due to my screwdriver length. If you have a stubby, then you don't need to do this. Remove by pulling out on bottom until the two clips at top disengage from dryer top panel.
2. We removed the four 1/4" head sheet metal screws that hold the front tub support panel (with lint screen). Be carefull of wiring. One moisture sensor wire has to be removed from front cover on lower right side near bottom of tub opening. The remaing wires on left side are long enough to leave them attached and "swing" front panel to your left and in my case, lay it back uprite against the washer front.
3. We slid the tub forward enough to lay old belt down so I could see how it was routed around drive. I wanted to verify paperwork that came with new belt. We then set entire tub out of dryer. You might want to take it to another room if you laundry room is cramped.
4. We removed the nut from back of each support roller shaft, I believe it was 3/8 hex. Then reveresed this procedure to install the new roller and shaft. It was easier to assembly rollers before installing as a unit.
5. I removed the old belt and confirmed its length to new belt. I then installed the new belt over drive sheave and tensioner.
6. We then installed the tub and worked belt around it while keeping it on the drive sheave and tensioner pulley. Had to kind of stick my head into tub to start belt unto it.
7. We checked tub front and rear felt seals and I would recomment\d changing these if your dryer is older than 10 years, we did not have then so kept old ones.
8. We replaced the front tub support and installed the four sheet metal screws.
9. We replaced the front cover and installed the two lower philips head screws.
10. Re-connected power and tested operation.
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Customer:
Tima from Pomfret Center, CT
Parts Used:
Y303836
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Screw drivers, Socket set
Rumbly noise
I removed the front panel (two screws at bottom, then lifted bottom toward me until the top holders slid out). Then I unscrewed the front assembly that holds the dryer drum (four screws), first propping the drum from below so it would stay in place. I removed the blower housing (seven screws) and could see that the blower wheel was loose on the spindle. The 'D' shaped fitting had rounded out. A pair of snap ring pliers made removing the retaining ring and the wheel clamp a cinch and saved a good deal of teeth gnashing. I slid on the new blower wheel and then did everything in reverse. One caution: be sure the drum is pushed firmly up and back when reattaching the front assembly. (It can be done successfully with two hands). I had to re-do this part of the reassembly because the bottom of the drum was rubbing against the blower assembly. Once that was corrected, the dryer ran noiselessly. Thank goodness for PartSelect's diagrams. They're invaluable.
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Customer:
james from WOODBURN, IN
Parts Used:
306508
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Screw drivers
front glides wore out
Followed instruction video
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All Instructions for the GDG23CD
106 - 120 of 1060