MDE9557AYQ Maytag Dryer - Instructions
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- Customer:
- John from Palmdale, CA
- Parts Used:
- WP33002535, WP6-3705180, WP6-3700340
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers, Socket set
Squeaking sound then Barrel stoped turning
Unplugged the unit
Removed door and two clips that hold front panel on (6 Philip crews)
Then removed front panel by hand hold each side of the panel at the top
Of the “U” shape and pulling out ward until it frees it self from the two
Bottom clips.
You can now see a belt that is no longer tight around the drum
When I tried to put the belt back on I noticed the idler pulley was flopping around and I would need to replace it .That where you guys saved me.
Your exploded model and parts list made it easy to see exactly what parts I
Needed to order.
The rest gets a little tricky there is another plate that supports the barrel
A couple of clips that hold the top cover in place all of this must be removed
Note the top cover only need to be lifted up an inch or two at the front where the
Two steel clips where and doses not need to be removed to get this panel off that
Supports the barrel.
There are some wires attached to it also I only had to unplug the three that go to
The door safety switch then I was able to rotate it off to the side out of the way
And now the barrel can be lifted out. You can now remove the idler pulley assembly
I used pliers to remove the spring and a crocket wrench to remove a bolt that holds
The bracket that also should be replaced due to ware at the idler pulley barring pin
The tricky part is putting it all back together again. To explain this I would need to Wright a book. It takes a lot of good common sense. I was proud of how I reached
Around from each side of the motor and by feel alone and get the belt around
The motor pulley and the idler pulley that keeps the belt tight around the barrel
Makes me think I should have been a repairman.
Removed door and two clips that hold front panel on (6 Philip crews)
Then removed front panel by hand hold each side of the panel at the top
Of the “U” shape and pulling out ward until it frees it self from the two
Bottom clips.
You can now see a belt that is no longer tight around the drum
When I tried to put the belt back on I noticed the idler pulley was flopping around and I would need to replace it .That where you guys saved me.
Your exploded model and parts list made it easy to see exactly what parts I
Needed to order.
The rest gets a little tricky there is another plate that supports the barrel
A couple of clips that hold the top cover in place all of this must be removed
Note the top cover only need to be lifted up an inch or two at the front where the
Two steel clips where and doses not need to be removed to get this panel off that
Supports the barrel.
There are some wires attached to it also I only had to unplug the three that go to
The door safety switch then I was able to rotate it off to the side out of the way
And now the barrel can be lifted out. You can now remove the idler pulley assembly
I used pliers to remove the spring and a crocket wrench to remove a bolt that holds
The bracket that also should be replaced due to ware at the idler pulley barring pin
The tricky part is putting it all back together again. To explain this I would need to Wright a book. It takes a lot of good common sense. I was proud of how I reached
Around from each side of the motor and by feel alone and get the belt around
The motor pulley and the idler pulley that keeps the belt tight around the barrel
Makes me think I should have been a repairman.
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After initial ignition & first heat cycle, gas valve would fail to re-ignite
The good: No need to pull out dryer beyond point where (wall) gas valve could be shut off.
The gotcha: Be sure to wear thick leather gloves to protect your hands. I discovered sharp edges the hard way!
The tip: To loosen gas valve inlet nut and to remove gas pipe from valve, use a bottom-to-top wrench motion. Despite threads being right-handed, this counter-intuitive operation (the thinking is that you are tightening the nut instead of loosening it) is necessary due to nut being located on the valve rather than the gas pipe which reverses the context.
The ending: Wife is happy to be back in the drying business and I'm happy just to have her happy not to mention saving a little $ in the process! Thanks PartSelect.com!!!
The gotcha: Be sure to wear thick leather gloves to protect your hands. I discovered sharp edges the hard way!
The tip: To loosen gas valve inlet nut and to remove gas pipe from valve, use a bottom-to-top wrench motion. Despite threads being right-handed, this counter-intuitive operation (the thinking is that you are tightening the nut instead of loosening it) is necessary due to nut being located on the valve rather than the gas pipe which reverses the context.
The ending: Wife is happy to be back in the drying business and I'm happy just to have her happy not to mention saving a little $ in the process! Thanks PartSelect.com!!!
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- Customer:
- Ryan from Raleigh, NC
- Parts Used:
- W10410997
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers, Socket set
Over the last year the 'start' button has had to be held to 'start' the dryer, with a humming noise during the process. Eventually it hummed, stank, and wounldn't start.
Yanked the front panel, observed motor operation while my smoking hot wife started the unit. Our washer and dryer get beaten like rented mules with kid laundry. I tried this site, and decided to spend a little $$ on a replacement motor. I was impressed with the operator, she even asked what the symptoms were and helped to avoid wasting time and money.
The part arrived on time, and installed quickly. I am a hero in my wife's eyes, and that certainly carries weight.
Then again, I didn't have to dispose of the old dryer, pay for a new one, or haul the replacement upstairs.
Win-win!
The part arrived on time, and installed quickly. I am a hero in my wife's eyes, and that certainly carries weight.
Then again, I didn't have to dispose of the old dryer, pay for a new one, or haul the replacement upstairs.
Win-win!
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- Customer:
- Richard from Loretto, MN
- Parts Used:
- 306508
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
My dryer - which is about 20 years old - was starting to make some rubbing/scraping sounds from the drum area.
This was pretty much as easy as most other folks had described on this site.
1. Removed the two screws at the front bottom that are holding on the fromt panel, and then lift up and remove the panel.
2. Disconnect the door-open-safety-switch, remembering which color of wire goes on which connection.
3. Remove the four screws (two on each side) on the front bracket that supports the drum and tthat contains the front glides.
4. Remove support bracket and lint trap, letting the drum rest gently on the stuff underneath.
5. Remove the screws holding the lint trap to the support bracket. (My model had five screws.) Remove lint trap from support bracket.
6. Drill out the two pop rivets on each of the two glides, noting the orientation of the teflon pad and mounting strip.
7. Secure - and here is where I had a little problem - new glides in place with pop rivets. (I hadn't use a rivet gun in a while, so I messed up the first pop rivet and had to go to the hardware store to get a replacement. I didn't hold the pop rivet in all the way while I was accuating the gun!)
8. Reverse the process for assembly, and you are all done.
It's simple.
1. Removed the two screws at the front bottom that are holding on the fromt panel, and then lift up and remove the panel.
2. Disconnect the door-open-safety-switch, remembering which color of wire goes on which connection.
3. Remove the four screws (two on each side) on the front bracket that supports the drum and tthat contains the front glides.
4. Remove support bracket and lint trap, letting the drum rest gently on the stuff underneath.
5. Remove the screws holding the lint trap to the support bracket. (My model had five screws.) Remove lint trap from support bracket.
6. Drill out the two pop rivets on each of the two glides, noting the orientation of the teflon pad and mounting strip.
7. Secure - and here is where I had a little problem - new glides in place with pop rivets. (I hadn't use a rivet gun in a while, so I messed up the first pop rivet and had to go to the hardware store to get a replacement. I didn't hold the pop rivet in all the way while I was accuating the gun!)
8. Reverse the process for assembly, and you are all done.
It's simple.
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- Customer:
- Philip from La Palma, CA
- Parts Used:
- WP338906
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Wrench set
No heat
Took everything apart, replaced the igniter flint, and still didn't get heat. Then found out the thermal sensor wasn't running a electrical current through it with voltmeter and just replaced that, now it we have heat again!
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- Customer:
- Manuel from Jurupa Valley, CA
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers
Dryer not Drying
Replaced both Coils. Purchased M Series coils much less expensive buying coils together instead of seperately. Problem solved.
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The dryer drum would not rotate when the start button was pushed.
First this I did was to disconnect the power cord. Then I removed the screws that held on the door and the two on the other opposite side. This allowed the front panel to be removed. Next I removed the top two screws which allowed the top to hinge up and out of the way. Then I removed the rest of the screws that held the front drum support and moved it to the side. I did have to unclip the wires that ran to the interior light. I did not how ever have to disconnect any wires at the front of the dryer. Next I reached in from the bottom of the drum and released the drive belt from the spring loaded pulley. at this point the drum was able to be removed out the front of the unit. This gave access to the motor. It was necessary to remove the several screws that held on the front half of the fan housing. Again I did not remove any wires as this too could be moved to the side out of the way. I then removed the snap ring and clamp from the fan end of the motor shaft and pulled the fan off of the shaft. Next I unclipped the wiring connector from the top of the motor and used a screw driver to pry the connector off. Next I used a socket on a long extension to push down on the motor clamps while tilting the socket out to allow the clips to release. I then removed and replaced the motor and assembled in the reverse order. While I had the drum out I inspected the rear support wheels and noted that one would hardly turn. I removed both wheels via a nut on the back side of the shafts. I found that one had shifted on the bushing and was making contact with the frame. I used a vise to press the wheel back into the correct location. I also applied anti seize with a small amount of dry graphite to both wheels and insured that the both rotated freely. I then installed the front two glide slide pads using the pop rivets provided in the kits. I used a shop vac and cleaned any lint from inside the dryer. I then reassembled the front covers in reverse of the disassembly process. I rotated the drum by hand prior to applying power. I also ran the unit with the heat off for the first five minutes. Total cost was under $160.00 or half of the replacement cost.
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- Customer:
- Barry from League City, TX
- Parts Used:
- 306508
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
Noisy and thumping drum
I set the dryer on its back to make alignment of the front drum guide cover easy to reinstall in the seal after completion. I removed the 2 screws at the bottom front then removed the white and yellow wires to the interlock switch and set the front cover aside. I then removed the 4 nut screws holding the front drum cover and removed. On the back side there are two teflon and cork "bearings". I had ordered two even though only one was worn down to metal. On each one I then removed the two rivets by drilling them out. Then I placed the corks into the bearing slots with a little glue then inserted the teflon into the slots and riveted them into place with the rivets that came with the kit. I replaced the drum cover, connected the switch and screwed the dryer front cover back on. I set the dryer back up. Connected the vent hose and turned the dryer on. Beautiful sweet smooth and quiet operation. I had replaced the front and back drum seals a few months ago and saw the teflon was missing but did not have the kits at that time. With a complete job I would recommend replacing the front and rear drum seals and the two teflon/cork bearing kits at the same time.
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- Customer:
- Landon from SPANISH FORK, UT
- Parts Used:
- WP6-3129480, WP33002535, WP33001807, 12001541
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
Very Loud Squeaking / Clothing having rips
The support rollers were fried, literally. I'm honestly surprised they held on. Let's just say that the "roller" part wasn't even attached to the support wheel... That bad. Because there wasn't much support there is a small tear in the metal on the back drum. The felt seal for the drum had basically been worn down to pieces. So I order two drum support rollers, two roller shafts, a new drum felt seal, and a new rib belt.
After the repair, no more squeaking, literally a huge difference, and because of there's plenty of support now for the drum, there isn't any clothes being torn. If it weren't for the videos and the parts, we would of spent hundreds of dollars on a new dryer. Instead we spent just over $100 and now our dryer is quiet and operating better than when we got it.
After the repair, no more squeaking, literally a huge difference, and because of there's plenty of support now for the drum, there isn't any clothes being torn. If it weren't for the videos and the parts, we would of spent hundreds of dollars on a new dryer. Instead we spent just over $100 and now our dryer is quiet and operating better than when we got it.
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- Customer:
- Glenn from Ossian, IN
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set, Wrench set
gas dryer would fire, but shut down before getting warm enough to dry clothes
Removed lower front cover of dryer, located coils, removed old coils by disconnecting the wires and removing the hold down bracket screws. Pulled the old coils out replaced them with the new coils by aligning the index pins on the coils with the holes in the bracket then reattached the bracket and plugged the wires into the new coils. Then closed the cover on the front of the dryer. Dryer now ignites and stays on to heat up and dry clothes.
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- Customer:
- Vicki from Springfield, MO
- Parts Used:
- WP33001808
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Drying time was taking longer than it should.
I simply went on line and ordered the part. I had it shipped to my office since I am here all day, M-F. I received the part in 2 days. I took it home, pulled out the old lint filter and slid in the new one. It is amazing how much more efficient my dryer is. The old lint filter had about a 6 inch tear in it so it was not catching all the lint.
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- Customer:
- Ken from Rochester, NY
- Parts Used:
- 306436
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Latch was broken over 15 years
Old latch and door striker were pried out with a flat blade screwdriver. New components popped right in. Repair was less than two minutes.
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- Customer:
- Georgio from Oradell, NJ
- Parts Used:
- WP338906
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Pliers
the glow ignitor would not cycle on
I had an issue where I was not getting any power to my ignitor. After replacing the ignitor with a fresh one, the problem persisted. Next, I went hunting all the fuses and therrmostats for continuity. All seemed fine. So finally I decided to jump the flame sensor which is located on the outside of the flame tube. WHALLA! It ignited the glow plug. So with one 1/4"" nut driver I removed the single bolt from the unit, then I used a pliers to remove the two wires from the old unit. I replaced the sensor with Tue new unit and all was well. It took less than 5 min once I diagnosed the problem.
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- Customer:
- Mario from Hugo, MN
- Parts Used:
- 4391996
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
No heat generated in dryer
My dryer stopped producing heat and everything else was working fine. I did some research on this site and others had the similar problem pointing to the ignitor going bad. I needed to determine which ignitor fit my dryer. What I learned is that some of the parts come with a series number and you need to know which one matches your serial number. My serial number started with 40 and I had a choice of buying the part for a series 10 or 60 series. In my case I needed to buy the 10 series since you either go with the same number as your serial number or lower, never higher. When the part came in I removed the dryer door by removing the 2 screws. I then removed the 2 screws on the opposite side of the door. Once the 4 screws were removed I was able to take the front cover off. The ignitor was on the right side and easy to get to. I unplugged the ignitor and used my socket set to remove the bolt. Once removed I vacuumed the lint in the dryer and installed the new ignitor carefully not touching the black area of the part. I put the front cover back on, put the door in place and put all 4 screws back in place. I started the dryer and it was fixed! This was an easy job to repair that saved me money.
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- Customer:
- Jim from Germantown, WI
- Parts Used:
- LA-1003
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
old latch broke
I inserted the clip
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