LDG9904AAL Maytag Dryer - Instructions
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- Customer:
- jim from sierra vista, AZ
- Parts Used:
- Y303836
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Blower fan came loose and broke
No manual on this so had to remove about 12 screws to figger out disassembly,after locating the right ones[front]the job was easy.Remove front plate,remove drum bearing,remove blower front cover,remove snap ring,remove broken fan,clean fan shaft,slide new fan onto shaft[there is a flat in the bore of new fan]instal fan retainer on stub of fan,reinstal snap ring,reinstal the rest of the parts,test drive system[all sat]The part was exactly as ordered,thanks,Jim Thompson
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- Customer:
- William from ORANGEBURG, SC
- Parts Used:
- WPY312959, WPY312527, WP6-3037050, WP6-3033630, WP315772
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
old was belt stretched and idler pulley gummed up, drum won't tumble a normal sized load
Replaced all the parts per the very good video provided on the website.
I recommend watching the video very closely several times. BE SURE THE BELT IS NOT IN THE DRUM'S GROOVE. The video mentions this very very briefly; I caught it on my third viewing. If your belt is not the correct location, it may still turn the drum for you - and eat the belt up in about an hour.
I recommend watching the video very closely several times. BE SURE THE BELT IS NOT IN THE DRUM'S GROOVE. The video mentions this very very briefly; I caught it on my third viewing. If your belt is not the correct location, it may still turn the drum for you - and eat the belt up in about an hour.
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- Customer:
- paul from WHEELING, IL
- Parts Used:
- WP33002793, 279834
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Flame goes out after 5 seconds.
Tilted dryer back to access the two screws on the front panel, remove front panel, by raising it up 90° and pull the wires off for the door switch, first I remove the one 5/16 self tapping screw That holds the burner assembly onto the bracket, removed the hot surface igniter screw from old burner assembly, attached to new burner assembly, reinstalled burner assembly and also cleaned orifice from gas valve, also while the front cover was off I remove the fan housing cover and vacuumed out all The lint attached to the fan assembly, unit works great again.
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- Customer:
- Charles from Long Beach, CA
- Parts Used:
- WP338906
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Socket set
No heat...
Removed and replaced both the thermostat sensor and the ignitor. Tested thej dryer and it worked. Replaced the front panel and it was good to go.
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- Customer:
- William from Winter Park, FL
- Parts Used:
- WP6-3037050
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Squealing noise on start up.
I opened the back acess panel and started the dryer. Looking at the motor and idler pulleys it was obvious by the frequency of the squealing noise that it was coming from the idler pulley.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
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- Customer:
- Tom from Schaumburg, IL
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
My drier would start create heat,than stop heating after 8-10minutes.
After reading the many different common stories,I replaced both coils (m series).Very simply lifted up the top of driver,held by 2 snap springs and 2 lint vent screws.Removed front cover,2 screws and 2 bottom snaps,coils down on bottom left.r/r both coils,reinstalled covers and let there be heat!This website is a blessing!!
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- Customer:
- chuck from smithtown, NY
- Parts Used:
- 279834
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Dryer heat would go off and timer would not move. Dryer would continuously run
Replaced coils on gas valve.
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- Customer:
- Anthony from New Port Richey, FL
- Parts Used:
- 307208
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Dryer would over heat,temp uncontrolable
The repair was very simple.I removed the door and the front cover.Right in front of the blower housing sat the temperature control thermistor.All that was needed to do the swap was a nut driver.Everything I read said the high limit thermostat may of been bad but it was fine.Ordering the parts was easy and fast all I needed was the model number and all the charts and numbers were easy to find.Thank you Parts select..
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- Customer:
- John from Floyd, VA
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Too much drying time, not hot enough
I removed the Drier Door and removed the Front Drier Panel exposing the Gas Valve & associated parts. I removed two (2) screws holding the Gas Valve Coils in place & replaced the 2 terminal coil, then replaced the screws, Front Cover & Drier Door. I liked the results so much, I ordered the other Gas Valve Coil and will replace it also when it arrives.
Good trouble shooting information.
Good trouble shooting information.
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- Customer:
- Dale from Livingston, TX
- Parts Used:
- LA-1003
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Door wasn't staying closed
popped up top of dryer -- With pliers squeezed clips on inside of latch - - with screw driver pryed latch out -- just pused new latch in.......... Thanks to parts select for sending part sooo fast.. wife was happy.. Thanks, Dale
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- Customer:
- Gale F. from Atlanta, GA
- Parts Used:
- 33001167
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Needed a replacement lint filter.
I pulled out the old filter, the screen of which had ripped, and put in the new one...It took a few seconds! Mainly I was delighted that from the online photo guide I had chosed correctly!
Glad your site exists! It prolongs the life of older but functional equipment.
Glad your site exists! It prolongs the life of older but functional equipment.
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- Customer:
- Lori from Moreno Valley, CA
- Parts Used:
- MAL9000AXX, 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable), Wrench set
Dryer was not heating consistently
Inherited an older Maytag natural gas dryer that was not heating . Just heated at start then would not after 5 mins or so. Went to Partselect site and it had a troubleshooting section and read and narrowed down the part needed by ohming the coils. Ordered the coils for less than $20 and ordered a natural gas to propane conversion kit. Parts arrived in 2 days on regular shipping, very quick! Instruction were very simple to follow and coils were installed in under 15 mins. Propane conversion kit was perfect and was installed in 30 mins and dryer ran just like new. Cleaned inside thoroughly and couldn't be happier. Thank you partselect for great service and saving what would have been more than a $300 service call. Did myself for under $50. I highly recommend this site and will use when ever I can!!! Great service, great way to do business!!!
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Loud, rumbling noise
1. Removed two screws from front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
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- Customer:
- John from ELBRIDGE, NY
- Parts Used:
- WPY312959
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
Broken Tumbler & Motor Belt
Disassembled per instructions. Additional time used to clean inside unit.. Its much easier to install belt on motor pulley and tension pulley ( Roller) from rear access panel. Also ensures proper belt alignment on all items.
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Drum would not turn, drive motor humming loudly and unable to turn drum/blower wheel
The repair video is terrific and many others here have thoroughly described the steps involved to replace the drive motor.
The biggest hurdle for me was that the motor came with a new switch that required a different wiring configuration. No wiring diagram was included. Several others had posted questions about wiring in the Q&A and unfortunately PartSelect kept copy/pasting the same confusing and incomplete answer over and over:
"The Yellow goes to T6, Red to T5 Black to T2, blue to T1 and the white you will remove the blue jumper lead between the switch terminal 4 and 1/4" protector tab, connect the grey harness lead to the 1/4" protector tab."
Reading that doesn't tell me what to do with the white wire, doesn't address that my blue and white wires were crimped into the same connector from the factory, doesn't address that I had 2 black wires crimped into the same connector from the factory, and doesn't address a factory ground wire that connected the frame of the OEM motor to the bracket that the motor sits in.
With all the other excellent info supplied by PartSelect, this was surprising and frustrating. The sales dept ignored an emailed question from me, and the Q&A section didn't allow me to post a question.
Searching the internet, I found a wiring diagram on aceappliancesd dot com that addressed my dryer's OEM wiring configuration. Here's what I ended up with:
TI - Blue and white, crimped together into a single connector
T2 - Black & black, crimped together into a single connector (the wiring diagram I found said this should be black & brown, but they both look black to me)
T5 - Red
T6 - Yellow
1/4" Thermal protector tab - Grey (from the harness)
The new motor switch had a grounding tab with nothing connected to it. I removed the screw holding that tab into the switch and connected the (also grey) OEM short ground wire from the motor frame to the mounting bracket.
I had to cut 2 of the pieces of tape holding the OEM wiring harness together in order to get enough slack for all the connections to reach. If you do this too, make sure all the wires are still clear of the moving parts and the hot bits. You may need to retape the wires together at a different location to keep things tidy.
I also laid the belt over the drum and put 2 pieces of tape over it to hold it in place while I got the drum positioned, then I reached through the back access panel to loop the belt around the motor pulley and idler. Once that's done, just reach over the top of the drum and peel the tape off. I found that much easier than trying to loop the belt by reaching through and past the drum.
The biggest hurdle for me was that the motor came with a new switch that required a different wiring configuration. No wiring diagram was included. Several others had posted questions about wiring in the Q&A and unfortunately PartSelect kept copy/pasting the same confusing and incomplete answer over and over:
"The Yellow goes to T6, Red to T5 Black to T2, blue to T1 and the white you will remove the blue jumper lead between the switch terminal 4 and 1/4" protector tab, connect the grey harness lead to the 1/4" protector tab."
Reading that doesn't tell me what to do with the white wire, doesn't address that my blue and white wires were crimped into the same connector from the factory, doesn't address that I had 2 black wires crimped into the same connector from the factory, and doesn't address a factory ground wire that connected the frame of the OEM motor to the bracket that the motor sits in.
With all the other excellent info supplied by PartSelect, this was surprising and frustrating. The sales dept ignored an emailed question from me, and the Q&A section didn't allow me to post a question.
Searching the internet, I found a wiring diagram on aceappliancesd dot com that addressed my dryer's OEM wiring configuration. Here's what I ended up with:
TI - Blue and white, crimped together into a single connector
T2 - Black & black, crimped together into a single connector (the wiring diagram I found said this should be black & brown, but they both look black to me)
T5 - Red
T6 - Yellow
1/4" Thermal protector tab - Grey (from the harness)
The new motor switch had a grounding tab with nothing connected to it. I removed the screw holding that tab into the switch and connected the (also grey) OEM short ground wire from the motor frame to the mounting bracket.
I had to cut 2 of the pieces of tape holding the OEM wiring harness together in order to get enough slack for all the connections to reach. If you do this too, make sure all the wires are still clear of the moving parts and the hot bits. You may need to retape the wires together at a different location to keep things tidy.
I also laid the belt over the drum and put 2 pieces of tape over it to hold it in place while I got the drum positioned, then I reached through the back access panel to loop the belt around the motor pulley and idler. Once that's done, just reach over the top of the drum and peel the tape off. I found that much easier than trying to loop the belt by reaching through and past the drum.
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