MDG13PDAAW Maytag Dryer - Instructions
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- Customer:
- paul from WHEELING, IL
- Parts Used:
- WP33002793, 279834
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Flame goes out after 5 seconds.
Tilted dryer back to access the two screws on the front panel, remove front panel, by raising it up 90° and pull the wires off for the door switch, first I remove the one 5/16 self tapping screw That holds the burner assembly onto the bracket, removed the hot surface igniter screw from old burner assembly, attached to new burner assembly, reinstalled burner assembly and also cleaned orifice from gas valve, also while the front cover was off I remove the fan housing cover and vacuumed out all The lint attached to the fan assembly, unit works great again.
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- Customer:
- Tom from Schaumburg, IL
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
My drier would start create heat,than stop heating after 8-10minutes.
After reading the many different common stories,I replaced both coils (m series).Very simply lifted up the top of driver,held by 2 snap springs and 2 lint vent screws.Removed front cover,2 screws and 2 bottom snaps,coils down on bottom left.r/r both coils,reinstalled covers and let there be heat!This website is a blessing!!
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- Customer:
- John from Floyd, VA
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Too much drying time, not hot enough
I removed the Drier Door and removed the Front Drier Panel exposing the Gas Valve & associated parts. I removed two (2) screws holding the Gas Valve Coils in place & replaced the 2 terminal coil, then replaced the screws, Front Cover & Drier Door. I liked the results so much, I ordered the other Gas Valve Coil and will replace it also when it arrives.
Good trouble shooting information.
Good trouble shooting information.
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- Customer:
- chuck from smithtown, NY
- Parts Used:
- 279834
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Dryer heat would go off and timer would not move. Dryer would continuously run
Replaced coils on gas valve.
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- Customer:
- Anthony from New Port Richey, FL
- Parts Used:
- 307208
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Dryer would over heat,temp uncontrolable
The repair was very simple.I removed the door and the front cover.Right in front of the blower housing sat the temperature control thermistor.All that was needed to do the swap was a nut driver.Everything I read said the high limit thermostat may of been bad but it was fine.Ordering the parts was easy and fast all I needed was the model number and all the charts and numbers were easy to find.Thank you Parts select..
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- Customer:
- William from Winter Park, FL
- Parts Used:
- WP6-3037050
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Squealing noise on start up.
I opened the back acess panel and started the dryer. Looking at the motor and idler pulleys it was obvious by the frequency of the squealing noise that it was coming from the idler pulley.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
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- Customer:
- Dale from Livingston, TX
- Parts Used:
- LA-1003
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Door wasn't staying closed
popped up top of dryer -- With pliers squeezed clips on inside of latch - - with screw driver pryed latch out -- just pused new latch in.......... Thanks to parts select for sending part sooo fast.. wife was happy.. Thanks, Dale
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Loud, rumbling noise
1. Removed two screws from front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
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- Customer:
- PATRICIA from ANAHEIM, CA
- Parts Used:
- 4391996
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Socket set
Dryer would not heat up
Just unscrew the front of the dryer the Igniter kit is on the right side of dryer unscrew one bolt then replace with new Igniter kit very easy fix make sure to unplug dryer first that way you don't get a shock by touching exposed wires before putting front panel back on clean out any lint that may be in or around bottom of dryer.
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- Customer:
- David from Calvert City, KY
- Parts Used:
- WP6-3129480, 12001541
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Wrench set
drum support roller had come apst from bearing and was making a squealing noise when dryer was running
first i removed the screws holding back cover. Then I remeved nut from tumbler roller shaft. Then I slid shaft from roller .I removed roller then replaced with new one. Installed new shaft then replaced back cover. recieved parts from parts direct very promptly & they were the right parts the first time thanks very much
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Drum would not turn, drive motor humming loudly and unable to turn drum/blower wheel
The repair video is terrific and many others here have thoroughly described the steps involved to replace the drive motor.
The biggest hurdle for me was that the motor came with a new switch that required a different wiring configuration. No wiring diagram was included. Several others had posted questions about wiring in the Q&A and unfortunately PartSelect kept copy/pasting the same confusing and incomplete answer over and over:
"The Yellow goes to T6, Red to T5 Black to T2, blue to T1 and the white you will remove the blue jumper lead between the switch terminal 4 and 1/4" protector tab, connect the grey harness lead to the 1/4" protector tab."
Reading that doesn't tell me what to do with the white wire, doesn't address that my blue and white wires were crimped into the same connector from the factory, doesn't address that I had 2 black wires crimped into the same connector from the factory, and doesn't address a factory ground wire that connected the frame of the OEM motor to the bracket that the motor sits in.
With all the other excellent info supplied by PartSelect, this was surprising and frustrating. The sales dept ignored an emailed question from me, and the Q&A section didn't allow me to post a question.
Searching the internet, I found a wiring diagram on aceappliancesd dot com that addressed my dryer's OEM wiring configuration. Here's what I ended up with:
TI - Blue and white, crimped together into a single connector
T2 - Black & black, crimped together into a single connector (the wiring diagram I found said this should be black & brown, but they both look black to me)
T5 - Red
T6 - Yellow
1/4" Thermal protector tab - Grey (from the harness)
The new motor switch had a grounding tab with nothing connected to it. I removed the screw holding that tab into the switch and connected the (also grey) OEM short ground wire from the motor frame to the mounting bracket.
I had to cut 2 of the pieces of tape holding the OEM wiring harness together in order to get enough slack for all the connections to reach. If you do this too, make sure all the wires are still clear of the moving parts and the hot bits. You may need to retape the wires together at a different location to keep things tidy.
I also laid the belt over the drum and put 2 pieces of tape over it to hold it in place while I got the drum positioned, then I reached through the back access panel to loop the belt around the motor pulley and idler. Once that's done, just reach over the top of the drum and peel the tape off. I found that much easier than trying to loop the belt by reaching through and past the drum.
The biggest hurdle for me was that the motor came with a new switch that required a different wiring configuration. No wiring diagram was included. Several others had posted questions about wiring in the Q&A and unfortunately PartSelect kept copy/pasting the same confusing and incomplete answer over and over:
"The Yellow goes to T6, Red to T5 Black to T2, blue to T1 and the white you will remove the blue jumper lead between the switch terminal 4 and 1/4" protector tab, connect the grey harness lead to the 1/4" protector tab."
Reading that doesn't tell me what to do with the white wire, doesn't address that my blue and white wires were crimped into the same connector from the factory, doesn't address that I had 2 black wires crimped into the same connector from the factory, and doesn't address a factory ground wire that connected the frame of the OEM motor to the bracket that the motor sits in.
With all the other excellent info supplied by PartSelect, this was surprising and frustrating. The sales dept ignored an emailed question from me, and the Q&A section didn't allow me to post a question.
Searching the internet, I found a wiring diagram on aceappliancesd dot com that addressed my dryer's OEM wiring configuration. Here's what I ended up with:
TI - Blue and white, crimped together into a single connector
T2 - Black & black, crimped together into a single connector (the wiring diagram I found said this should be black & brown, but they both look black to me)
T5 - Red
T6 - Yellow
1/4" Thermal protector tab - Grey (from the harness)
The new motor switch had a grounding tab with nothing connected to it. I removed the screw holding that tab into the switch and connected the (also grey) OEM short ground wire from the motor frame to the mounting bracket.
I had to cut 2 of the pieces of tape holding the OEM wiring harness together in order to get enough slack for all the connections to reach. If you do this too, make sure all the wires are still clear of the moving parts and the hot bits. You may need to retape the wires together at a different location to keep things tidy.
I also laid the belt over the drum and put 2 pieces of tape over it to hold it in place while I got the drum positioned, then I reached through the back access panel to loop the belt around the motor pulley and idler. Once that's done, just reach over the top of the drum and peel the tape off. I found that much easier than trying to loop the belt by reaching through and past the drum.
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Much noise when drying clothes.
Installation of drum support kit was difficult because my snap ring pliers would not fit in the snap ring holes. Had to use pliers and screw driver to get them off and to put them back on. That took much patience and time. Installation of front guides was a bit difficult because the rivets were loose and turned when trying to drill them out. Also they were bigger and I needed a larger drill bit than the 1/8 told about in the video. Used drill, screw driver and pliers to get the rivets out. Also took more time and patience to do this. Belt did not need replacement but felt it a good idea to do it as long as I was in there. Belt installation was easy because my dryer has a rear view opening and I could use it to thread the belt. Tried it from the front as shown in the video just to see if I could and found it impossible. Could not even get my hands to hold the belt. Also vacuumed out 20 years of lint and dust that was inside the dryer. The videos were excellent in showing what to do and how to do it. Not sure how well I would have done without them.
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- Customer:
- Alan from Pacific Palisades, CA
- Parts Used:
- WP33002970
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
lint filter was frayed
used a utility knife to open the box in which the part was shipped, discarded the old filter and inserted the new one
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- Customer:
- CHUCK from HARDIN, KY
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
ignitor failed to ignite gas or would fail to after first ignition.
Watched youtube video to problem shoot. Cause determined to be coils bad. Searched web found Parts Select to be easiest site to deal with and had coils for best price. Followed instructions supplied with parts. Dryer works like new.
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- Customer:
- Jodel from SAN DIEGO, CA
- Parts Used:
- 279834
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Screw drivers
Heat up then gas flame shuts down after 5 or so minutes igniter glows again trying to reignite but no gas supply coming out of the tube.
I ordered the top 5 items that may cause this problem based on the troubleshooting guide presented by the technicians I found in youtube. I replaced the coils and that fixed the problem. The coils are the first to go out according to techs, but I have the other parts just in case I may need them later on. My Maytag dryer which is over 19 years old is alive and working again. The coils are accessible from the bottom access panel secured by 2 nut screws, unplug the dryer first, then the coils are secured by a bracket with 2 small philips head screw, I used a stubby philips screw driver to remove the bracket, undo the 2 electrical connectors on the coils one with 2 prongs and the other with 3 prongs. Put the new coils attached the electrical connectors and secured them with the bracket. Checked for any loose wiring ensuring connectors are secured in place, then test run the dryer with the panel off so you can see the if the flame stays on, if you run the dryer without wet clothes the flame may stop after 15 or so minutes. It is better to test run the dryer with wet clothes just like when your drying fresh washed and wringed clothes. It was really easy, good luck!
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