DG26CA Maytag Dryer - Instructions
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- Customer:
- Conrad from CHESAPEAKE, VA
- Parts Used:
- W10169313
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Dryer No longer shuts off When Door Opened
All you need for a Maytag is a snub nose Philips screw driver. The screws on the front panel are at the bottom angled down, so a regular length Phillip's won't work. Just unscrew the 2 screws, then lift the panel up and out. Careful not to pull out too far, there are 2 wires attached to the switch. The replacement switch is NOT an exact copy of the old one. My Maytag is over 30 years old and it only had 2 prongs on the switch. The new one has 3. Don't let that throw you. It is the same size. Just attach, 1 wire to the bronze connector & the other to the silver. Push the switch into the door opening, re-attach the door. Total time 20 minutes. Saved well over $100 in a service call. Anyone with an IQ above freezing can do it.
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- Customer:
- Robert from Somers Point, NJ
- Parts Used:
- WPY312959
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Dryer tumbler did not turn, dryer still turned on, dryer still produced heat : diagnosis broken tumbler belt..
I looked for dryer repair videos on my computer. I found several and they all showed me that what was most likely broken was the tumbler belt. I didn't even know dryers had a belt. My dryer still turned on,and still produced heat. It just wouldn't rotate. One of the videos even used the exact Maytag dryer in their video that I had. After watching it a few times, I knew I could make this repair. I am pretty good at fixing things if I can first see it done. I had never taken a dryer apart before though. I pulled the dryer away from the wall and unplugged it. I unscrewed the small access panel on the back of the dryer. This let me see the two belt pulleys back there. Then I went to the front and removed the two screws(my particular model) that held the front panel on and removed it. I then unscrewed the four screws holding on the front face plate in front of the tumbler. Next, I pulled the tumbler out, it is not screwed in. There was the broken belt. It took two days with regular shipping for the belt to come in. I put the tumbler back in, resting it on its two supports, placed the belt on, flat side down, and routed the belt through the pulleys in the back of the dryer exactly as it had been shown in the videos. I turned the tumbler clockwise two full rotations by hand to make sure the belt was seated correctly on the pulleys, and it was. I then screwed the face plate back on in front of the tumbler, put the front panel back on and screwed it in. I then reattached the back access panel. I plugged the dryer back in and turned it on. It worked. Though it may take a bit longer, this type of repair is about as easy as replacing a broken belt on a vacuum cleaner even for someone who has never done a dryer repair before. Watch a Repair Clinic video and if you enjoy fixing things, replacing a belt on a clothes dryer will be your next successful repair. It really is pretty easy.
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Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
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- Customer:
- John from COHUTTA, GA
- Parts Used:
- WP6-3129480, WP6-3051850, WP314820, WP312535, W10410999, 306508, 12001541
- Difficulty Level:
- Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Dryer would not start
This website is awesome. After imputing my dryer model I was able to select from the list if symptoms my issue...Dryer will not start. From there was percentage of issues that would cause my issue. After determining it was the motor (after 25 years who would have thought that!!!). In this process I discovered other non related issues that i should attend to. So I basically rebuilt the dryer and it worked right away. I am retired military and in the tax preparation/representation business now, so a lot of this was new to me. The detailed instruction and especially the videos provided foolproof methods to complete each of the repairs. It was a little time consuming but very easy to complete. I did gain some new tools and diagnostic equipment that will come in handy in the future. Now I am going to tackle my daughters dishwasher. Thank you Parts Select and Steve (on the videos). John Beazle
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- Customer:
- Alan from BETHESDA, MD
- Parts Used:
- WPY312527, WP6-3037050, WP6-3033630
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
After a period of the dryer not being used, the idler pulley wheel froze up on the shaft of the idler pulley arm.
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.
That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.
Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.
So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.
The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.
The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.
Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.
Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
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- Customer:
- Benjamin from Baton Rouge, LA
- Parts Used:
- WP6-3037050, WPY312959, WP314820, 12001541
- Difficulty Level:
- Really Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
Very noisy.
My first attemp was to replace the drum roller and idler roller, drive belt, and the felt seal for the back, since I had experience replacing these on an older machine many years ago. The dryer was very easy to work on....After installing the new parts, I reassembled and discovered it still made the same loud noise. I then, disassembled for the second time to discover the blower wheel was worn out; so i ordered another blower wheel and a drum support roller (i only ordered one the first time.). After reassembling it made an annoying high pitch sound. I attributed that to the new parts...probably the new belt and new felt seal. Gave it some time to run-in and it seems to have quieted down. Overall, i found the dryer very easy to work on. I actually found the felt seal the most onerous to install....needed to have about three hands to get the drum back in place! I just wish that the stamped metal dryer housing didn't have such sharp edges. I had to be very careful to avoid sharp burrs but still got nicked a couple of times.
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- Customer:
- Joseph from Colts Neck, NJ
- Parts Used:
- W10169313
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Replaced door switch
Door switch was very easy to replace as it simply snaps in for the outside and you just clip on the two control wires that already have clips on them.
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- Customer:
- Jeffrey from Glenshaw, PA
- Parts Used:
- 4391996
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Wrench (Adjustable)
Dryer not heating....Had to be igniter or solonoid
Upon receipt of part, just loosened 1 fastener, slid igniter forward and out....unclipped wire connection and replaced... Could not have been easier. Be careful not to overtighten fastener when replacing. Description and pictures made for very easy selection.
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- Customer:
- David from Manhattan, IL
- Parts Used:
- MAL9000AXX
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Switch Samsung dryer (w/ Maytag gas valve) to LP
The directions provided to modify the gas valve were very clear. Getting to the gas valve I was on my own. Taking the top and the face off the dryer, once I figured out that there was no reaching the gas valve from any of the access ports on the back, was the only way to access to the gas valve. If you have worked on any other dryers, this modification was definitely doable.
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- Customer:
- William from Springfield, OH
- Parts Used:
- WP6-3129480, WP312535, 12001541, WP9703438
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
One of the roller shafts was worn
Replaced both rollers,shafts, bearings and snap rings.
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Squeaking noise
I had replaced belt, but the noise continued. Ordered new rollers and washer. Removed the front panel by tipping the dryer back against the wall and removing two screws at the bottom of the panel. Tipping the dryer makes it easy to remove the front panel. Removed the front drum support by removing four (4) screws. I was then able to just move the drum enough to have access to the rollers. Didn't even have to remove the belt. Replaced the rollers. Needed special pliers to remove and replace the retaining rings. Put the drum back into position and mounted the front drum support. Tightened four screws and then put the front panel back on. Plugged it in and tested it. Problem solved. Took about 35 minutes. Thanks
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- Customer:
- Loretta E. from Miamisburg, OH
- Parts Used:
- W10169313
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Button to start dryer
Per instructions I printed off online: took off door, then the front panel. Pulled out the old switch/button, connected the new switch/button, made sure the new button was working; put the panel back on then the door and DONE!
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When the dryer grumbles check the blower wheel too.
If your dryer is making a rumbling noise, change the blower wheel. It's plastic and the heating and cooling cycles causes the keyway in the plastic to give out and the wheel just spins causing the noise and the slower dry time. The other parts I replaced see below. Like many other repairs, remove screws below dryer door. Mark all wires and locations for re-assembly. Next remove front tumbler/lint screen assembly (4 sheet metal screws 2/L 2/R. Work belt off back of tumbler and remove. Use flathead screw driver to release tabs that hold felts on both front and back tumble supports. Make sure you know rotation of tumbler and install new felts so the overlap goes in direction of spin. Use a drum stick or 3/8 ratchet extension, something dull and flat to press tabs back down on felts. A screwdriver could slip off and tear cloth. Next drill out heads of the rivets on the glides and remove teflon glide and cork backer. Make sure all rivet material is removed front and back. Install new cork and glide. Rivet one side back in, then the other. Repeat on 2nd glide. Re-assemble dryer. Super smooth, super quiet.
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- Customer:
- Horacio from Houston, TX
- Parts Used:
- 4391996
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set, Wrench set
Not enough heating to dry clothes.
My Maytag gas dryer model MDG7600AWW is about 12 years old. Everything else works fine except it takes 4-5 drying cycles instead of 1 to completely dry my clothes properly. The flat igniter was simply cracked but not broken so it only worked some times. My gas dryer igniter and the 2 ignition coils work hand in hand so I replaced all 3 parts. The ignition coils provide a solid and consistent power supply to the igniter for proper burner tube function. Disconnect power cord from wall outlet. Shut off gas supply by turning the wall gas valve off. Remove 2 small philips screws to detach front panel door from dryer frame. Remove 2 additional philips screws on left front side panel inner door frame. Gently pull front dryer panel off beginning at top and put it aside. Igniter and the 2 ignition coils are plainly visible and easily accessible at bottom right corner of dryer. Igniter is attached to the burner tube and facing into the heater housing assembly. The 2 ignition coils are attached just above the gas valve on the rear of the burner tube. The ignition coils are simply attached to the rear of the heater tube with one bracket using 2 small philips screws. First, disconnect igniter plug wire harness. Next, I recommend using a small open end applicable size wrench (5/16 perhaps) to remove attaching igniter screw. A small 1/4 ratchet with applicable socket size may also be used. Handle the igniter only from the white ceramic part when installing. You don't have to completely remove the igniter screw from the burner tube. The igniter has a white ceramic horse shoe shape slot in which the attaching screw goes through for tightening to the burner tube. Just unscrew generously for removal and replacement of the igniter. Do NOT over tighten igniter screw as the white ceramic plate may break from over torqing. Reconnect igniter wire plug harness. The igniter part I used was PartSelect Number PS373025. Next, remove the ignition coil bracket by unscrewing the 2 small philips screws from rear of the heater tube frame. Remove only 1 ignition coil at a time by removing the wire plug harness and simply lifting upward. One coil will have 2 prongs while the other has 3 prongs so you can't go wrong when reconnecting the wire plug harnesses. I used the PartSelect 'M' Series New Style Coil Kit (2 coils included)which was PartSelect Number PS334310. Replace the front dryer panel back. Attach the front door to the panel and dryer frame using the 2 philips screws. Attach the 2 left side inner door front panel philips screws to dryer frame. Turn on the wall gas valve. Reconnect power cord to wall outlet.
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- Customer:
- Robert from Sacramento, CA
- Parts Used:
- WP33002970
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
I relaced our worn out lint filter
My part was not amazing. What was genuinely cool: I ordered it one day and it was here the next, took out the old and put in the new. Thanks for getting it here so quickly.
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