GDE8300 Maytag Dryer - Instructions
Jump to:
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
- Customer:
- Kevin from San Diego, CA
- Parts Used:
- WP6-3129480, WP9703438, WP33001443, WP312535, 12001541
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
drum support roller was squeaking
My 11 year old grandson and I did the repair together. He had a blast and I did too. First we removed a bunch of screws that got us no closer to getting the machine apart than when we started. Then I remembered from the last time I had the machine apart that there are two screws just below the door, angled as not to be visable unless you know where to look. Once we removed those the from came off. We removed the wires for the door light and heat sensor, remembering the order of the wires for later reinstallation. Then we undid the bolts holding down the top. Once the top was removed we took off the belt and removed the drum. We used the retainer pliers to remove the retainer ring from the first roller. We removed the roller and also the shaft as this roller was the noise maker and the shaft was not in reusable condition. We installed a new shaft, roller washer, roller, another roller washer and then the retainer ring. We repeated the same process on the other roller, although we did not replace the shaft as it was in good condition. It turned out I did not need to order the shaft washers as the rollers came with washers. Oh well, its not a good job unless you have parts left over when you are done. Once we replaced the rollers we commenced reinstallation. But first we had to google for diagram of the proper belt installation, which we found and that got the drum and belt installed properly. Thankd god for the internet. Once we had the drum installed we put the machine back together in the opposite order we took it apart. An operational test showed we did the job right, no more squeaking. The only injury was my grandson cut his thumb right after I gave him the speech about watching where your hand is going to end up when that bolt breaks free. It broke loose and into the metal bracket went his thumb. Oh well it was a good lesson and it was not a bad cut. All in all a good repair.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Jeff from Gardendale, AL
- Parts Used:
- WPW10116756
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
idler pulley, idler bracket, idler spacer & Belt worn from age
First I unplugged the machine; an essential to avoiding getting shocked during this repair. This is a must and should not be overlooked it could cost you your life.
Removed two screws from lower area of front panel, pulled bottom of front panel toward yourself so as to swing out and up, continue to swing panel up to your self until it comes free from top clips.
Once free set gently on floor and remove door switch wires, noting which wire goes to which contact is not essential but could be more convenient when putting it all back together.
Remove door switch wire from clasp at top inside from panel, set front panel aside in safe place.
Now look under the two top front corners on the inside and you will see a screw in each corner; these screws must be removed in order to raise top panel.
This is kind of tedious because sometimes these screws are long and difficult to turn and space is limited and tight in getting rachet or nut driver on the head of these screws.
Be patient , because they will come out with a little work. To make this process a little easier you might do the following step first but you cannot do this little trick when putting it back together.
Once these screws are out raise top panel and lean back against wall; be careful because the two enamel surfaces are slick and if leaned too far back the top will want to slide out at the bottom from being on a lean.
Remove four screws from tumbler front, lift slightly so as to come off side clips then pull straight out. Remove door wire from clasp and drop wire gently back inside so as to let it fall to the bottom of the machine and away from the tumbler, which is to be removed next.
Once this is done the tumbler will go down in the front due to pressure from belt. The belt could have been removed from pulley right from the start to relieve this tension but I just do it this way.
Once tumbler sags or leans down in the front gently work the belt off of the back of the tumbler; there will still be a little pressure on the belt and gentle force may be required in sliding it toward the back and then off; once belt is off gently lift tumbler up and out and put in a safe place.
Once this is done you will be able to easily see everything in the bottom of the dryer; motor, gas valves, thermal switches, vent pipe and pulley, pulley bracket and belt which by this time has fallen to the bottom of dryer; gently remove belt from pulley and set aside in safe place.
Make sure it is out of reach of children or it will be played with or used as a hangmans noose; it is long an flexible and children just seem to love playing with it.
At this point you can either continue to work from the front of the machine or the back; I f you choose to work from the back then lower the top panel so as to allow it to just sit back down on the sides of the machine, pull the machine away from the wall and work from the back; because I am experienced at this I continue to work from the front.
If you choose to work from the back then while standing in the back of the machine look to lower right corner and you will see an access panel with four screws in it; remove these screws and the panel will come free giving you a clear view of the belt pulley.
From either back or front view you will see a spring attached to pulley bracket which can easily be removed when pulley bracket is in relaxed position; remove this spring and put in a safe place if you have plans of reusing it. I installed a new spring on this repair.
Once this spring has been removed then look directly beneath bracket at what is easily seen to be its pivot point and you will see a mounting screw. Remove this screw with a nut driver and the bracket will then come completely free; slide through access hole and come out with it.
Once it is out the white spacer is easily seen on bracket; look at the bracket side of the spacer and you will see a mounting screw; remove this screw and spacer will come off.
When installing new space
Removed two screws from lower area of front panel, pulled bottom of front panel toward yourself so as to swing out and up, continue to swing panel up to your self until it comes free from top clips.
Once free set gently on floor and remove door switch wires, noting which wire goes to which contact is not essential but could be more convenient when putting it all back together.
Remove door switch wire from clasp at top inside from panel, set front panel aside in safe place.
Now look under the two top front corners on the inside and you will see a screw in each corner; these screws must be removed in order to raise top panel.
This is kind of tedious because sometimes these screws are long and difficult to turn and space is limited and tight in getting rachet or nut driver on the head of these screws.
Be patient , because they will come out with a little work. To make this process a little easier you might do the following step first but you cannot do this little trick when putting it back together.
Once these screws are out raise top panel and lean back against wall; be careful because the two enamel surfaces are slick and if leaned too far back the top will want to slide out at the bottom from being on a lean.
Remove four screws from tumbler front, lift slightly so as to come off side clips then pull straight out. Remove door wire from clasp and drop wire gently back inside so as to let it fall to the bottom of the machine and away from the tumbler, which is to be removed next.
Once this is done the tumbler will go down in the front due to pressure from belt. The belt could have been removed from pulley right from the start to relieve this tension but I just do it this way.
Once tumbler sags or leans down in the front gently work the belt off of the back of the tumbler; there will still be a little pressure on the belt and gentle force may be required in sliding it toward the back and then off; once belt is off gently lift tumbler up and out and put in a safe place.
Once this is done you will be able to easily see everything in the bottom of the dryer; motor, gas valves, thermal switches, vent pipe and pulley, pulley bracket and belt which by this time has fallen to the bottom of dryer; gently remove belt from pulley and set aside in safe place.
Make sure it is out of reach of children or it will be played with or used as a hangmans noose; it is long an flexible and children just seem to love playing with it.
At this point you can either continue to work from the front of the machine or the back; I f you choose to work from the back then lower the top panel so as to allow it to just sit back down on the sides of the machine, pull the machine away from the wall and work from the back; because I am experienced at this I continue to work from the front.
If you choose to work from the back then while standing in the back of the machine look to lower right corner and you will see an access panel with four screws in it; remove these screws and the panel will come free giving you a clear view of the belt pulley.
From either back or front view you will see a spring attached to pulley bracket which can easily be removed when pulley bracket is in relaxed position; remove this spring and put in a safe place if you have plans of reusing it. I installed a new spring on this repair.
Once this spring has been removed then look directly beneath bracket at what is easily seen to be its pivot point and you will see a mounting screw. Remove this screw with a nut driver and the bracket will then come completely free; slide through access hole and come out with it.
Once it is out the white spacer is easily seen on bracket; look at the bracket side of the spacer and you will see a mounting screw; remove this screw and spacer will come off.
When installing new space
Was this instruction helpful to you?
Thank you for voting!
Loud rumbling noise when dryer operates
Frist I removed the front cover panel via removing 2 screws. Second I disconnected the door switch wires. Third I removed the 4 screws that hold the drum onto the rollers and guides that allows access to the blower wheel assembly cover. Fourth I remover the blower wheel assembly cover to gain access to the blower wheel. Fifth using the retaining removal tool removed the retaining ring from the shaft then removed the blower wheel using plyers. Then reassembled all of the parts and enjoy a quiet dryer again.
Thank you parts select!!!
Thank you parts select!!!
Was this instruction helpful to you?
Thank you for voting!
Dryer Would Not Heat, Noisy Tumbler
First step was diagnosis. I unplugged the dryer and removed the front panel to access the heater. I disconnected the push on terminal at the heater over temp sensor and tested heater for continuity using a dvm. No continuity meant the heater element was bad. I visually inspected the tumber belt and found it to be split. I ordered the parts heater element and belt from partselect on a thursday at 2:00 pm. I received notice that they shipped the same day! Fedex delivered the parts by saturday. It took me about an hour to remove the heater and replace the element (its the 2nd replacement in 28 years) and about another hour to replace the belt and do a general cleaning of the dryer interior. All in all, it was a fairly easy repair (for a technically inclined guy).
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Richard from Anchorage, AK
- Parts Used:
- W10410999
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
dryer was making a squealing noise on start up then the drum would not turn at all.
First I unplugged the dryer. Then I removed the two phillips head sheet metal screws near the bottom of the front panel at either side, swung the panel out from the bottom until it unhinged at the top for removal. I disconnected the wire to the door switch and placed the front panel out of the way. Next I unbolted the top from the side panels by removing the single bolt at the front top of each side panel. This allows the Top panel of the dryer to be raised enough to remove the drum. I slipped the drive belt off the back of the drum, lifted the top a few inches and removed the drum. Next I removed the face plate of the blower channel to get at the squirrel cage blower and disconnect it from the motor by removing the outer snap ring from the motor shaft and then used pliers to remove the spring clip from the hub of the blower cage allowing it to slide off the shaft. There was a second snap ring to remove behind the hub. With the blower off the 3 screws holding the blower channel to the motor mount were accessable and able to be removed along with a couple of scews holding the air channel to the dryer base allowing the whole assembly to be moved out of the way to get at the motor. Two more screws at the motor base were removed to free the motor. Three color coded wires were unclipped from the motor and it was out after removing the drive belt from the pulley. Getting the pulley off the old motor after 29 years of service proved to be the most difficult part of the repair. Had to heat the pulley with a propane torch until the glue holding the allen head set screw decomposed enough to allow me to break the set screw loose. Releasing the spring clips holding motor to frame was easy using a large screwdriver to push down in the end recess of the clip while prying against the frame. Reassembly took less than an hour. The color coded dots on the electrical connector block were identical to the original motor making the electrical reconnection a snap (These dots were clearly seen in the photos of motor on the PartSelect website so I knew I had the right motor). The drive belt reinstallation was a little tricky as you have to spool the belt correctly around the pulley then put the drum back in 3/4 of the way and start the belt on the back of the drum and work it forward about 5 inches to its running position. Rest was easy, no parts left over and it works like new again.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Scott from Palm Bay, FL
- Parts Used:
- 306436
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Dryer door latch broken, using duct tape every time to dry clothes.
Piece of cake. Used flat screwdriver to pry out female part on cabinet side, same with the male part on door. Every new replacement part was tight and operated like new. Thanks Part Select, you'll be forever on my list of online parts buying.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- John from Midway, GA
- Parts Used:
- WP307473
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Dryer would not turn start
I troubleshot the repair using the repair help section from Parts Select. It made finding the problem a snap. I then removed the four wires and two screws that held the heating element in place. Removed two screws that held thermal fuse in place and replaced. By accomplishing the repair myself I saved well over a hundred dollars.
Was this instruction helpful to you?
Thank you for voting!
Heater element burned out in dryer.
Had replaced the heater element a few week earlier under the thought that it had failed just because the dryer was old. But shortly after replacing the element the dyrer started making a lot of noise when started. A few dryer loads later the hearte element had faild again.
The design of the Maytag Dryer makes most repairs easy. The machine is very well made.
Since I was investigate the noise that the dyrer was making, I did a complete teardown of the dryer to check things out. Fould that the drum drive belt was old and the blower fan had spun off the locking tab and also that the heater element was burned out. again. Did a complete check of all moving parts and orded the parts that needed to be replaced. Did a clean up of all old lint in the dryer vent system and fan unit. The fan and belt parts were easy to replace. The heater element does take time and care when working with the ceramic holders. But since I had done it before I did not find any surprised.
The dryer works like new now. Just hope none of the sensors or ideler wheels give out.
The design of the Maytag Dryer makes most repairs easy. The machine is very well made.
Since I was investigate the noise that the dyrer was making, I did a complete teardown of the dryer to check things out. Fould that the drum drive belt was old and the blower fan had spun off the locking tab and also that the heater element was burned out. again. Did a complete check of all moving parts and orded the parts that needed to be replaced. Did a clean up of all old lint in the dryer vent system and fan unit. The fan and belt parts were easy to replace. The heater element does take time and care when working with the ceramic holders. But since I had done it before I did not find any surprised.
The dryer works like new now. Just hope none of the sensors or ideler wheels give out.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Terry from Livermore, CA
- Parts Used:
- 33001012
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver
My son broke a short baffle drying out his work boots
The repair was very simple. I took off the two screws on the fron of the dryer to remove the front panel which gained me access to the drum. I used a nut driver to remove the two screws that held the orignal short baffle and screwed in the new short baffle. Very simple very quick. The amazing thing with this problem is that I ordered the part on Thursday and recieved it on the very next day!!!!!!
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Joseph from Hampton bays, NY
- Parts Used:
- Y303836
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Noise in dryer
How to disassemble the dryer has been covered in past repair stories. I will add a make shift repair that will get you up and running until you get your replacement blower wheel. We repair gas dryers for a living and this repair works and some machines are still running for two years. Remove the blower wheel. Cut a piece of plumber strap of similar sized metal to about 3/16" x 1/2". Hold it with vise grips and then heat it with a torch. When it is hot melt it into the hole in the blower wheel. This will give you a flat spot in the shaft hole that will keep the blower from spinning on the motor shaft. Some trial and error fitting is involved. If you do it carefully the blower wheel will fit very nicely and will not vibrate or make noise.
Was this instruction helpful to you?
Thank you for voting!
noisy operation and then no heat
First I removed the two screws near the bottom of the front panel. Then I removed the front panel by rotating it outwards. Next I removed the front frame section by removing the four screws. The tumbler rests on this frame piece so remove it carefully and it will stay put - no need to take it out. The grinding noise I was hearing was the tumbler (drum) running on the frame - the glides (bearings) were worn out. This had generated piles of metal powder which I vaccumed up. It was easy to locate the reason there was no heat - the thermostat was burned to a crisp. It torched part of the blower seal in the process. The reason the thermostat fails in this manner is the lint duct gets clogged up increasing the duty cycle of the heater which fries the thermostat. I had to strip back the red wire and install a new blade connector but the thermostat just bolts on easy enough. You'll need a rivet gun to replace the glides. Drill out the old rivets and pull them out with some pliers. Easy enough to do and it runs like new! Good luck.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- David from Apopka, FL
- Parts Used:
- Y303778
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers, Socket set
Dryer runs but never heats
Googled Maytag dryer troubleshooting and arrived at partselect.com. Using their site, I was able to learn more about how my dryer operated, was configured and how to remove the front panel. I then removed front panel. Tested fuses and thermostats. All were good. Visually inspected heater element. No apparent break in heater coils. I ultimately removed the heater assembly to get a better view of the heater element and then noticed the break in the heater element. Once I saw that it was obvious where my problem was. I then ordered the part, installed it and tested it and it appeared to work fine. My wife tells me it works great and she is impressed. FYI - I don't know much about dryers except that it drys my clothes. Thank you partselect.com!
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- John from College Place, WA
- Parts Used:
- WPY313538
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
The Dryer no longer would heat to dry the clothes
I first unpluged the dryer, then I removed the front cover of the dryer. The Heating unit in located in the lower right side of the machine. I unscrewed the heating "tube" from the dryer and unpluged it from the dryer. ( good idea to mark the wires because they are same color.) I unscrewed the two halves of the heating unit and saw that indeed the heating coil was broken. I unscrewed the coil and fed it through the insulators. The coil was old and uncooperative, so I decided to cut it at each insulator with wire cutters. This sped up the process and protected the insulators. I carefully fed the new coils through the insulators and attached the ends to the terminals. Be careful not to over tighten or you may break the insulation on the terminals. I reinstalled the heating unit and attached the wires and tested the dryer. Job Done! Thanks Parts Select!
Was this instruction helpful to you?
Thank you for voting!
My Blower wheel had broken at the center where it attached to the axle. It made a rattling sound and no air was being blown into the drum to dry the clothes. There was also a loud skidding sound that turned out to be due to a worn felt seal.
I took off the front of the dryer with the screws at the bottom. I removed what wires would easily come off and took a picture to remember where they go. Then I took of the front panel and had to take off the cover for the blower wheel. Some screws were difficult to reach because they were in a very tight space. I used a combination of needle nose pliers and a hex screw bit to loose hared to reach hex screws.
For the felt seal on the front panel, I used a flathead screwdriver to remove the old seal and replace the new seal. The most tricky thing was making sure the seal was laying right along the drum when putting the front panel back on. Once back together, the skidding sound disappeared.
Replacing the blower wheel is pretty easy once I got past the difficult screws holding the cover down. I used snap ring pliers to remove the snap ring then put the new blower wheel on and put it all back together. I found that the tip diameter of the snap ring pliers needed to be less than 0.05'' to fit into the snap ring holes of both the snap rings for the roller wheels and the blower wheel.
For the felt seal on the front panel, I used a flathead screwdriver to remove the old seal and replace the new seal. The most tricky thing was making sure the seal was laying right along the drum when putting the front panel back on. Once back together, the skidding sound disappeared.
Replacing the blower wheel is pretty easy once I got past the difficult screws holding the cover down. I used snap ring pliers to remove the snap ring then put the new blower wheel on and put it all back together. I found that the tip diameter of the snap ring pliers needed to be less than 0.05'' to fit into the snap ring holes of both the snap rings for the roller wheels and the blower wheel.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- william from salt lake city, UT
- Parts Used:
- WP33002970
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
lint filter was old and had hole in it
ordered new filter,,,,
Was this instruction helpful to you?
Thank you for voting!