MLE19PDDGW Maytag Dryer - Instructions
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- Customer:
- Melissa from Cedar Rapids, IA
- Parts Used:
- WP33001755
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
The short baffle came loose and was rattling around in the dryer.
The repair was easy, based on the comments from this website. I used a 6-in-1 screwdriver, and that was the only tool. I removed the two screws holding the hinges, removed the door, then the two screws on the opposite side of the opening. This allowed the front panel to come off. I spun the dryer tumbler until the baffle that was loose was at approximately 5 o'clock. I unscrewed the remaining screw and found the missing screw in the bottom of the dryer. I put those two screws into the new baffle, and popped the front back in place. I reinstalled the four screws (two opposite the hinge, then the two that hold the hinges)...all done in about 20 minutes (including vacuuming the lint out from that lower area).
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- Customer:
- Nova from Hudson, OH
- Parts Used:
- WP303396
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers, Socket set
Broken contact on high limit thermostat - dryer no start
First I unplugged the dryer! Then unscrewed the two screws at the bottom of the front door. To remove the front door, swing the bottom up about 30 degrees until the two triangular hooks at the top of the door release. Then release the two wires going to the door switch from their harness so as to gain more slack to move the door out of the way. The switch was secured by 2 hex head sheet metal screws1/4inch in diameter. I used a small right angle socket wrench to get these loose. I only had to remove the front screw completely to be able to take the switch out for exchange purposes. Once this was done, reverse the process and plug it in! (BTW, the electrical schematic for this dryer is up under the top console)
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Seal failure, leading to bearing failure
Not much to add to others' descriptions of the repair except for two things- one, the procedure for removing the front shroud on a stackable unit is somewhat different than what is described in the seal kit directions. The door switch assembly gets in the way; though the whole repair can be done by one person, it would be better (and safer) to have a second person helping at least during this part. The whole shroud is unwieldy, with two drain hoses attached, along with two dispenser hoses, the door switch/light, and the side & bottom mounting brackets, and it has to be eased out one step at a time. During the last part of this you will have to lift up the front of the dryer at the same time.
Second, our particular washer has a 90xxxx serial number. The bearings are Chinese-sourced, not the good NSK bearings. Though the listed bearing numbers are the same... the rear bearing is held in by a retainer that is permanently fixed into the outer tub. There is no easy way to drive the bearing forward, either, as the retainer covers nearly all the bearing outer shell. The chances are very high that the outer tub would be damaged beyond repair if the retainer or bearing was removed. Fortunately in this washer, the back bearing was still in reasonable shape and had some grease left; I was able to pop out the grease seal and re-pack it with wheel bearing grease. The front bearing & seal are replaced as others have described. The front bearing takes a majority of the load, so others may have similar wear.
This washer was only 3 1/2 years old; we bought six Maytag appliances at the same time, and four of the six have had major repair problems (two were cheaper to replace than repair). That, and the $678 replacement cost of the outer tub, explains why the Maytag repairman is so lonely...
Second, our particular washer has a 90xxxx serial number. The bearings are Chinese-sourced, not the good NSK bearings. Though the listed bearing numbers are the same... the rear bearing is held in by a retainer that is permanently fixed into the outer tub. There is no easy way to drive the bearing forward, either, as the retainer covers nearly all the bearing outer shell. The chances are very high that the outer tub would be damaged beyond repair if the retainer or bearing was removed. Fortunately in this washer, the back bearing was still in reasonable shape and had some grease left; I was able to pop out the grease seal and re-pack it with wheel bearing grease. The front bearing & seal are replaced as others have described. The front bearing takes a majority of the load, so others may have similar wear.
This washer was only 3 1/2 years old; we bought six Maytag appliances at the same time, and four of the six have had major repair problems (two were cheaper to replace than repair). That, and the $678 replacement cost of the outer tub, explains why the Maytag repairman is so lonely...
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- Customer:
- Laurence from Leesburg, VA
- Parts Used:
- WP6-3129480, 12001541
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers, Socket set
Rattling sound.
Turned off circuit breaker. Removed two screws at base of front panel with stubby Phillips-head screwdriver. Swung panel up about 30-degrees, and removed panel, disconnecting red and yellow wire to door switch. Removed four sheet metal screws and took off large drum support bracket. Checked drum support rollers and shafts. They were fine. Reset circuit breaker and turned on dryer. Rattling noise still present.
Removed six small screws holding blower fan assembly. Shaft receiver on squirrel cage fan was worn completely round (it should fit onto a half-round shaft). Ordered new blower fan from PartSelect.com. Replaced tonight, and it works beautifully. This dryer is 29-years old. All it's ever needed in the 10-years I've owned it is a belt replacement and this repair. Long live the 1970s Maytags, and good parts suppliers like this one.
Removed six small screws holding blower fan assembly. Shaft receiver on squirrel cage fan was worn completely round (it should fit onto a half-round shaft). Ordered new blower fan from PartSelect.com. Replaced tonight, and it works beautifully. This dryer is 29-years old. All it's ever needed in the 10-years I've owned it is a belt replacement and this repair. Long live the 1970s Maytags, and good parts suppliers like this one.
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- Customer:
- Pam from Aberdeen, WA
- Parts Used:
- 12001541
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers
Dryer was making awful noise during use
Removed the screws and took the door off then took the front panel off and popped up the top. Then pulled the drum out. Took snap ring pliers and removed rollers and replaced with new rollers then vacuumed all lint from machine and reversed operation to put everything back together. Operation was a total success!
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- Customer:
- Lisa from Trenton, NJ
- Parts Used:
- WP6-3705180, WP6-3700340, WPY312527, WP354987
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
Dryer made very loud squealing, screeching noise. (Sometimes Intermittent, sometimes constant)
Note: You may want to consider replacing the 2 Drum Support rollers at this time (while your in there)
1. UNPLUG YOUR DRYER FIRST.
2. Using a phillips head screw driver - Remove 2 screws that secure the dryer door hinges to the frame, Lift door very slightly to unhook hinges and pull out door with hinges attached as straight as possible, set aside. Remove the 2 plastic tabs from the opposing side of the door hinge also secured by screws.
3. Remove the front panel (panel is shaped like a football goal post) by tilting out the top ends of the front panel toward you, then lift up to remove panel from the bottom metal retaining tabs.
4. Remove the 2 hexhead screws from the 2 retaining clips (security hooks) that secure the top
of the dryer closed.
5. Systematically remove the hexhead screws from the rest of the front of "shroud" (it holds (suspends) the drum in place between the front and back of the dryer).
*** I didn't disconnect any wires, I carefully swung out each piece that had wires attached, propped up those parts vertically ensuring no strain on the attached wires. Others may want to disconnect wires to avoid breaking or damaging them.
6. Vacuum out any dust/lint that may be present.
7. Draw a quick diagram of how the underside of the belt is threaded on the idler pulley and motor pully first. Release the tension of the belt from the underside of the drum. The easiest way is to push the idler pulley arm away from the belt and slide off the belt from the idler pulley and motor pulley. Slide the drum out.
8. Remove the hexhead screw from the bottom of the idler arm. Disconnect from retaining spring.
9. You may only need to replace just the Idler Pulley Wheel. I recommend replacing as a "unit" the Idler Pulley Wheel, Idler Arm, Ring-E and Idler Shaft Washer(s) - then you can just swap out the old one for the new one.
10. Reassemble
(When reassembling the belt - place around drum first and slide drum in place. Now from the underside-place (drape) belt around the motor pulley (it will be very loose) Now push the idler pulley arm toward the motor pulley, engage the left side of the belt around the idler pulley and slowly allow idler pulley to increase its tension on the belt) You can test manually by rotating the drum by hand to ensure proper movement.)
1. UNPLUG YOUR DRYER FIRST.
2. Using a phillips head screw driver - Remove 2 screws that secure the dryer door hinges to the frame, Lift door very slightly to unhook hinges and pull out door with hinges attached as straight as possible, set aside. Remove the 2 plastic tabs from the opposing side of the door hinge also secured by screws.
3. Remove the front panel (panel is shaped like a football goal post) by tilting out the top ends of the front panel toward you, then lift up to remove panel from the bottom metal retaining tabs.
4. Remove the 2 hexhead screws from the 2 retaining clips (security hooks) that secure the top
of the dryer closed.
5. Systematically remove the hexhead screws from the rest of the front of "shroud" (it holds (suspends) the drum in place between the front and back of the dryer).
*** I didn't disconnect any wires, I carefully swung out each piece that had wires attached, propped up those parts vertically ensuring no strain on the attached wires. Others may want to disconnect wires to avoid breaking or damaging them.
6. Vacuum out any dust/lint that may be present.
7. Draw a quick diagram of how the underside of the belt is threaded on the idler pulley and motor pully first. Release the tension of the belt from the underside of the drum. The easiest way is to push the idler pulley arm away from the belt and slide off the belt from the idler pulley and motor pulley. Slide the drum out.
8. Remove the hexhead screw from the bottom of the idler arm. Disconnect from retaining spring.
9. You may only need to replace just the Idler Pulley Wheel. I recommend replacing as a "unit" the Idler Pulley Wheel, Idler Arm, Ring-E and Idler Shaft Washer(s) - then you can just swap out the old one for the new one.
10. Reassemble
(When reassembling the belt - place around drum first and slide drum in place. Now from the underside-place (drape) belt around the motor pulley (it will be very loose) Now push the idler pulley arm toward the motor pulley, engage the left side of the belt around the idler pulley and slowly allow idler pulley to increase its tension on the belt) You can test manually by rotating the drum by hand to ensure proper movement.)
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- Customer:
- Robert from Buffalo, NY
- Parts Used:
- WP694674
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Temperature setting not working
Took off back cover, thermostat was easily identified because of photos I've seen on website. Took 2 connectors off, removed 2 screws and removed old thermostat. That was pretty much it!
NOTE: Replacement thermostat 694674 has an adjustable temperature range setting that MUST be manually set prior to installing! You need to use the enclosed chart to find your original part# and make sure the setting is matched. My original part# 341146 had a "D" setting so I had to change but very easy to do.
NOTE: Replacement thermostat 694674 has an adjustable temperature range setting that MUST be manually set prior to installing! You need to use the enclosed chart to find your original part# and make sure the setting is matched. My original part# 341146 had a "D" setting so I had to change but very easy to do.
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- Customer:
- Matthew from Lombard, IL
- Parts Used:
- WP33001807
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers
Rear Felt seal came out, squealing sound when drying
Turned off gas and unplugged dryer
1) Removed bottom front panel
2) lifted top panel up like a car hood
3) Removed door springs
4) disconnected electrial connections to door unit, removed door unit
5) removed drum, scraped old felt from drum
6) glued new felt with a very strong glue (nanoglue or gorilla glue, same thing), let it dry overnight
7) secured back inside panel, replaced drum and put dryer back together.
1) Removed bottom front panel
2) lifted top panel up like a car hood
3) Removed door springs
4) disconnected electrial connections to door unit, removed door unit
5) removed drum, scraped old felt from drum
6) glued new felt with a very strong glue (nanoglue or gorilla glue, same thing), let it dry overnight
7) secured back inside panel, replaced drum and put dryer back together.
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- Customer:
- Paul from Tallahassee, FL
- Parts Used:
- 22003728
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers
Bad pressure switch on front loading washer allowed water level to exceed proper height leading to water leaking from door seal.
First I sent the local repair man away. I recieved much better advice from this forum. Partselect saved me literally hundreds of dollars. The local repair man was headed in the totally wrong direction.
After identifying the problem with the online partselect repair forum I ordered the part. It was in stock and delivered the next day.(local dealer needed 2 weeks to get the same part) The repair was fairly easy. The pressure switch sits on top of the water manifold for the pump. Removing the old pressure switch required disconnecting the connector and then pulling it free from the snap clip on the backside of the switch. After taking out the old switch I took off the pipe boot that the pressure swich inlet tube seats into. This pipe connects directly to the drain hose that runs into the manifold. I would recommend this to make sure this pipe is not clogged. The pipe needed to be cleaned as a plug of old detergent was totally blocking the pipe.( In fact this was probably the cause of the problem as no water could make it to the actual pressure switch. I had already ordered the new swith so I installed it anyway.) After cleaning out the pipe I put the boot and retaining clip back over the top of the pipe. This was the most difficult part of the repair. It took some time as the clip is very difficult to replace. From there it was just snaping the new switch into place, plugging in the connector and it was done. After putting the front washer cover back in place it was ready to go.
After identifying the problem with the online partselect repair forum I ordered the part. It was in stock and delivered the next day.(local dealer needed 2 weeks to get the same part) The repair was fairly easy. The pressure switch sits on top of the water manifold for the pump. Removing the old pressure switch required disconnecting the connector and then pulling it free from the snap clip on the backside of the switch. After taking out the old switch I took off the pipe boot that the pressure swich inlet tube seats into. This pipe connects directly to the drain hose that runs into the manifold. I would recommend this to make sure this pipe is not clogged. The pipe needed to be cleaned as a plug of old detergent was totally blocking the pipe.( In fact this was probably the cause of the problem as no water could make it to the actual pressure switch. I had already ordered the new swith so I installed it anyway.) After cleaning out the pipe I put the boot and retaining clip back over the top of the pipe. This was the most difficult part of the repair. It took some time as the clip is very difficult to replace. From there it was just snaping the new switch into place, plugging in the connector and it was done. After putting the front washer cover back in place it was ready to go.
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- Customer:
- Gregory from El Dorado, AR
- Parts Used:
- 12002022
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Screw drivers, Socket set, Wrench (Adjustable)
Bearings making loud rough noise
Thanks to all the others who gave detailed information I was able to replace the front & rear bearings and front seal. I must say it was a time comsuming job but at least I am alot clearer on the quality of clothes washing machines. I do believe I could give a manufacturer / designer some design points after working on this Maytag Neptune. I was able to knock out the bearing shaft that held the stainless perforated tumbler inside the plastic tub/drum by using a #3 LB hammer I reinstalled the old screw in the shaft which held the plastic pully on because this would keep the end of the shaft from being damaged. After several blows it started moving I was afraid I might damage the plastic drum but fortunately no damage was done to it. After removing the stainless steel perforated tumbler here is where it really got interesting. The Hub that held the old seal was shot! pretty much deteorated from corosion it seems. Here is where I could significantly help a manufactured/designer out The bearing/seal hub should have been made out of stainless instead of Pot metal/ aluminum or whatever they made it from. After much cleaning with a small wire brush and vacuming all the debree out of the Tub I didn't have much hub left to install the new seal. Also the three armed Spinner was very coroaded it attaches to the back of the stainless tumbler I removed it from the stainless tumbler and wire brushed it the back side was full of crud, it looked like left over washing powder or soap and Corosion debree it was a job just cleaning it up. I pressed on and on though replacing both bearings front and rear. Thanks to another person who explained the easy way to remove the bearings and race I was able to do so without removing the Drum/Tub as others stated they had to do. The Dremmel and a few Cutter blades did the trick I cut a wide V notch in the bearings and the bearings fell out I then cut through the bearing race being careful not to cut too deeply although if you did slightly cut beyond the race it really wouldn't matter because the front seal will keep it from leaking anyway. Anyway when I cut through the race it made a ping sound and the race pulled away and fell right out of the HuB. The front & rear bearings a definately serviceable and it doesn't have to be a beat/bang ordeal. after cleaning up the hub I tapped the new bearings in place and discarded the metal spacer that went inside the middle of hub. I then brainstormed on how I could install the new Lip Seal upgrade and then it dawned on me that since the inner Hub that holds the seal was so far gone and only enough left to barely hold the new seal in I remembered the ole saying Don't Discard just use JB Stick or JB Quick I used JB Stick to fill in around the new seal because it is supposed to bond to metal and it did just that I pressed the putty in quickly before it hardened bringing it out even with the plastic drum where the origional hub should have been and made the repair to the deteriorated Hub so that the Seal would stay in place it Worked! This Maytag Neptune was given to me by my mother in-law she did not want to wait on the repair after I tried to previously repair the problem with it I just did not delv deeply enough into the problem with this washingmachine at first. I previously removed both Pumps thinking they were not pumping all the water out because the Towels especially were staying soaked. Both the pumps were nasty with alot of debree inside of them now I know that because of the deteriorated Seal Hub on the inside had done the dirty work. The Pumps can be easily taken apart only a few screws and the plastic impeller can be gently pried off also that is where I found alot of particles from the deteoriated Seal Hub I then reinstalled the pumps and they worked fine pumped out the water. Then that is when I noticed it wasn't cycling properly also Ha Ha I thought to myself what else could possibly be wrong with this washing machine? Thanks to Parts Select site I wa
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- Customer:
- SALLY from ANAHEIM, CA
- Parts Used:
- WP33001762
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Dryer wouldn't start
We tried replacing the door switch first, still didn't start. Next we tried the thermal fuse and it turned on and has worked ever since.
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- Customer:
- William from Colver, PA
- Parts Used:
- 12002039
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Wrench set
LR Code on the display, washer would not spin.
Removed the front panel and took out the old control board, which had a burnt spot on it. Removed back panel and took out the old motor. Put in the new motor and then the new control panel. Runs perfect.
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- Customer:
- Bick from Alameda, CA
- Parts Used:
- 12002039
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers, Wrench set
the problem is the motor
first i follow the instruction come with parts in box...and replace easy this the best place to buy parts for all home appliance...thanks
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- Customer:
- Shawn from Dover, NH
- Parts Used:
- 306436
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
broken clip for door latch
popped out old female clasp on dryer itself with screwdriver, undid 2 screws on dryer door and door handle with phillips screwdriver, popped in new male clasp part, put door knob back on and put the two screws back in door and it was all set to go. Less than 15 minutes to do. Better than new and wife is happy. No more duct tape holding door closed now.
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- Customer:
- john from richland, MI
- Parts Used:
- 12002022
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers, Socket set, Wrench set
Front bearings totally destroyed rear bearings rusted out
I found your site where other people worked on their washers . I removed the front & rear panels. at the front I found that removing the rubber tub seal was easy, then I removed the 3 agitaters that cover the nuts that hold the tub to the support drive shaft ,I saved the plastic shims nuts & washers then removed the tub,I removed the drive wheel, I put the bolt & washers back in the shaft end & knocked it out with a 1lb hammer.I removed the motor and all the hoses also the front & rear WeightsI left the switches connected to the wires, for everything I removed including screws I taped them all to the parts that they camefrom .Then I knocked out the rear bearing with a 8" long 1/2'dia.piece of steel rod taking care to drive evenly around the circomference of the bearing. the front bearing was in 2 pieces with the bearings in a pile inside the hub because of the spacer between the bearings there was not a lot of bearing to hit but eventually it came out I saved the spacer & the rear bearing clip & cleaned them up for reuse.The face of the crap metal insert was badly corroded ,I cleaned it and all surfaces inside the hub with a wire brush in my drillmotor I found bearings at an industrial store and found NO problem matching the old bearings I ordered the lipseal kit from Part select It came with 2 seals & dubious instrutions I found the revised seal did not fit my support shaft but the other one did ,it comes in 2 parts that are stuck together with grease pry them apart with e small screw driver. I then tapped the new bearings in rear first then the spacer. then the front bearing I tapped it in enough to get it started then I inserted a cardboard toilet roll center folded enough to go in through the spacer & the rear bearing this lined up the parts so the shaft will go throughafter the bearings & new seal were in I used a marine silicon to put over the corroded face & made shure that it snugged up to the seal ,sealing it good I let it set for 24 hrs Then I putthe shaft back onto the tub put the agataters back on, then put the outer shell with the new bearings back in place connected the hoses, the weights, the switches, the wire clips,the motor,hooked up the springs ,inserted the tub, put the drive wheel back on the shaft then the belt , then put all the front panels back and IT ALL WORKED. total cost $36.00 for bearings $53.00 for the seal kit so about $90.00 total & two weeks at about a couple of hours a day .shure beats $650.00 + $300.00 at a repair facility . GOOD LUCK .IAN
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