PDWT400V50BB General Electric Dishwasher - Instructions
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- Customer:
- Brett from Ocala, FL
- Parts Used:
- WD18X10010, WD12X10061
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable)
Water was leaking out of bottom and not filling washer. Mouse at through this piece
Shut off water, disconnect drain line from disposer. Remove dishwasher from wall and remove water feed line. Unplug or disconnect power to unit. Remove upper and lower dish racks as well as lower water sprayer bar, and filters. Lay dishwasher down on backside (make sure to catch water with bowl). Disconnect pump connector with nut driver and replace. Stand dishwasher back up and reverse removal process
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- Customer:
- MICHELLE from CHESTERFIELD, NJ
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
The Wheel Was Stuck And It Was Hard To Rolled It
I just ordered another one of the wheel rack and it was that easy. No tool required.
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- Customer:
- Mary from Dana Point, CA
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
The rack assembly needed replacing
Just removed the prior rack and put the new one in. Much improved design on the wheels and rack seems of better material as well. The rack does not have as many holders as the prior rack dishes and pans do not fit as well.
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- Customer:
- Charles from Walnut Creek, CA
- Parts Used:
- WD12X10163
- Difficulty Level:
- Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers
Installation video
removed front panel and replaced new part. Timer did not work because plug kept disconnecting. Called GE service and watched him remove panel without removing control panel. Plug for timer can be installed easily and front panel replaced without disturbing cable.
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- Customer:
- Jonathan from Keller, TX
- Parts Used:
- WD12X10163
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers
Soap dispenser did not open
Replaced wax motor and soap dispenser (all one piece). Only problem was the plastic seal on the very bottom of door had come unseated, and therefore was leaking. You need to check that it is snapped all the way in, and then the leak ceased. Took me a few tries, which made a ten minute repair into an hour long one.
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- Customer:
- William from Sterling, VA
- Parts Used:
- WD15X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable)
Serious water leak into basement from around a kitchen sink pipe.
Removing two screws holding the bottom trim/sound baffle opened a view of water dripping from the water intake valve at the left front of my Monogram dishwasher. I then turned off the local (under my adjacent sink) separate feed valve for the washer, then opened the (dedicated) breaker for the machine at my breaker panel.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
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- Customer:
- William from Bradenton, AL
- Parts Used:
- WD19X10039
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
Dishwasher would not drain
First broke the tab on trying to get the sprayer arm out - had to buy replacement part. The tab to release the sprayer arm is on the BACK and can't be seen. FYI, pull the tab gently out from the back to release the sprayer arm. Problem wasn't a clogged drain. Next figured it had to be clogged in the Impeller and Seal assembly. Replaced that and realized the motor wouldn't turn. As an electronic engineer, determined the starting capacitor was defective. Found Mr. Nice GET (who owns Hotpoint) would not sell the capacitor, only the entire motor assembly for about $125.00 more or less. Found a capacitor at local motor shop with the correct value and hung it under the dishwasher. (wasn't the right package size to replace where the old one was). All is well - Finally.
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- Customer:
- Craig from Massapequa Park, NY
- Parts Used:
- WD18X10026, WD18X10010
- Difficulty Level:
- Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Screw drivers, Socket set, Wrench (Adjustable), Wrench set
Water leaking from below
After determining that the leak was coming from the sump connector, I had to completely remove the unit from the counter. After removing all the parts in the wash cabinet (wash arms,conduit,fine,course and sump filters),the sump connector nut was revealed which I loosened, but did not remove, with a channel lock plier. The unit was then placed up-side down where I then loosened all the worm clamps that attached the drain motor,pump,and turbidity sensor to the sump and sump connector.then I removed the brackets that braced the pump to the washer body and removed the pump.at this point,you should be able to remove the drain motor and turbidity sensor from the sump and remove the sump from the washer. You should also be able to remove the connector as well.Both these items are made of some type of rubber which seems to deteriorate from the soap which was caked all over them in my case. Just reverse the above process to re-install everthing. I didn't find this job terribly difficult and it was certainly better than spending hundreds replacing the unit.
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- Customer:
- Ryan from Blaine, WA
- Parts Used:
- WD18X10026
- Difficulty Level:
- Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
Standing water in bottom of washer at end of cycle.
Found numerous references on internet that most likely cause was due to a fouled or plugged suction screen. I unscrewed anchor tabs on top securing the dishwasher to the countertop, slightly lowered the front screw legs, turned off circuit breaker at the electrical panel, checked to verify the power was off, removed the small electrical cover under the dishwasher and disconnected the 3 wire nuts, pulled the dishwasher partially out, then disconnected the small corrugated drain hose from the discharge pump under the washer being careful to collect small amount of drain water in a bowl. Finally, carefully pulled dishwasher out from under the countertop leaving the hot water supply hose connected. Tipped washer over onto back (the frame rails are rounded in the back to help facilitate this). Had to unscrew the hose clamps to remove the rubber sump. Then stood the dishwasher back up to disassemble the plastic screen parts from inside the dishwasher. The screen was in fact plugged with white slimy deposits that when dried became chalk like. During cleaning out the white caked on deposits in the rubber sump, I accidentally pushed my screwdriver through a rubber vent stand tube and this is why I had to buy a new rubber sump. The sump rubber material appeared to be partially deteriorated which is why my screwdriver passed through it. Reassembly wasn't very easy. It was difficult to get the rubber sump boot over the plastic flange on the bottom of the tub. It helped to remove the metal hose clamp completely and to have someone hold the dishwasher in place lying on its back while I pushed and prodded to get the rubber seal over the oval flange. Once on, everything went back together easily in reverse order. It probably took me a total of 6 to 8 hours of real working time. But taking into account that I only worked for short periods of time on evenings after work and the fact I had to lug around my extra 70 lbs of gut, the constant laying down and getting back up, the 4 day wait for the new rubber sump to arrive, and my near senior citizen age stretched this 8 hours of work out to a two week home repair project. BUT, I was successful and everything is back to perfect working order. Thank you Partselect.com for having the sump in stock and to my door in only 4 days!
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- Customer:
- Karl from Maple Grove, MN
- Parts Used:
- WD26X10056
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
Loud Blower - Replaced Blower Fan Unit
I began to notice a loud grinding sound when my dishwasher blower motor kicked in (mostly at the end of the entire washing cycle). It was obvious where the noise was coming from (upper left side of door). Ordered blower motor / fan and replaced it. Problem solved! When taking the front panel off, be very aware of all screws. There is a screw on the right side of the door that screws inward. It holds the control unit. If not removed, the control unit screw hole will break off and it will be difficult for you to secure the control unit. Be aware that there are two small screws that point UP below the front panel. Be sure to remove those too. Take pictures of the wires before disconnecting from the control unit. It's fairly obvious, but cheap insurance if needed when reassembling. The fan motor in the upper left of the panel. There are a large gray venting unit above it. You will need to remove that unit in order to expose the screws to remove the fan motor. Once removed, replace the fan motor and work backwards to connect everything again. Possibly take a few moments to clean the inside of your door panel to remove any hard water build up from any moisture that leaked into your door panel. Hope this helps.
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- Customer:
- Pierangela from River Forest, IL
- Parts Used:
- WD12X10163
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
the soap dispenser door had broken off
Open the door and go along entire edge of door and use Philipps to unscrew the front panel of the door from the inside panel of the door. Once unscrewed open carefully. There are screws in the dispenser cup. Undo those and then there are two plugs to be undone. There is also the main black computer component that has to be unplugged from its cord. Just remove and screw everything back the way it was. This was my first time and I am a female age 58 years old. It was simple. If I had to do it again I could do it in less than half the time.
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- Customer:
- Edward from Granite Bay, CA
- Parts Used:
- WD08X10032
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
tear in the tub gasket
Pulled out the old gasket and replaced with the new gasket. Inserted the steel spring clip into the ends of the gasket. Repair complete.
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- Customer:
- Gary from Willoughby, OH
- Parts Used:
- WD26X10056
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
water leak left side of door bottom intermittent
Remove door cover shell by removing screws in inside of door. Unplug harness to control module.Remove outer door shell.Remove four screws at the blower motor. Replace with new motor after disconnecting harness to motor. Reinstall module harness reinstall door shell.
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- Customer:
- joseph from pittsburgh, PA
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
bottom rack was rusting away
opened the dishwasher .............removed the old and slid in the new ...then attached by dropping in the utensil compartment.....piece of cake
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- Customer:
- Peter from Davenport, FL
- Parts Used:
- WD14X10009
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Hing arm broke
Removed dish washer from cabinet area and snapped new clip into cable and hook into support.. The time that took the longest was to removed the screws to pull the unit out of the cabinet area.. Very easy fix...
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