MAT10DAABL Maytag Washer - Instructions
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- Customer:
- Jacob from SMITHFIELD, KY
- Parts Used:
- WP22001619
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers
Washer was overfilling from water level selected
Tried the water level control first. didn't fix it.
Then replaced the air tube for tub fill volume.
The thing here is that it didn't have a hole in it nor was it blocked where you couldn't blow through it.
The prolbem was that at the tub end it has a larger diameter and that was nearly filled with softener residue so it changed the air volume.
That reduced air volume caused the air pressure to be wrong to the water level sensor.
My most useful tool was a magnet mount flashligt inside the cabinet so I could see to get the hose back on.
Then replaced the air tube for tub fill volume.
The thing here is that it didn't have a hole in it nor was it blocked where you couldn't blow through it.
The prolbem was that at the tub end it has a larger diameter and that was nearly filled with softener residue so it changed the air volume.
That reduced air volume caused the air pressure to be wrong to the water level sensor.
My most useful tool was a magnet mount flashligt inside the cabinet so I could see to get the hose back on.
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- Customer:
- JACLYN from RICE LAKE, WI
- Parts Used:
- 6-2095720
- Difficulty Level:
- Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers, Socket set, Wrench set
Washer Leaked Water From Bottom Seal
Removed washer tubs inner and outer nut (part # 10 ) on inner was hard to remove and is a reverse thread used hammer to loosen once off removed 1st tub - then removed set screw #17 and then unscrewed mounting s item #29 this again required some hammer tapping to loosen - once off used flat head screwdriver to pry & remove the rubber piece on bottom of outer or 2nd tub -but keep going as the leak will probably be from part #20 tub bearing ( this will save you the time to test and find out it still leaks and have to take apart again after only replacing #29 removed 3 bolts holding tub - disconnected hoses and removed 2nd tub - used rubber hammer to knock out and install #20 tub bearing - reasembled and wow no leaks to cost about $120 - time worked on 3 hrs - only because took apart 2 times - down time on washer 10 days as we didn't order all parts to start with no beer needed but did enjoy a nice red wine - good luck
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- Customer:
- Sandra L from Warren, OH
- Parts Used:
- WP211726
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
Washing machine lid hinge balls fell off machine lid
First I had to hold the balls into the little holes on the side of the lid - one at a time- and tap the plastic ball into the side with a small hammer. I did the same with the other side. Silde the lid to match the holes located on the washing machine - give a little push to make sure that the balls are in place. You have your lid fixed to your machine where you can lift the lid and it will stay up without falling.
Note: If the balls fall out - make sure to tap a little harder so that the balls stay in place.
Note: If the balls fall out - make sure to tap a little harder so that the balls stay in place.
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- Customer:
- Henry from Southside, AL
- Parts Used:
- WP22001187, WP22001186
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
Upper and lower filler injectors broken
Power cord out, of course.Popped off the front panel, swinging bottom outward. Wedge shaped protrusions on top of front panel work as a hinge until the bottom is swung out and the entire front lowered. Unscrewed the top--one screw in each front corner accessed from the front opening (removed panel). Panel behind control panel must be removed (5 hex head screws). Tilted front of top up revealing broken injector. Retaining screw for injector accessible from behind control panel loosened and broken injector assembly removed. New (easily assembled--snap together) injector slid into holding slot on one side and screwed down with previously removed hex screw. Reassemble in reverse.
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- Customer:
- Don from Crescent City, CA
- Parts Used:
- WP22001083
- Difficulty Level:
- Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver
The washer would only go on the delicate cycle no matter what cycle it was set on.
This is a coin-op washer so the timer had to be removed through the coin box. The top lid was first removed from the coin box. There is one 5/16 hex head screw holding the timer in. After removing the screw the timer was lifted from the box. It is a tight fit that requires some wiggling around of the timer. There are two plug in wire harnesses attached to the timer. Because of the position of the timer the wires are a little short, but are able to be unplugged. The new timer was installed and the procedure reversed.
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Very old washer was leaking oil and grease drops into the wash water.
Followed the procedures recommended for replacement of all the parts included in the Tub Bearing Kit and the Mounting Stem/Tub Seal kit as illustrated in a detailed, 32 minute repair video for the Maytag A606 washer which is available on YouTube. Many difficulties were experienced in the disassembly procedures due to extensive corrosion of tub bearing and tub stem parts (the washer is 47 years old).
I was not successful in using a special tub wrench that was purchased to break loose the old tub mounting stem and its threaded lock nut. The old tub mounting stem, lock nut, and the tub bearing race had to be cut off the threaded support shaft using a saws-all electric tool. Finally, corrosion on the edge of the tub caused problems with water leaks once the tub top and its rubber tub seal ring were reinstalled and the washer was put back into operation. The bottom line is that it may be questionable to attempt major repairs on washers that are 40+ years old and have any extensive corrosion in internal, mechanical parts.
I was not successful in using a special tub wrench that was purchased to break loose the old tub mounting stem and its threaded lock nut. The old tub mounting stem, lock nut, and the tub bearing race had to be cut off the threaded support shaft using a saws-all electric tool. Finally, corrosion on the edge of the tub caused problems with water leaks once the tub top and its rubber tub seal ring were reinstalled and the washer was put back into operation. The bottom line is that it may be questionable to attempt major repairs on washers that are 40+ years old and have any extensive corrosion in internal, mechanical parts.
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- Customer:
- Howard from ALBRIGHT, WV
- Parts Used:
- WP6-2022030
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver
The old pump was beginning to drag due to the age of the washer.
Removed the front panel. Then blocked up the front of the machine. Removed the pump belt. Removed the 3 5/16" screws from the bottom of the old one and tilted it slightly to remove. Put the new one in and reinstalled the 3 screws. Put the belt back on and slid new pump all the way to the right and tightened 1 screw. Loosened the screw until there was about 1/4" of gap when squeezed the belt together. Tightened the one screw, then the other 2. Put the front panel back on and lowered the machine. New pump works great.
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Broken belt
It was as simple as leaning the machine back far enough so I could get to the belts - which were on the bottom. The diagrams that came with the ordered parts were right on. This is the first time I have attempted this myself - my repairman has retired - I'm sure I will do it again.
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- Customer:
- Gary from Grosse Pointe Woods, MI
- Parts Used:
- 22001299
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
Crack on the side of tub cover
Very Easy Repair! Removed 2 screws at the bottom using a philips screw driver(one on each side). Lifted the cover up to detach. 2 screws at the top were removed using a socket set (one on each side). Old tub cover snapped off easily. Make sure you set the cover the same way as the old cover. The new cover snapped on with minimal force. Make sure it's fully seated. Put everything back together in reverse. Took 20min. Most of the time searching for the tools.
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- Customer:
- curtis from ROCKDALE, TX
- Parts Used:
- WP6-2008160
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
Noise from dryer in spin cycle,
Found noise to be belt slapping the base sheet metal, from being too loose. Belt was loose because the drive pulley was worn and one side of pulley was loose! Used allen wrench to loosen the pulley set screw, and pryed off the old pulley. Replace d with new pulley and new belts. Works and sounds like new!
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- Customer:
- Greg from Manhattan, KS
- Parts Used:
- WP6-2022030
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
Water was leaking from under the front of the washer when it was used.
After turning the water off and unplugging the machine, I took the front panel off the washing machine. I then slipped the belt off the pump sprocket. The pump was right in the front and easy to remove. All I needed was a screwdriver, for the hose clamps, and a 5/16" socket to remove the old pump. I then installed the new pump, with the existing screws, re-attached the 2 hoses, slipped the belt back on, and popped the front panel back into place. The new pump works great and the leak is gone. The whole job onlt took about 30 minutes.
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- Customer:
- Wayne from SEDONA, AZ
- Parts Used:
- 22003428
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Wrench (Adjustable)
Threads on old legs had been damaged in moving to new location.
Removed the damaged legs, replaced with parts from this site and leveled the washer .
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Broken Belts
Lets just say thank god for part select!!!! # 1 By far. This was a one two three job.
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Repairs Were Easy.
Removed top. Removed agitator and tubs . Replaced seals and reassembled.
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- Customer:
- EL from O'Fallon, IL
- Parts Used:
- WP211726
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
Resin balls on which the top loader lid hinges had broken.
Cleaned the cavities. Lubed them with olive oil. Inserted one ball on left side, while holding tension against that side to hold the ball in the lid and top indentations. Applied olive oil to right hand side indentation, and placed the new ball into lid indentation. Put lid down into closure cavity with ball, and with lid vertical, began pushing it rearward so as toslightly spring metal lid rolled edge and top metal away from one another UNTIL the new ball snapped into the hinge indentation in the machine cover. Done.
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