11081375410 Kenmore Washer - Instructions
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- Customer:
- Danny from Woodstock, GA
- Parts Used:
- 285753A
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Motor runs, but tub does not spin or agitate
Woulkd have taken alot less time had I not taken off the control board, back...etc. Laying the unit on its back is perfect. Took it out into the garage when I could have done it in the laundry rooom with very little water loss.
1. Removed all hoses connected to top of motor. This was not very easy since the spring clamps had been in the same place for 20+ years. Also removed all wire harness connected to and from the motor.
2. Removed metal clamps from top of motor unit, and removed the plastic "valve".
3. Removed screws holding in clamps on each side of the motor used to hold motor on motor plate. Removed motor. Trick is to make sure that the back clamp stays in place...makes it a little easier when you go to re install.
4. Cleaned out around agitator shaft, and fitted one side of the coupling and the neoprene type joiner on to the agitator shaft.
5. Fitted other side of coupling on to motor...This is where it got a little tough......and then placed motor unit on the motor plate, making sure to line up teeth to neoprene joiner.
6. Replaced clamps on each side of the motor and screwed in nuts holding them in place.
7. Replaced plastic "valve" and the clamps that hold it in placed...back one is a little tough.
8. Reattached hoses to "valve" and hooked all wire harness back into place.
9.Tested perfect...little burning smell on first spin....but works great now!!
1. Removed all hoses connected to top of motor. This was not very easy since the spring clamps had been in the same place for 20+ years. Also removed all wire harness connected to and from the motor.
2. Removed metal clamps from top of motor unit, and removed the plastic "valve".
3. Removed screws holding in clamps on each side of the motor used to hold motor on motor plate. Removed motor. Trick is to make sure that the back clamp stays in place...makes it a little easier when you go to re install.
4. Cleaned out around agitator shaft, and fitted one side of the coupling and the neoprene type joiner on to the agitator shaft.
5. Fitted other side of coupling on to motor...This is where it got a little tough......and then placed motor unit on the motor plate, making sure to line up teeth to neoprene joiner.
6. Replaced clamps on each side of the motor and screwed in nuts holding them in place.
7. Replaced plastic "valve" and the clamps that hold it in placed...back one is a little tough.
8. Reattached hoses to "valve" and hooked all wire harness back into place.
9.Tested perfect...little burning smell on first spin....but works great now!!
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- Customer:
- Helen from NASHUA, NH
- Parts Used:
- WP89503
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
Leaking water inlet hoses.
Removed the old hoses and screwed on the new hoses.
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- Customer:
- Jim from Waxahachie, TX
- Parts Used:
- WP3357328
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
a mouse got in the washer looking for water and chewed up the hose
I WATCHED YOUR VIDEO AND IT CHANGED OUT VERY GOOD IT WAS NOT AS HARD AS I THOUGHT IT WOULD BE. I HAD TO TAKE IT APART 3 TIMES. HE CHEWEW THE HOSES ON THE PUMP AND THE LITTLE HOSE THAT GOES TO THE WATER FILL CONTROLE. I THINK I AM A WASHER EXPERT.I AM 81 YEARS OLD SO ANYONE CAN DO IT.
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- Customer:
- Connie from BATON ROUGE, LA
- Parts Used:
- 285805
- Difficulty Level:
- Very Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers, Socket set
leaking valves
We watched a video on YouTube; it was very easy . We had to use the mounting bracket.
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- Customer:
- Melody from ENTERPRISE, FL
- Parts Used:
- 285753A
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
washer quit spinning
Followed the video posted on the website. Everything went great - first repair attempt took about 45 minutes. Time consumed mostly due to the straps that hold the motor in place being very difficult to put back on and that the cabinet was a little difficult to replace due to the amount of rust around the bottom of it. Tried out the washer when done, and noticed a burning rubber smell. Took everything apart again, checked it, and everything seemed to be ok (made sure all four rubber feet were in place on the motor) so put it all back together again. Noticed the smell again so took it apart a third time, and when the motor felt pretty warm, decided to do an internet search for "burning rubber smell after replacing drive motor coupling." The answer popped right up - the replacement parts were not solid plastic like the original ones- they had metal on the inside of them, and needed to be tapped, a bit forcefully, with a hammer and socket until flush on the both the motor and transmission axles. Once the parts were flush, the straps that hold the motor in place snapped right on. Still a challenge with the rusted cabinet, but once all together again, worked perfect! Thanks to this site , I have fixed washers, dryers, and refrigerators and used them now nearly 20 years! I showed my daughter and granddaughter how to repair them and they don't hesitate to pitch in and help or handle the repairs on their own - again with much appreciation to this sitefor the accurate "how to" videos, the right parts, fast shipping, and great prices.
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- Customer:
- James from ARVADA, CO
- Parts Used:
- WP62780
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
Leaked, disassembly revealed it was the drive seal washer grommet. Drive block was also rusted out and frozen to the washer drum
Disassembled lower part found nothing wrong.
Started disassembly from the top. Immediately ran into trouble not knowing exactly how the tub was anchored to the drive. Once I got down to the tube and drive block there was nothing I could do to go further. I guessed it was a press fit onto the drive, but there were many instructions and I couldn't be sure. Parts Select expanded drawing was the most useful tool; it was correct omitting a few details. Anyhow, cleaning out my garage I found one of my old gear pullers that I could ring to complete the disassembly. All the sudden I was in business, pulling the washer drum off the drive block and shaft, getting down to the leaky lower seal. A that point it was just a matter of cleaning everything up and buying all the rusted out parts to reassemble. I spent $150-200 on parts, but its completely rebuilt now and runs like a charm. Probably have around 20-50 hours all told, into the repair. Most of this was reading instructions, watching videos, and trying to figure out the rest (3). Doing the actual work spread over time until my wife and sons threatened to throw the thing out. Never. Once I decide I'm gonna do something, I do it. LOL!
Started disassembly from the top. Immediately ran into trouble not knowing exactly how the tub was anchored to the drive. Once I got down to the tube and drive block there was nothing I could do to go further. I guessed it was a press fit onto the drive, but there were many instructions and I couldn't be sure. Parts Select expanded drawing was the most useful tool; it was correct omitting a few details. Anyhow, cleaning out my garage I found one of my old gear pullers that I could ring to complete the disassembly. All the sudden I was in business, pulling the washer drum off the drive block and shaft, getting down to the leaky lower seal. A that point it was just a matter of cleaning everything up and buying all the rusted out parts to reassemble. I spent $150-200 on parts, but its completely rebuilt now and runs like a charm. Probably have around 20-50 hours all told, into the repair. Most of this was reading instructions, watching videos, and trying to figure out the rest (3). Doing the actual work spread over time until my wife and sons threatened to throw the thing out. Never. Once I decide I'm gonna do something, I do it. LOL!
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- Customer:
- Robert from Henrico, VA
- Parts Used:
- 285785
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
Kenmore Series 80 Lazy Spin
Remove metal cover; remove pump, remove motor, remove tub spin assembly; remove transmission. Remove clutch be removing retaining ring. Installation was reverse. No problems, part worked like champ.
Note: Called Sears to see if I could get the part locally. Turns our I had to call an 800 number. Lady said that the part was not carried and would have to be shipped from warehouse. Tried to sell me some discharge hoses. Then said the part would cost $65 before S&H. Told her I didn't want to spend that much, she asked how much I wanted to spend and seemed upset when I told her your price. She didn't comp it, just said that theirs was an official part from Sears, blah, blah, blah. Anyway, thanks for the great service!
Note: Called Sears to see if I could get the part locally. Turns our I had to call an 800 number. Lady said that the part was not carried and would have to be shipped from warehouse. Tried to sell me some discharge hoses. Then said the part would cost $65 before S&H. Told her I didn't want to spend that much, she asked how much I wanted to spend and seemed upset when I told her your price. She didn't comp it, just said that theirs was an official part from Sears, blah, blah, blah. Anyway, thanks for the great service!
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- Customer:
- Albert from ROSELLE, IL
- Parts Used:
- 285744
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers
Machine made loud banging noise and vibration when running and tub ran off center
Disassembled top control console and surrounding sheet metal cabinet per the video from this site. i then used a screw driver to carefully pry up each wear pad location individually and inserted the wood wedge. to about 1 1/2 inch height. rwmoved the old wear pads and popped in the new pads one by one. Closed up the unit and tested the machine . It ran like new. No more noise or viberation
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- Customer:
- david from WEBSTER, NY
- Parts Used:
- 285785
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set, Wrench (Adjustable)
When the washer went to spin, first a grinding sound then THUMP, THUMP, THUMP
The washer agitated ok, so I figured it wasn't the motor or agitator. Watching the repair videos, I assumed the clutch might be the culprit. The videos are very good, so I should have taken the machine apart and actually looked at the clutch - it wasn't too bad. Trying to put the new clutch on anyway, I noticed it didn't turn on level. I thought it wasn't seated correct, but it was then I realized the shaft was tilting. This would explain the THUMP, and the grinding must be a gear inside the transmission. As much as I hate to get a new machine, given the tremendous downturn in quality, I think that because this machine is old, it is not worth a $200 transmission. Anyone need a brand new (but test fitted so not returnable) clutch?
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- Customer:
- David from Kansas City, MO
- Parts Used:
- 285805
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
The water was not switching properly, hot water was barely coming out.
Installed part, now it works great!
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- Customer:
- DEREK from ASHEVILLE, NC
- Parts Used:
- 285753A
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
Broken Coupling
Disconnect power & water then drain hoses.
We flipped the washer on it's side to gain access to the bottom. There was no need to take off the back panel. Keep a 5 gallon bucket and a few rags handy for the extra water in the pump line.
Disconnected the wiring harness. Removed the brackets holding the motor. It's a little tight on the back bracket. It has a 1/4" hex nut on the back side, so I used a 1/4" drive socket (see: small). Removed the bolts holding the gear case (this makes it a lot easier). Disconnected the pump hose and rotated the motor & gear box and pulled forward. This gives you access to the coupling. Remove the broken part. Clean the area for debris. NOTE: each part of the coupling has 3 fingers (these are what breaks off), so check to make sure you get all broken parts. Insert the new coupling. It has 3 parts; the plastic fittings go on tight and need to be snug to the shaft. Use a screwdriver handle on the center and tap down with a small hammer. Spray silicone on the rubber coupler to allow a little better slide.
Reverse the process. Line the gear box and motor up and push back into the tub assembly. We used 2 people to do this. It's easier to have someone stand over it and hold / rotate the gear box while the other one can align the motor & bolt everything back on.
It took us an hour, however, if you were doing a couple you could get it down to 30 min. flat.
Go wash your clothes!
We flipped the washer on it's side to gain access to the bottom. There was no need to take off the back panel. Keep a 5 gallon bucket and a few rags handy for the extra water in the pump line.
Disconnected the wiring harness. Removed the brackets holding the motor. It's a little tight on the back bracket. It has a 1/4" hex nut on the back side, so I used a 1/4" drive socket (see: small). Removed the bolts holding the gear case (this makes it a lot easier). Disconnected the pump hose and rotated the motor & gear box and pulled forward. This gives you access to the coupling. Remove the broken part. Clean the area for debris. NOTE: each part of the coupling has 3 fingers (these are what breaks off), so check to make sure you get all broken parts. Insert the new coupling. It has 3 parts; the plastic fittings go on tight and need to be snug to the shaft. Use a screwdriver handle on the center and tap down with a small hammer. Spray silicone on the rubber coupler to allow a little better slide.
Reverse the process. Line the gear box and motor up and push back into the tub assembly. We used 2 people to do this. It's easier to have someone stand over it and hold / rotate the gear box while the other one can align the motor & bolt everything back on.
It took us an hour, however, if you were doing a couple you could get it down to 30 min. flat.
Go wash your clothes!
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- Customer:
- David from Danville, VA
- Parts Used:
- 350733
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
no spincycle
pried out old actuater with screwdriver and pushed in new one
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- Customer:
- Linda Dianne from Poteau, OK
- Parts Used:
- WP358237
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Socket set
could not get the bottom agitator to release, so finally just left it in place, first bolt I had did not fit right so ordered one directly from your store also had to wait dor my tools to get in
I am an old woman who is disabled and without any tools or knowledge, but sheer stubbornness and will power, I waited for my tools and other parts to come in, in the mean time I fixed my young neighbors whirlpool washer, well We took top off the nut I had already pre assembled her cam so set it in place of old one put bolt back in place and the top of agitator she says works perfectly now, my parts came in I had nothing to remove as my handicap daughter had already thrown away all the loose parts, I threw away old top agitator, assembled cam and put in place still did not feel tight enough so added seal from other nut!! it worked tight enough, put the inner part back in with new part and soap put the top back on and now works good as new, was disappointed could not put bottom agitator in place, just not strong enough lol well this was my story
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- Customer:
- Lee from HOLLY SPRINGS, MS
- Parts Used:
- WPW10358149
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers
The drain hose had a leak
Watch the video
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- Customer:
- Joseph from North Charleston, SC
- Parts Used:
- 285785
- Difficulty Level:
- Very Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Socket set
Spin cycle worked very poorly
1. Removed back panel.
2. Removed Entire control paned, control and switch units disconnecting wiring assembly from motor.
3 Tilted front and side panel assembly away from frame, tub assembly and motor transmission assembly.
4.Removed cap from top of agitator, removed bolt holding agitator. Removed agitator, this part was tricky since some corrosion on shaft made agitator very difficult to pull off.
4. From bottom of unit disconnected motor/transmission unit from wash tub.
5. Located clutch assembly and removed lock washers. Removed clutch and replaced with new one.
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Steps 1 thru 3 were unnecessary.
All that needed to be done was to removed the agitator assembly. then turn unit on it's side or back and removed motor and transmission from the bottom.
2. Removed Entire control paned, control and switch units disconnecting wiring assembly from motor.
3 Tilted front and side panel assembly away from frame, tub assembly and motor transmission assembly.
4.Removed cap from top of agitator, removed bolt holding agitator. Removed agitator, this part was tricky since some corrosion on shaft made agitator very difficult to pull off.
4. From bottom of unit disconnected motor/transmission unit from wash tub.
5. Located clutch assembly and removed lock washers. Removed clutch and replaced with new one.
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Steps 1 thru 3 were unnecessary.
All that needed to be done was to removed the agitator assembly. then turn unit on it's side or back and removed motor and transmission from the bottom.
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