LTG6234AN2 Whirlpool Washer Dryer Combo - Instructions
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- Customer:
- Charles from Rose Bud, AR
- Parts Used:
- WP63907
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers
tub off center, rubbing on outer tub in spin
turned the washer on it's back and shoved the tub to the side to release pressure on a spring ,pulled it loose and installed new one. this worked for the back two then turned washer on it;s face and repeted the process on the front spring.
Washer works great now.
Washer works great now.
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- Customer:
- Chris from Laguna Niguel, CA
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Would not heat sometimes
Pulled the big front panel by removing two screws near bottom of front and pulling out at bottom until the top pops loose. Vacuumed out all of the dust and checked for loose connections. Ran dryer - igniter would light, but no gas. Checked the two solenoids with a VOM. the one with the two leads would intermittently read Infinity (open). Super simple repair. Remove two screws on solenoid bracket on top of the gas valve, Replace solenoid and plug it back in with the easy push-on connector. NO PROBLEM - all fixed.
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- Customer:
- Russell from Santa Maria, CA
- Parts Used:
- 279311
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable)
No Heat, no ignition in burner
Our dryer would not heat and it seemed that no gas was coming from the regulator. The igniter was working fine but the burner never turned on. To check the problem, i followed the instructions to remove all body panels until I had access to the burner assembly. I dismantled both gas valve coils and tested each one for open or closed circuit using my multi-tester. I found that the three terminal gas valve coil was an open circuit and was not functioning so I ordered a new one from PartSelect and within just a couple days, had the drier back up and functioning. I also replaced the igniter due to a malfunctioning igniter that has been changed by the manufacture. I must say that PartSelect has the fastest shipping I have ever seen. One part I ordered was at my door in less than 24 hours and I only paid standard shipping...un real! OUTSTANDING....5 STAR SERVICE
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- Customer:
- Keith from Richmond, VA
- Parts Used:
- 279640
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Socket set
Idler Pulley broke
I disconnect the power, then the vent pipe. I removed the back panel of the dryer to access the pulley and removed the belt. Replaced the back and put everything back together.
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- Customer:
- Thomas from Commack, NY
- Parts Used:
- 285753A
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers, Socket set, Wrench set
Although the motor was running, washer wouldn't agitate or spin.
After disconnecting the electrical supply, first remove the two screws at either end of the control panel and fold it back away from the washer top. Then, unplug the electrical lid switch connection. Now, remove the two clips at either end on top to disconnect the housing from the washer back and chassis. The motor is sandwiched between the water pump in the front and transmission at the rear. The Direct Drive Coupling connects the rear motor shaft to the transmisson. After you have taken the outter portion of the washer off, remove the two snap clips that hold the water pump in place and slide the pump off the front shaft. Best to also disconnect the upper hose connection so the pump can be moved out of the way. Caution though, remaining water in tub will drain out. Now remove the two screws that hold the clips in place which secure the motor to the transmission. Careful, as the old Direct Drive Coupling is probably destroyed, the clips are the only thing holding the motor in place and the motor needs to be supported so it won't drop to floor when the clips are removed. Be careful not to lose the four rubber grommets which sit between the motor and transmission bracket. After motor is on floor remove the old plastic slip-on direct drive coupling discs from both the motor and transmission shafts. The new replacement discs have steel centers which do not slide onto the shafts as easily as the old plastic ones did. I had to tap the center steel portion onto the shafts using a hammer and a deep wall socket the same width as the steel portion of the disc. Be careful! I'm sure that tapping the plastic portion of the disc to properly seat it on the shaft will break it away from the steel portion. In my case, It took me several attempts to completely seat the new discs. I had to do quite a bit of tapping to get the discs seated far enough onto the shafts so that the motor slipped easily against the transmission bracket grommets and the retainer clips snapped back into place easily. Reassembly is simply reversing the steps you took when taking the unit apart. Before putting the outter housing back in place, I checked to make sure everything was running smoothly by jumping out the electrical snap-in connection for the lid switch and running the machine in the spin cycle. Remember, if you don't jump out the lid switch and just try to test the unit in the aggitate cycle, the machine has to first fill with water.
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Replaced two parts in the gas heater assembly
I removed the front panel of the dryer by removing the 2 screw that secure it at the bottom and pulling upward to disconnect the cover at the top. I then removed the two screws that hold the metal cover that secures the 2 elements in place. I disconnected the wire plugs from the 2 elements, removed the 2 elements and replaced them with the new parts making sure to place them in the same positions as before. I then replaced the housing cover and tightened the screws. Then I replaced the front cover of the dryer.
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- Customer:
- Tracie from Culver City, CA
- Parts Used:
- 279311
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 15 - 30 mins
dryer worked but no heat
Initially we thought the problem was the igniter, so we ordered an igniter kit. Installed it but was unsuccessful. We then went on the websight and read further, about 50% of dryers with no heat but working had a problem with the thermal fuse.So we ordered the thermal fuse installed it, which was very easy, and success. Once the problem was diagnosed properly it was fast and easy. Recommend looking at the statistics for specific problem.
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- Customer:
- Lynn from Novi, MI
- Parts Used:
- WP338906
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver
Heat Would Not Come On
After replacing all the other fuses and sensors I finally replaced the Radiant Flame Sensor and it is working perfectly.
After replacing the other parts and the heat still not coming on I read somewhere that the Radiant Flame Sensor is a normal closed circuit and when I checked with a meter it was open. I would have saved a lot of time and money if I had read that earlier.
After replacing the other parts and the heat still not coming on I read somewhere that the Radiant Flame Sensor is a normal closed circuit and when I checked with a meter it was open. I would have saved a lot of time and money if I had read that earlier.
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Dryer drum was not turning when started.
I moved the dryer to a location where I could get to both the front and back sides. I opened the back by first removing the top cover and then the back. It requires either a Phillips head screwdriver or a quarter inch socket. In addition, it requires removing the four power wires which connect to the computer. If you are unfamiliar with the wiring layout, take a photo with your cell phone which you can then refer to when re-assembling. Once the back was removed, I saw that the belt was still intact, but the pulley which provides tension to the belt was frozen. Take a photo of the belt route between the motor and the pulley. Try to get the spring position in the photo. Remove the belt from the pulley by reducing the tension and then sliding the belt out (this assumes the belt is not broken). The pulley arm is held in place by a single bolt which can be removed by a socket set. Remove the arm with the pulley attached. Examine the pulley to figure out why it is frozen. In my case, the pulley had been frozen for some time and the belt had actually chewed through the pulley and was sliding (polishing) on the pulley axle? I used a pair of pliers to loosen the destroyed pulley by rotating it back and forth over the axle while gripping the arm the axle is attached to. As it loosened up I worked it off the axle. I used a cloth to clean the axle of grime from the belt, pulley, and dryer lint. The new pulley comes with a washer and triangular plastic "fastener". First you put on the washer, then the pulley and then you secure it on the axle by sliding the triangular fastener over the axle so it sits in a small grove near the end of the axle. Then put the pulley arm back by replacing the bolt. Make sure you do not overtighten the arm since it is intended to rotate about the bolt. If the dryer belt breaks, the spring will pull the arm down and throw a cutoff switch. Its operation should be obvious. Once the arm is back in place, refer to your photo and replace the spring (this can be tricky and frustrating, particularly if you don't use something like needle nose pliers). Once the spring is in place, depress it and re-install the dryer belt. Refer to the photo you took earlier if you've forgotten how the belt was routed. Then re-install the dryer's back panel, re-attach the electric wires (again refer to the photo you took earlier), and re-attach the top cover. You might want to test your handiwork at this point before you reconnect the dryer vent
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- Customer:
- Jerry Duty from Fort Walton Beach, FL
- Parts Used:
- 279640
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
idler pully sqwieling
once the back is off remove belt from tentioner and remove v clip. smooth shaft with wd-40 and scotch brite , then install new idler replace v clip
and your done !!!
and your done !!!
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- Customer:
- Charmaine from Slidell, LA
- Parts Used:
- 80040
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Socket set
Agitator was barely agitating. Making a clicking noise.
Removed agitator cap. Removed bolt inside with socket wrench. Located plastic cogs Pulled out old cogs and slid in new cogs and put back together and works great. Easy to take apart and put back together. Very cheap repair. Cogs less that $4.00 plus shipping. Shipped next working day.
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- Customer:
- Donald from Fredericksburg, VA
- Parts Used:
- 80040
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Socket set
Top Half of Agitator would not function without appying sideways pressure
Heard about the website... 1 minute to find it, 10 minutes to order new cogs... 3 day wait for new parts... Rec'd Fedex, 15 minutes total to pull the agitator cover (bleach dispenser) then the bung cover with o-ring (just lift out) expose bolt, unskrew and remove top portion of agitator or entire agitator if it's easier. Seperate, remove black cog holder (slides up the spindle) and replace cogs one at a time just like the old ones. Reassemble in reverse and you are back in business. Saved the $75 deductible on my home appliance warrenty. You guys are the best... cheers...
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- Customer:
- floyd from Slidell, LA
- Parts Used:
- 285785
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
Would not spin
Remove the nut from the top of the motor shift inside of wsher. then remove the wire harness plug. Take out three bolts side the shaft and motor out. Replace clutch and install in reverse order.
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- Customer:
- Dennis from Oak Island, NC
- Parts Used:
- 285805
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
The movers broke both water intakes off flush with the back of the machine
took off two screws that held the top part on took the screws that held the back on 4 screws removed the one screw that held the replacement valve put the black mounting plate on the machine replaced screws very simple.
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Cold water flow was slow
Removed old part; exchanged rubber plungers between the hot and cold. Symptoms still the same - so eliminated the need for new rubber plungers (even though they still needed to be replaced). The only item left were the magnetic switches opening and closing the flows. The syphon was replaced due to broken plastic mountings causing the syphon to hang into the drum. Repair was a snap and finding the parts on your site was very easy and parts were there within 2 days at standard shipping. Thank you.
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