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LTE6234DQ2 Whirlpool Washer Dryer Combo - Instructions

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All Instructions for the LTE6234DQ2
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Customer:
Lori from Parchment, MI
Parts Used:
WPW10250667
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Pliers
sounded out of balance even after shifting clothes
The tub was out of alignment and water fell behind it and onto the floor. My brother-in-law suggested my problem could be the tub balancing spring and when I moved my washing machine, there it was on the ground.
The schematic does not show where it hooks up. So after I did what I thought looked right, the machine still did not work properly. Then I replaced the three suspension springs and that didn't solve the problem.
I found a whirlpool "do-it-yourself" repair book at the library and was prepared to tear into the machine. However, I did not have the tub balancing spring in the correct spot at one end. It hooks up from one of the outer bracket to the back of the housing unit along between the legs. There is a hole that had rusted through. I simply drilled a new hole nearby and low and behold it works!
Easy fix - the frustration was with the poor schematic.
35 of 37 people found this instruction helpful.
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Customer:
Craig from Yadkinville, NC
Parts Used:
80040
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Socket set
Upper agitator stopped moving
First, I removed the softner cup from the top of the agitator. Second, I removed the plastic seal by pulling it out. I then used a socket to remove the bolt holding the agitator down. I then removed the agitiator from the machine and seperated the upper and lower agitator by placing my feet on the lower agitator and pulling up. The dog-ears were in the upper agitaotr section and easy to see and replace. I re-assembled in reverse order. The whole process took less than 30 minutes.
38 of 46 people found this instruction helpful.
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Customer:
Wiliam from Belleville, MI
Parts Used:
WP3387134
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver
Dryer would not shut off on auto dry settings
I removed the discharge duct from the back of the dryer. Then, I removed the screws on the back of the dryer and the back itself. This exposed the cycling thermostat. I removed the screw holding the thermostat. I took the wires off the defective thermostat and reinstalled them on the new thermostat. Then, I reassembled in reverse order.
36 of 41 people found this instruction helpful.
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Customer:
Michelle from Richardson, TX
Parts Used:
72017
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Scratches in Surface
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.
64 of 125 people found this instruction helpful.
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Customer:
Debra from Milton - Freewater, OR
Parts Used:
W10814296
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Pliers, Screw drivers, Socket set
leaking from tub
First I turned off the water and unplugged the washer from the outlet. I took the two screws off the console and turned it up to undo the clips that hold the cabinet to the back. I took out the 2 phillips screws at the top corners of the back. I was then able to pull cabinet off and not have to remove the console, but carefully slid it to the side, as ther wires were still attached.
Pried off agitator cap & reached into agitator to pry out another cap to access 7/16 bolt. Checked over the agitator parts for wear (dogs) Took agitator, top outer (white) and inner (brown) tub rings off.
Sprayed lots of liqid wrench around spanner nut and drive block and gave it time to work. Used spanner tool to get spanner nut off. Hard work. Pounded and pounded and pounded and pounded with hammer. It gave a tiny bit. Then I got an idea: I pounded it back the other way, as you would to tighten. This helped. I then pounded back the other way and did this again. It worked amazingly well.
Got to drive block and it was rusted out along the bottom and also hard to get off. The diagram showed a "lock" (horseshoe shaped thing) on top of it, but mine was all in one piece but I couldn't tell that. I sprayed and pryed and pounded from the bottom and it split in half. It needed to be replaced anyway.
The inner tub was also hard to get out and I used some dish liquid. I pushed down, (using the rags here, the edges can cut you). I twisted, I pulled. I pushed, I pulled, I cussed, and begged. I then went to bed and then next day I pushed backwards and forwards and side to side & finally it came off. Then I undid the brackets on the bottom of the outer tub along the bottom and disconnected the clear hose in back. When loosening the black hose clamp in front to the pump, water started to come out of the hose so I grabbed a cool whip container to catch it. It smelled yucky. Once I had the outer tub off I put the new seal in, using some plumber's grease to help get ithe tub over the shaft..Then I hooked up the hoses & brackets on the bottom of the outer tub. I cleaned out the outer tub, as there was crud in the bottom. Then I poured about 5 gallons of water in it to see if the seal was set in right. Make sure the drain hose hasn't fallen out! (You can leave this water in the tub, you'll find out why) I cleaned up the rust on tube of the inner tub with steel wool and inspected everything else. Something didn't look quite right about the outer shaft that goes around the spin tube. It looked like something should go there. I discovered there SHOULD have been a seal there but one was never put in. So I put one in. I used a little grease to help put the new drive block on, and tightened the spanner nut with the spanner wrench. I put everything else back on EXCEPT for the cabinet-with the console attached. Ha Ha All the other directions I read wrote to take the console off first. If I had done that I wouldn't have been able to do the most important part of the job: testing the result. I finished filling the tub to the lowest water level to watch it go thru it's cycles and checked for leaks. If the console was "flopped over" the back how can you check? (I don't play with wiring)
I turned off the water & unplugged the washer and slid the cabinet on.. I tipped the console back to access the large gold squiggly brackets that hold the cabinet to the back and reattached them to the back, by removing them, hooking them onto the back, and snapping them into place. I double-DOUBLE checked to see if anything had come loose, then slid the console first on top of the back and put the two screws back in. The screws on my machine are not covered up by the end caps, but they are at a wierd angle, so I held the console up slighly and started the screws first. As they tightened down the console slid into the holes on the cabinet.
There is a small sppliance shop in my town & the guy loaned me the spanner wrench. It was very nice of him.I guess I will have to give his & his famil
37 of 45 people found this instruction helpful.
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Customer:
David from Washington Crossing, PA
Parts Used:
WP3363892
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Pliers
Leaking water pump where casing halves split.
Replaced pump without disassembling the cabinet or disconnecting motor or any other parts.

Disconnected power, drain, hot and cold water lines. drained lines to pail before taping to top of unit.

Tipped the unit to a 45 Deg. angle, leaning the top side edge onto a stool so that pump presented well at the raised bottom edge.

Removed hose clamps at pump suction and discharge ports and drained water into a shallow soaking pan. Kept clamps on hoses to facilitate reinstallation of pump.

Removed spring clamps at front and rear of pump housing.

Wiggled motor shaft away from coupling in pump. This is a friction fit, so no parts removal was required and no parts "come loose" in the process.

Wiggled new pump housing onto the motor shaft after checking square shaft alignment with respect to square female coupling on pump.

Pushed and twisted hose ends onto pump suction and discharge ports, then pulled spring clamps down over hose ends at pump ports.

Reset spring clamps so that they were aligned and square with pump ports. Reconnected power, drain, hot and cold water line connections.

Washer ran as before but without leaks this time.
34 of 36 people found this instruction helpful.
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Customer:
Jonathan from Arlington, VA
Parts Used:
285805
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Pliers, Screw drivers, Socket set
Washer filled v e r y slowly
I'd noticed for a while that our 15-year-old Kenmore washer was filling slowly, but when it started to take 30 minutes to fill to the "medium" level, I knew something was really wrong. There was plenty of water pressure, so I replaced a hose that was loaded with minerals and cleaned the filter (also clogged with minerals). But that didn't help! So I ordered a new water inlet valve, and replaced that. There's nothing tricky about the repair -- the hardest part is opening and closing the washer, for which I found instructions online. (Even so, it's the most time-consuming part of the project.) The result is the washer now fills as fast as when it was new. Just for fun, I took apart the old valve and expected to find it encrusted with minerals, but it looked fine, so I'm not sure where the actual breakdown was. But since the part only cost $25 -- less than a service call, for sure -- I was very happy to use a half hour of my time and keep the machine going a while longer.
33 of 36 people found this instruction helpful.
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Customer:
Tom from Grove, OK
Parts Used:
WP3390291
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers
dryer works but no heat.
Measured resistance on thermostats & heating element. Found thermostat open so ordered replacement part and heat again.
35 of 42 people found this instruction helpful.
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Customer:
John from Tucson, AZ
Parts Used:
WPW10314173, WPW10359272, W11236646, WPW10512946
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Nutdriver, Screw drivers, Wrench (Adjustable)
worn out part
The repair was fairly easy. The most timely part of the repair was removing the twelve screws from the back panel to expose the repair.
41 of 60 people found this instruction helpful.
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Customer:
David from Joppa, MD
Parts Used:
279816
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers
The dryer would run i.e. the drum would turn, but there was no heat so the clothes didn’t dry.
I took a ¼ inch nut driver and removed the rear cover from the unit, and then used a continuity tester to determine which safety device was open. According to the schematic there was one non-resettable safety device in the heating circuit, and that was open. The kit that I ordered came with thermal cutoff and a thermostat. I replaced both parts and the unit now operates normally. While I had the dryer open I thoroughly cleaned the dust and lint from the unit and also the 4 inch vent pipe. I ordered this part on Friday morning and received it early Saturday afternoon.
33 of 37 people found this instruction helpful.
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Customer:
John from Saint Clair Shores, MI
Parts Used:
WP3364293
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Pliers
Original timer knob was plastic construction , twisted apart
The repair was very easy. The original dial was a poor design and did not hold up to the twisting and finally let loose. The threaded bottom of the dial stayed on the threaded shaft, so it was a simple matter of grabbing it with nose pliers and spinning off. Glue does not work with this type of plastic, I tried instant glue and hot glue. The replacement part was re-designed with a metal threaded center, so when it arrived in the mail, 3 days after online ordering, I spun it onto the shaft and job was complete. While I waited for the new part to arrive, I threaded 2 nuts onto the shaft and tightened them to each other to give me a temporary 'knob' that I could grab with my nose pliers.
31 of 32 people found this instruction helpful.
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Customer:
Edward from Easthampton, MA
Parts Used:
WP64067, WP64065, WP273556
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Pliers, Screw drivers
unbalanced load...knocking sound.
Unbalanced load was creating a knocking sound (as if the clothes load was unbalanced). Dismantled the washer to find that one brackets had rusted out. [FYI: 3 bracket at 120 degree apart (for the 360 degree circle)]. I found that the hole (on the bracket) where the spring holds was gone. Purchased parts. Replaced them (spring, bracket, screw). Reassembled washer then ran wash for a cycle. Successful fix.
31 of 36 people found this instruction helpful.
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Customer:
Bill from Houston, TX
Parts Used:
279570
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Dryer door catch broke
The old catch on my dryer door was gone and I was keeping the door closed using tape. I ordered the part and it arrived with no hassles in about 5 days. The repair was too easy. I just popped the new catch in place. It took all of about 30 seconds to complete using no tools. I wish all home repairs were this easy.
35 of 49 people found this instruction helpful.
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Customer:
ANTHONY from MONROE, NC
Parts Used:
WP3387134, 279816
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver
Dryer had heat intermittently and would take 3 cycles to dry a load of clothes
First, remove the back panel of dryer which is about 10 screws. Then remove the 2 thermal switches, one is above the heating element and the other is where the hot air comes out. They are both really easy to get to and the pictures on Part Select.com are identical, so you can order the part first and then just "match them up" if you are not sure what to replace. Oops, the first step is to unplug the dryer.
34 of 46 people found this instruction helpful.
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Customer:
Ted from SOUTH MILWAUKEE, WI
Parts Used:
285753A
Difficulty Level:
A Bit Difficult
Total Repair Time:
30 - 60 mins
Tools:
Screw drivers, Wrench (Adjustable)
Washer would fill/empty but would not agitate nor spin
Unplugged power cord and disconnected water lines; note which is hot/cold. Washer was then tipped on its front. Discharge hose was disconnected. Washer was then rolled over onto its back as this would put the pump on top for much easier removal.

Pried off two clips attaching pump on motor using a flathead screwdriver. The rear clip was done by touch. Unplugged wiring plug from motor. Using an adjustable wrench (socket set would have worked better), remove two screws holding 2nd set of clips attaching motor on transmission. Then pried off clips.

Removed old coupling from transmission shaft and motor shaft, plus middle 6 hole widget thingy.

Installed new parts on transmission shaft and motor shaft with fingers pointing towards each other. Using a small hammer, tapped the parts onto each shaft. Placed 6 hole widget thingy on the transmission part, and then rotated motor so motor part would fit in remaining three holes.

Replaced clips to hold motor on transmission and reinstalled screws holding clips.

IMPORTANT: Replace motor wire now. I forgot to do this and after the tub was filled with water, realized that, and since the pump was also disconnected, could not get the water out. Had to get wife to hold washer up while I crawled underneath to reattach motor wire. Learn from my mistake!

Attach pump onto motor and replace clips. Double check everything is back in place.

Roll washer onto front side. Attach discharge hose. Tip washer back upright. Reconnect water. Reposition discharge hose and plug washer into power.

First try it smelled like something plastic was burning, but I think that was the old part shavings getting ground away.
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All Instructions for the LTE6234DQ2
46 - 60 of 1478