LSG7806AAQ Maytag Washer Dryer Combo - Instructions
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- Customer:
- Phil from Grand Rapids, MI
- Parts Used:
- WP207166
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
washer would stop in mid cycle
Determined that the lid switch was not completing the circuit. I then removed the 3 wires from their posts along with the 1 screw and removed the bad switch. Then, in reverse order installed the new switch. The part was 1/3rd the cost of the part sold locally. I ordered the part at 3:15pm Monday afternoon and it arrived at 1:00pm Tuesday- the next day. UNBELEIVABLE SERVICE....!
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- Customer:
- Reece from Joplin, MO
- Parts Used:
- 6-2095720
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
Leaking from under tub
removed screws on front of washer, removed bolts holding top cover hinged back, nut driver to remove agitator, slipped agitator off, removed tub hoses, did not have special wrench to remove large nut on shaft, used punch and grinder to removed, had new large nut so wasn't concerned about damaging old one, pay attention to thread pattern to know how to turn, if you had special wrench job would be easier, removed spring bolts and took out inside drum and tub. cleaned corrosion and installed new seals, can be hard to slip on new seal, don't use grease, get dishwashing soap to use as lubricant to put on. Put back together and all is good.
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- Customer:
- Luke from Elmira, NY
- Parts Used:
- WP3387134
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver
Dryer would leave clothes damp
First, I unplugged the dyer and then I removed all of the screws for the panel that covers the rear of the dryer. This exposed the cycling thermostat's location. I then removed the wires, one at a time so I would be able to put them back on in the same place. Then I removed the one screw using a nut driver and then put the new cycling thermostat in place. It was pretty easy.
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- Customer:
- William from Batavia, IL
- Parts Used:
- 4391996
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Wrench (Adjustable)
Dryer would not heat.
First I removed the front panel on the dryer. While the dyer was running, I noticed the igniter did not turn its normal amber color and ignite the gas supply. I then disconnected the wire to the igniter and removed the screw holding the igniter in place. Next I replaced the igniter, tightened the screw and reconnected the wire. Finally, I replaced the front panel. This is a relatively simple repair.
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- Customer:
- Basil from St. Charles, MO
- Parts Used:
- WP6-2022030
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Socket set
Washer did not drain.
Took front panel off. Ran machine. Pump is see-through. Could not see any "aeration" of the water in the pump and no water was coming out of drain hose. Disconnected electric. Disconnected hose from drum to pump(first emptied ALL water from drom)and drained in bucket. Disconnected drain hose from pump to drain and drained any water. Checked for obstructions in hoses. Removed pump. Checked belt (was fine after 14 years). Ordered new pump. Received the next day! Replaced pump and tighten belt. Connected hoses and test it. All OK. Replace panel and did laundry.
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- Customer:
- James from Baton Rouge, LA
- Parts Used:
- WP6-2022030
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Standing water in washer tub
Thinking the water pump was not doing its job in removing all of the water after the rinse cycle, I replaced the water pump.
1. Unplug washing machine.
2. Remove front cover (2 screws).
3. Pull belt and hoses off pump body (watch for water in drain hose!).
4. Remove 3 screws holding pump to bottom pan. 5. Reverse process with new pump.
This job is straighforward, and it helps to have 2 wood blocks to prop up the front of the washer.
Unfortunately, this didn't fix my problem. Actual cause of the water in the tub was a leaking inlet valve (solenoid assy).
1. Unplug washing machine.
2. Remove front cover (2 screws).
3. Pull belt and hoses off pump body (watch for water in drain hose!).
4. Remove 3 screws holding pump to bottom pan. 5. Reverse process with new pump.
This job is straighforward, and it helps to have 2 wood blocks to prop up the front of the washer.
Unfortunately, this didn't fix my problem. Actual cause of the water in the tub was a leaking inlet valve (solenoid assy).
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- Customer:
- Franz from Lakeland, FL
- Parts Used:
- 12112425, 12112425, WP6-2008160
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
no water drain
removed old pully, put new one on with hex driver, removed belts, put new belts on and finished.
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- Customer:
- Joseph from Hampton bays, NY
- Parts Used:
- Y303836
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Noise in dryer
How to disassemble the dryer has been covered in past repair stories. I will add a make shift repair that will get you up and running until you get your replacement blower wheel. We repair gas dryers for a living and this repair works and some machines are still running for two years. Remove the blower wheel. Cut a piece of plumber strap of similar sized metal to about 3/16" x 1/2". Hold it with vise grips and then heat it with a torch. When it is hot melt it into the hole in the blower wheel. This will give you a flat spot in the shaft hole that will keep the blower from spinning on the motor shaft. Some trial and error fitting is involved. If you do it carefully the blower wheel will fit very nicely and will not vibrate or make noise.
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- Customer:
- ian from new york, NY
- Parts Used:
- W10411000
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers, Socket set
Motor needed replacing (even though it was only 8 years old!)
In addition to the other helpful suggestions:
The key to replacing the motor is to remove the motor while it is still clipped in to the bracket (after removing the blower assembly, of course.) Don't remove the tumbler and belt thinking it will give you clear access to the rear clip, because it won't.
Removing the bracket is not complicated. There are two screws that are fairly easy to access and keep the bracket in place (refer to parts diagram for location); when the screws are removed, out comes the motor assembly (after disconnecting the wires, of course.) This is the only way to get access to the two clips that hold the motor to the bracket.
As for those pesky clips, I was able to use a flat screwdriver in one hand and vice grips in the other to pry off the clips. After a few tries, working on one end of the clip, I was able to apply quite a lot of downward pressure without braking the end of the clip. If anyone has another suggestion....
Putting the clips back on was much easier. First, remount the motor to the bracket, making sure to rotate the motor to the 2 o'clock position so you can re-attach the ground wire (or else you'll have to unclip the motor again, like I did!) Then re-attach the clip on one side. With the clip aligned properly, bear down with a flat screw driver on the other end of the clip. A swift knock with a hammer on the top of the screwdriver will easily re-attach the clip. Repeat with the second clip.
If you proceed carefully and patiently, this job can be accomplished without specialized tools or expertise.
The key to replacing the motor is to remove the motor while it is still clipped in to the bracket (after removing the blower assembly, of course.) Don't remove the tumbler and belt thinking it will give you clear access to the rear clip, because it won't.
Removing the bracket is not complicated. There are two screws that are fairly easy to access and keep the bracket in place (refer to parts diagram for location); when the screws are removed, out comes the motor assembly (after disconnecting the wires, of course.) This is the only way to get access to the two clips that hold the motor to the bracket.
As for those pesky clips, I was able to use a flat screwdriver in one hand and vice grips in the other to pry off the clips. After a few tries, working on one end of the clip, I was able to apply quite a lot of downward pressure without braking the end of the clip. If anyone has another suggestion....
Putting the clips back on was much easier. First, remount the motor to the bracket, making sure to rotate the motor to the 2 o'clock position so you can re-attach the ground wire (or else you'll have to unclip the motor again, like I did!) Then re-attach the clip on one side. With the clip aligned properly, bear down with a flat screw driver on the other end of the clip. A swift knock with a hammer on the top of the screwdriver will easily re-attach the clip. Repeat with the second clip.
If you proceed carefully and patiently, this job can be accomplished without specialized tools or expertise.
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- Customer:
- Paul from Cedar Falls, IA
- Parts Used:
- WP207166
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Washer would fill but not continue the cycle
I looked at the common problems in the owners manual and one item was the lid was not closed or the lid switch was bad. I took off the control panel and there was a schematic inside. This showed 2 lid switches. When trying to see if one switch was closed as it should be, touching the multimeter to the contacts was enough to get the washer going. .
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Dryer did not turn off in auto-dry mode
Unplugged the dryer (electric), removed two screws at bottom of front panel and removed front panel. Pulled electrical clips from sensor lugs near center.front of drum exterior. Located sensor inside front of drum interior, removed screw at each end. Removed old sensor, placed new sensor in position, attached with screws. Installed electrical clips on lugs, closed front panel and secured with two screws. Plugged in the dryer and it worked!
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- Customer:
- JOHN from ERWIN, TN
- Parts Used:
- WP207166
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
washer fills with water wont start
checked lid switch ,plunger stuck in the in position 1 amp fuse blown took switch apart it was full of green copper corrosion stopping plunger from moving correctly. replaced switch and fuse and wow washer works
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- Customer:
- Fritz from Redway, CA
- Parts Used:
- 6-2095720
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Wrench (Adjustable), Wrench set
tub leaked
followed instructions elsewhere here. Procedure went flawlessly
To undo the nut I used a 1 1/2 " long x 5/16 bolt to hammer on.
STILL LEAKS. Needed PS2347235 =Tub Bearing Kit . Going back in...
THe remainder concerns the bearing procedure:
The 3 bolts holding the outer tub to the legs have rectangular washers. Those are not totally flat, and are marked for outside, top ... so pay attention. It might make a difference.
Outer tub came off the rubber bushing. Took some pulling the bushing off the shaft, and removing the sleeve bearing was a challenge at first, it would not move on the transmission shaft. Soaked with wd40 overnight. Drove it off with cold chisel (driving upward). For re-attaching the 3 tub bolts I used a ratchet tiedown strap to pull the 3 legs together to get enough thread to start, what with all those washers and things.
Ran spin cycle dry for 3 minutes as per instructions before filling with water. Success.
To undo the nut I used a 1 1/2 " long x 5/16 bolt to hammer on.
STILL LEAKS. Needed PS2347235 =Tub Bearing Kit . Going back in...
THe remainder concerns the bearing procedure:
The 3 bolts holding the outer tub to the legs have rectangular washers. Those are not totally flat, and are marked for outside, top ... so pay attention. It might make a difference.
Outer tub came off the rubber bushing. Took some pulling the bushing off the shaft, and removing the sleeve bearing was a challenge at first, it would not move on the transmission shaft. Soaked with wd40 overnight. Drove it off with cold chisel (driving upward). For re-attaching the 3 tub bolts I used a ratchet tiedown strap to pull the 3 legs together to get enough thread to start, what with all those washers and things.
Ran spin cycle dry for 3 minutes as per instructions before filling with water. Success.
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- Customer:
- Barry from Highland Park, IL
- Parts Used:
- 4391996
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
dryer wouldn't heat
First I unplugged the dryer. I shut off the gas line to the dryer. I opened the access door on the lower front of the dryer. I illuminated the interior of the dryer with a small flashlight that was mounted on two legs with magnets on the end to allow the light to be specifically directed. I took few digital pictures of the electrical connections to the dryer gas valve and the various sensors attached to the unit. I shut off the gas line valve to which the dryer gas valve was attached. I removed the two screws holding the dryer gas valve an lifted the unit out of the dryer. I vacuumed the inside of the dryer with an electric vacuum and also vacuumed the lint and dust off the gas valve I took out of the dryer. The flat style igniter was mounted on the front of the gas value. I removed two screws and took off the old flat style igniter. I reattached the new flat style igniter (carefully holding it by the ceramic mounting area to avoid breaking the igniter itself). I reinserted the gas valve into the dryer and reattached the two screws holding the gas valve into the dryer. I reattached the gas valve to the gas line in the dryer. I reattached the electrical connectors to the gas line and the sensors in the dryer. I turned the gas line in the house to the dryer back on. I plugged in the dryer and started it. No ignition.! I unplugged the dryer and reached in through the access door. I angled the flashlight to each of the sensors attached to the gas valve and the dryer electrical harness and pushed each one to make sure the electrical contacts were solid. When I checked the flame sensor ( a little box with a window mounted over a rectangle cut in the wall of the cylinder in which the flame burns when the gas is shooting out of the valve) the lower wire was unattached to the sensor. (Because the sensor sits on the side of the cylinder pointing towards the interior of the dryer its connections at the sensor was not visible. I bought a new flame sensor. I detached the old flame sensor from its connector, removed the screw mounting it to the cylinder and lifted it out of the tab holding it to the cylinder. I installed the new flame sensor by putting its tab in the slot for the tab in the cylinder and reattached the screw holding the flame sensor to the cylinder. I reconnected the electrical connection from the flame sensor to the dryer electrical harness. I plugged in the dryer. I turned the dryer on and got ignition of the dryer heater flame. Repair complete!
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- Customer:
- NICHOLAS from PARMA, OH
- Parts Used:
- WP338906
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Wrench set
No Heat
I suspected a faulty igniter and disconnected the cable to the igniter and measured the resistance of the igniter and found it to be 70 ohms then I checked the voltage at the same cable towards the power source and found it to be 25 volts ac which should be 120 volts ac. Next I checked the radiant flame sensor and found it to be open (it should be a closed circuit when cold). I removed the flame sensor (with the power off) using a small box wrench and found a broken lead. Replacing the flame sensor solved the problem.
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