MHW2000AWW Maytag Washer Dryer Combo - Instructions
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Dryer was not heating
My 20 year old reliable Maytag 512 lgp dryer was not heating anymore. At first the heating element would glow red but not hot enough to ignite the gas. I replaced the element and it worked for a few loads but then stopped reigniting after the first cycle.
After some research and diagnosis (checking connections, amperage flow on each electriical part, etc.) I determined that the two coils were faulty. I ordered parts and replaced them (easy to do) and it worked again, for another few loads. Then nothing worked. The coil did not get hot and I did not hear the clicking sound that initiates current flow to the ignitor through the coils.
I checked the coils and ignitor again, they were fine. Frustrated, I called in a repairman to diagnose the problem. $55 and 15 min later he narrowed it down to the High Limit Thermostat. To demonstrate he bypassed the thermostat by directly connecting the two leads together and the ignitor fired right up.
His price to replace the thermostat? $45 part plus $130 labor. I bought the thermostat online for less than half his parts cost and the labor took me 5 minutes. Simply unscrew the small screws with a small socket set or nutdriver and replace the thermostat. Just two connectors, real simple.
All in all it was very easy to replace the parts, just tricky to diagnose unless you are good with electrical work.
After some research and diagnosis (checking connections, amperage flow on each electriical part, etc.) I determined that the two coils were faulty. I ordered parts and replaced them (easy to do) and it worked again, for another few loads. Then nothing worked. The coil did not get hot and I did not hear the clicking sound that initiates current flow to the ignitor through the coils.
I checked the coils and ignitor again, they were fine. Frustrated, I called in a repairman to diagnose the problem. $55 and 15 min later he narrowed it down to the High Limit Thermostat. To demonstrate he bypassed the thermostat by directly connecting the two leads together and the ignitor fired right up.
His price to replace the thermostat? $45 part plus $130 labor. I bought the thermostat online for less than half his parts cost and the labor took me 5 minutes. Simply unscrew the small screws with a small socket set or nutdriver and replace the thermostat. Just two connectors, real simple.
All in all it was very easy to replace the parts, just tricky to diagnose unless you are good with electrical work.
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- Customer:
- Stacie from Las Vegas, NV
- Parts Used:
- W10181639
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
The spinner support had sheared off
First, I removed the drum. Removed the spinner support. Removed old seals. Reinstalled new spinner support. Reinstalled pulley and belt. Reinstalled drum. Reinstalled machine covers.
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- Customer:
- Gregory from El Dorado, AR
- Parts Used:
- 12002022
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Screw drivers, Socket set, Wrench (Adjustable)
Bearings making loud rough noise
Thanks to all the others who gave detailed information I was able to replace the front & rear bearings and front seal. I must say it was a time comsuming job but at least I am alot clearer on the quality of clothes washing machines. I do believe I could give a manufacturer / designer some design points after working on this Maytag Neptune. I was able to knock out the bearing shaft that held the stainless perforated tumbler inside the plastic tub/drum by using a #3 LB hammer I reinstalled the old screw in the shaft which held the plastic pully on because this would keep the end of the shaft from being damaged. After several blows it started moving I was afraid I might damage the plastic drum but fortunately no damage was done to it. After removing the stainless steel perforated tumbler here is where it really got interesting. The Hub that held the old seal was shot! pretty much deteorated from corosion it seems. Here is where I could significantly help a manufactured/designer out The bearing/seal hub should have been made out of stainless instead of Pot metal/ aluminum or whatever they made it from. After much cleaning with a small wire brush and vacuming all the debree out of the Tub I didn't have much hub left to install the new seal. Also the three armed Spinner was very coroaded it attaches to the back of the stainless tumbler I removed it from the stainless tumbler and wire brushed it the back side was full of crud, it looked like left over washing powder or soap and Corosion debree it was a job just cleaning it up. I pressed on and on though replacing both bearings front and rear. Thanks to another person who explained the easy way to remove the bearings and race I was able to do so without removing the Drum/Tub as others stated they had to do. The Dremmel and a few Cutter blades did the trick I cut a wide V notch in the bearings and the bearings fell out I then cut through the bearing race being careful not to cut too deeply although if you did slightly cut beyond the race it really wouldn't matter because the front seal will keep it from leaking anyway. Anyway when I cut through the race it made a ping sound and the race pulled away and fell right out of the HuB. The front & rear bearings a definately serviceable and it doesn't have to be a beat/bang ordeal. after cleaning up the hub I tapped the new bearings in place and discarded the metal spacer that went inside the middle of hub. I then brainstormed on how I could install the new Lip Seal upgrade and then it dawned on me that since the inner Hub that holds the seal was so far gone and only enough left to barely hold the new seal in I remembered the ole saying Don't Discard just use JB Stick or JB Quick I used JB Stick to fill in around the new seal because it is supposed to bond to metal and it did just that I pressed the putty in quickly before it hardened bringing it out even with the plastic drum where the origional hub should have been and made the repair to the deteriorated Hub so that the Seal would stay in place it Worked! This Maytag Neptune was given to me by my mother in-law she did not want to wait on the repair after I tried to previously repair the problem with it I just did not delv deeply enough into the problem with this washingmachine at first. I previously removed both Pumps thinking they were not pumping all the water out because the Towels especially were staying soaked. Both the pumps were nasty with alot of debree inside of them now I know that because of the deteriorated Seal Hub on the inside had done the dirty work. The Pumps can be easily taken apart only a few screws and the plastic impeller can be gently pried off also that is where I found alot of particles from the deteoriated Seal Hub I then reinstalled the pumps and they worked fine pumped out the water. Then that is when I noticed it wasn't cycling properly also Ha Ha I thought to myself what else could possibly be wrong with this washing machine? Thanks to Parts Select site I wa
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- Customer:
- James from Scotts Valley, CA
- Parts Used:
- 22003721, WP22003718, WP22003716, WP22003715, WP22003067, W10859556, WP22002162
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
Door would not lock, stopping the wash cycle
Wax motor was operational but door would not always lock. Rebuilt the latch mechanism with new parts including all three switches. Latch now makes an audible click when it engages, like it did when new.
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- Customer:
- Terry from Caruthersville, MO
- Parts Used:
- 33001790, WP33001789
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers
loud noise inside dryer
After changing all the rollers in the dryer (which didn't fix the problem) I decided to take apart the blower. Sure enough, that was the problem. As the dryer heated up, the damaged wheel would swell and start rubbing the housing. I replaced both and fixed the problem. The repair was pretty easy, since I had taken the dryer apart several times replacing the rollers.
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- Customer:
- William from Colver, PA
- Parts Used:
- 12002039
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Wrench set
LR Code on the display, washer would not spin.
Removed the front panel and took out the old control board, which had a burnt spot on it. Removed back panel and took out the old motor. Put in the new motor and then the new control panel. Runs perfect.
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- Customer:
- SALLY from ANAHEIM, CA
- Parts Used:
- WP33001762
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Dryer wouldn't start
We tried replacing the door switch first, still didn't start. Next we tried the thermal fuse and it turned on and has worked ever since.
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- Customer:
- Bick from Alameda, CA
- Parts Used:
- 12002039
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers, Wrench set
the problem is the motor
first i follow the instruction come with parts in box...and replace easy this the best place to buy parts for all home appliance...thanks
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- Customer:
- Shawn from Dover, NH
- Parts Used:
- 306436
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
broken clip for door latch
popped out old female clasp on dryer itself with screwdriver, undid 2 screws on dryer door and door handle with phillips screwdriver, popped in new male clasp part, put door knob back on and put the two screws back in door and it was all set to go. Less than 15 minutes to do. Better than new and wife is happy. No more duct tape holding door closed now.
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- Customer:
- PHILIP from LONG ISLAND CITY, NY
- Parts Used:
- 279834
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Time clock not moving .Not enough heat
Opened front panel .Tested both coils on gas valve.
Found no continuity on one of the coils. Replaced coil,
dryer works like new.
Found no continuity on one of the coils. Replaced coil,
dryer works like new.
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- Customer:
- john from richland, MI
- Parts Used:
- 12002022
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers, Socket set, Wrench set
Front bearings totally destroyed rear bearings rusted out
I found your site where other people worked on their washers . I removed the front & rear panels. at the front I found that removing the rubber tub seal was easy, then I removed the 3 agitaters that cover the nuts that hold the tub to the support drive shaft ,I saved the plastic shims nuts & washers then removed the tub,I removed the drive wheel, I put the bolt & washers back in the shaft end & knocked it out with a 1lb hammer.I removed the motor and all the hoses also the front & rear WeightsI left the switches connected to the wires, for everything I removed including screws I taped them all to the parts that they camefrom .Then I knocked out the rear bearing with a 8" long 1/2'dia.piece of steel rod taking care to drive evenly around the circomference of the bearing. the front bearing was in 2 pieces with the bearings in a pile inside the hub because of the spacer between the bearings there was not a lot of bearing to hit but eventually it came out I saved the spacer & the rear bearing clip & cleaned them up for reuse.The face of the crap metal insert was badly corroded ,I cleaned it and all surfaces inside the hub with a wire brush in my drillmotor I found bearings at an industrial store and found NO problem matching the old bearings I ordered the lipseal kit from Part select It came with 2 seals & dubious instrutions I found the revised seal did not fit my support shaft but the other one did ,it comes in 2 parts that are stuck together with grease pry them apart with e small screw driver. I then tapped the new bearings in rear first then the spacer. then the front bearing I tapped it in enough to get it started then I inserted a cardboard toilet roll center folded enough to go in through the spacer & the rear bearing this lined up the parts so the shaft will go throughafter the bearings & new seal were in I used a marine silicon to put over the corroded face & made shure that it snugged up to the seal ,sealing it good I let it set for 24 hrs Then I putthe shaft back onto the tub put the agataters back on, then put the outer shell with the new bearings back in place connected the hoses, the weights, the switches, the wire clips,the motor,hooked up the springs ,inserted the tub, put the drive wheel back on the shaft then the belt , then put all the front panels back and IT ALL WORKED. total cost $36.00 for bearings $53.00 for the seal kit so about $90.00 total & two weeks at about a couple of hours a day .shure beats $650.00 + $300.00 at a repair facility . GOOD LUCK .IAN
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- Customer:
- paul from madison, CT
- Parts Used:
- W10169313
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Switch did not turn off dryer when door opened
Switch can be removed from outside of dryer and your video described the repair as having to work from inside dryer. But since wires were still attached to old switch, it could be popped out and wires switched. Since there were three wires on new switch to allow it to turn on and off a circuit, it was useful to check the resistance of the switch compressed or released to be certain I was attaching the two wires to the right two poles of the new switch. But that all required only a couple of minutes. Thank you.
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- Customer:
- gary from tecumseh, MI
- Parts Used:
- 12002533
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Pliers, Screw drivers
door boot seal was all milldew
Unpluged washer. Removed screws from front and removed door. Removed one more screw on each side and was able to remove front panel, and also lift the top. The boot seal was held in place with a wire and a spring. I unhooked the spring and removed the wire and then removed the old boot seal. I then proceeded to reverse the steps to put it all back together. It took me almost 4 hours. I also used the picture on your web sight to see how things were put together. It really helped a lot.
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Burner would not go on on my Stack Set Dryer
Took out two front Panel screws and removed the panel. Removed Gas solenoid coil holding bracket by removing two phillips head screws. Disconnected the coil leads. and removed the coils. Connected the new coils to the leads and set in place. Replaced the holding bracket and the two screws. Replaced the front cover and the two front cover screws. Piece of Cake!
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- Customer:
- William from Jennings, FL
- Parts Used:
- WP22002452
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Screw drivers, Socket set, Wrench set
Washer would not drain
Since the machine would not drain, I suspected the drain pump. A friend in appliance repair tested that for me and it was good. All one has to do with that is hook a test line to the pump with 120 volts and if it runs it is good. He then told me to see it the mother board which is located in the right upper area above the dryer drum had a burned place at a resistor and to note if the door would not lock. I checked this and the circuit board was not damaged and the wax motor which locks the door was working OK. (This unit is a combo stack dryer and washer) I then suspected the timer because my wife told me that it had been making a grinding noise. The timer was replaced by the one you sent me and it solved the problem. ( My friend really did not want to work on this machine since he had replaced the inner drum and bearing about six months ago and it took all day)Thanks a bunch. The timer came in one day from the time of order.
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