ESE9900 Maytag Washer Dryer Combo - Instructions
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- Customer:
- Richard from Loretto, MN
- Parts Used:
- 306508
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
My dryer - which is about 20 years old - was starting to make some rubbing/scraping sounds from the drum area.
This was pretty much as easy as most other folks had described on this site.
1. Removed the two screws at the front bottom that are holding on the fromt panel, and then lift up and remove the panel.
2. Disconnect the door-open-safety-switch, remembering which color of wire goes on which connection.
3. Remove the four screws (two on each side) on the front bracket that supports the drum and tthat contains the front glides.
4. Remove support bracket and lint trap, letting the drum rest gently on the stuff underneath.
5. Remove the screws holding the lint trap to the support bracket. (My model had five screws.) Remove lint trap from support bracket.
6. Drill out the two pop rivets on each of the two glides, noting the orientation of the teflon pad and mounting strip.
7. Secure - and here is where I had a little problem - new glides in place with pop rivets. (I hadn't use a rivet gun in a while, so I messed up the first pop rivet and had to go to the hardware store to get a replacement. I didn't hold the pop rivet in all the way while I was accuating the gun!)
8. Reverse the process for assembly, and you are all done.
It's simple.
1. Removed the two screws at the front bottom that are holding on the fromt panel, and then lift up and remove the panel.
2. Disconnect the door-open-safety-switch, remembering which color of wire goes on which connection.
3. Remove the four screws (two on each side) on the front bracket that supports the drum and tthat contains the front glides.
4. Remove support bracket and lint trap, letting the drum rest gently on the stuff underneath.
5. Remove the screws holding the lint trap to the support bracket. (My model had five screws.) Remove lint trap from support bracket.
6. Drill out the two pop rivets on each of the two glides, noting the orientation of the teflon pad and mounting strip.
7. Secure - and here is where I had a little problem - new glides in place with pop rivets. (I hadn't use a rivet gun in a while, so I messed up the first pop rivet and had to go to the hardware store to get a replacement. I didn't hold the pop rivet in all the way while I was accuating the gun!)
8. Reverse the process for assembly, and you are all done.
It's simple.
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- Customer:
- Pedro from Portland, TX
- Parts Used:
- WP213045
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers
Washing machine was leaking water from the bottom.
Hardest part was figuring out how to access the internals (not through the back or the top) It turns out there are two screws on the lower front of the machine, not easily found, which when removed allow the front panel of the machine to swing to front and out of the way allowing full access to the internals from the front. The water was comming from one of two water pump hoses. The hose was held in place with 1" hose clamps and was easily changed out.
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- Customer:
- James from Lakewood, CA
- Parts Used:
- 206638
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Small puddle of water on floor after water drains out.
I first removed the 2 screws at the bottom of the front panel. The front panel then pulls up and off. I then removed 2 hex head screws with a small socket, which kept the top attached to the two side panels. I then lifted the top and kept it propped up. I removed the internal drain hose from the siphon break on the inside of the back panel. I removed the 4 screws on the back panel that keeps the siphon break in place. I removed it and screwed in the new one. I re-attached the drain hose to the new part. I partially filled the tub and watched it drain with the lid still upright. No more leaks. The rubber seal in the siphon break had rotted.
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My Blower wheel had broken at the center where it attached to the axle. It made a rattling sound and no air was being blown into the drum to dry the clothes. There was also a loud skidding sound that turned out to be due to a worn felt seal.
I took off the front of the dryer with the screws at the bottom. I removed what wires would easily come off and took a picture to remember where they go. Then I took of the front panel and had to take off the cover for the blower wheel. Some screws were difficult to reach because they were in a very tight space. I used a combination of needle nose pliers and a hex screw bit to loose hared to reach hex screws.
For the felt seal on the front panel, I used a flathead screwdriver to remove the old seal and replace the new seal. The most tricky thing was making sure the seal was laying right along the drum when putting the front panel back on. Once back together, the skidding sound disappeared.
Replacing the blower wheel is pretty easy once I got past the difficult screws holding the cover down. I used snap ring pliers to remove the snap ring then put the new blower wheel on and put it all back together. I found that the tip diameter of the snap ring pliers needed to be less than 0.05'' to fit into the snap ring holes of both the snap rings for the roller wheels and the blower wheel.
For the felt seal on the front panel, I used a flathead screwdriver to remove the old seal and replace the new seal. The most tricky thing was making sure the seal was laying right along the drum when putting the front panel back on. Once back together, the skidding sound disappeared.
Replacing the blower wheel is pretty easy once I got past the difficult screws holding the cover down. I used snap ring pliers to remove the snap ring then put the new blower wheel on and put it all back together. I found that the tip diameter of the snap ring pliers needed to be less than 0.05'' to fit into the snap ring holes of both the snap rings for the roller wheels and the blower wheel.
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- Customer:
- Chris from Hoffman Estates, IL
- Parts Used:
- WP22003410
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Hose had a split in it
took off front of washer , took off hose clamp removed old hose . replaced with new hose clamped back on put on front cover ran washer check for any leakes. done and done
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- Customer:
- Edward from EUCLID, OH
- Parts Used:
- WP6-2011900, WP22003441
- Difficulty Level:
- Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
Washer made screeching sound during spin cycle. Also, the clothes were still very wet at end of spin cycle.
I used two vise grip wrenches in place of specialized tool that is no longer available. I put the vice grip wrenches on the brake assembly and hit them alternately with a hammer. I also used penetrating oil.
Note, the parts package stated made in USA but the bearings had China stamped on them.
Note, the parts package stated made in USA but the bearings had China stamped on them.
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- Customer:
- william from elmhurst, IL
- Parts Used:
- 205613
- Difficulty Level:
- Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
hot water not working in 30 yr old washer
-determined problem
--verify that hose not clogged, screen filters clean then swapped cold w/ hot and verified that the problem was in the hot valve.
-Moved washer to get access to hot/cold valves
--opened access panel holding valve and swapped wires between hot/cold to verify that hot did not activate when it should
--Used voltohmmeter to verify that hot water valve had open circuit.
--Obtained replacement valve, installed, reconnected water lines and verified that hot and cold water worked.
--verify that hose not clogged, screen filters clean then swapped cold w/ hot and verified that the problem was in the hot valve.
-Moved washer to get access to hot/cold valves
--opened access panel holding valve and swapped wires between hot/cold to verify that hot did not activate when it should
--Used voltohmmeter to verify that hot water valve had open circuit.
--Obtained replacement valve, installed, reconnected water lines and verified that hot and cold water worked.
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- Customer:
- Ken from Rochester, NY
- Parts Used:
- 306436
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Latch was broken over 15 years
Old latch and door striker were pried out with a flat blade screwdriver. New components popped right in. Repair was less than two minutes.
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- Customer:
- Franz from Woodcrest, CA
- Parts Used:
- 206638
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Screw drivers, Socket set
water leaking from machine during spin cycle
I initially could not figure out how to open the machine so I checked the internet for a repair manual. After getting it open I found the source of the problem. The siphon break was missing the diaphragm and was spitting water when the tub was draining. I did not know what a siphon break was or did. I am non mechanically inclined. So I sealed the top of the siphon break with a sandwich bag and a zip tie, put in a load and went to work. I now know what the siphon break does after it ran all day filling and draining for over 8 hrs. That is when I found this site, ordered the part and received it the next day as promised. It took about 10 minutes to put the part in and close the washer back up. It has been a week now and the garage is almost dry . HA , and my wife wanted a new washer ! This part and delivery was under $25. A new machine around $800 if I am lucky. The ability for me to be smug as long as she never finds out about the sandwich bag incident, PRICELESS !
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- Customer:
- Luis from Naperville, IL
- Parts Used:
- 306062
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Controller board display showed error F for both dryers on running mode but it wouldn't accept any command; went into the set up and here display showed F5. C
The difficult part was to find what component was bad. Maytag does not sell the manual for this machine any more. We could not figure out what the problem was until we decided to check the voltage on the board and compare it to a second machine that we have. The second machine showed different readings so we decided to compare voltages on the transformer (main) that is at the bottom of the machine. There is a Primary (110 volts) and two secondaries; one which output is about 26 VAC and the other is above 10 VAC. The bad transformer had no output in one of the secondaries. Replacing the transformer was pretty simple. Make sure to disconnect the machine please before doing the repair.
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- Customer:
- Dean from New Lenox, IL
- Parts Used:
- 203956
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Washer was shaking and not balanced
The instructions were clear. Did every step. Did 2 loads so far and everything works like new.
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- Customer:
- Chad from BOERNE, TX
- Parts Used:
- WP6-2011900, WP22003441, 12112425
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers, Socket set
Washer making high pitched squeal at stopping of spin cycles
My washer is apparently 37 years old. I bought it used in the 90’s and have had to do little or nothing to it repair wise. It started to make a loud squeal/squeak when the spin cycle stopped. I watched a couple videos showing the brake assembly, bearings and belt replacement and was able to find parts. However, one bearing appears to no longer be made (just repacked with heavy duty grease) and the special tool is nonexistent. I read others using a chain clamp vise to remove the brake assembly and bought a 20 inch chain clamp vise and a 3 set variety of vise grip pliers for about $20. They make an 18 inch chain vise but glad I got the 20 inch. I used two vise grip pliers to clamp chain around notch two notches that the specialty tool would normally grab. It was a cumbersome getting in there to whack the pliers with a small sledge hammer so I got a approx 18 inch 2x4 and cut a notch at the end to keep chain vise from digging into bottom of washer and whacked the end of the 2x4. Seemed to work ok and did the same to tighten back after replacing break assembly. Got it out back together and no more squeal.
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- Customer:
- Anthony from CHESANING, MI
- Parts Used:
- 207843
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set, Wrench set
Oil leak from lower lip seal
I didn’t have special tool for brake but punch and hammer worked. Seal was easy to replace. Several videos online to show you how. It wasn’t worth it to tear apart the transmission and buy more parts/seals (if they were even available). But I didn’t know how much oil was in it. I drilled a hole in the side to somewhat check level and added 80-90 gear oil. It was almost empty and added almost a quart. Used a self taping screw/bolt with gasket sealer to plug the hole. I got 34 yrs out of this washer. If it fails, oh well. Just hate to buy a new one that only last 10yrs if im lucky.
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- Customer:
- Nicholas from Little Canada, MN
- Parts Used:
- 205613
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Washing machine didnt fill with hot water.
The repair was very simple.
1. Shut off water and disconnected the water lines.
2. Removed screws holding water valve bracket to wash machine.
3. Disconnected electrical connections and water fill hose.
Installation was reverse of removal. The directions said to use a small piece of rubber hose that was included in the package, but it was not necessary. Double check for water leaks before finishing installation.
1. Shut off water and disconnected the water lines.
2. Removed screws holding water valve bracket to wash machine.
3. Disconnected electrical connections and water fill hose.
Installation was reverse of removal. The directions said to use a small piece of rubber hose that was included in the package, but it was not necessary. Double check for water leaks before finishing installation.
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- Customer:
- Larry from Swanton, OH
- Parts Used:
- WP303396
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Dryer ran hot
Took off door, then removed front of dryer to access the internal controls. Project went pretty darn well
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