YMEDB755DW0 Whirlpool Dryer - Instructions
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Dryer making loud squealing noise when running
The (front) bearing and seal are not metal parts but a fabric and and mesh like material. It is somewhat like a fabric belt made to hold up a pair of trousers. The belt sits in a channel that goes around the door on the inside of the front panel. To get to the combination bearing/seal you remove two screws that are located under the cover of the lint trap. These have to be removed to lift the top. Then using a putty knife or screw driver you must pop the top (which snaps down on plastic clips) at the front corners. The top lifts up and folds back on hinges. The front is attached to the sides by one screw on each side near the top. A nut driver will remove then easily. Once the 2 screws are removed lift the front panel about 2 inches to disengage the front panel from the clips that hold the front attached to the sides near the bottom. When you remove the front panel the dryer drum will literally fall out so you want to get hold of it before pulling the front panel away so it isn't damaged and and doesn't damage the gas burner assembly which is under the drum to the left side. The drum is very light. I supported it with an empty shoe box while the front was off.
Once the front is off you'll see the bearing/seal on the inside of the front panel and it will be obvious how to remove the old one and place the new one. There are three pegs on the front panel that receive the three holes in the fabric bearing/seal. The seal will stay in place while you remove the shoe box and put the front cover back on. The drum fits over the seal like a lid on a jar and just slides on the fabric when the drum rotates. Low tech but the drums slides easily on the bearing material and seems to last a long time.
I also did the rear dryer seal. This is similar to the front. To do this you follow the procedure above but to get to the real seal you will have to remove the drum. It will fall out on its own if the front panel is removed. The drive belt goes around the drum. It is about 3/8th of and wide and just wraps around the drum without any teeth or channels or anything. Let the belt fall to the bottom as you lift the drum forward and out of the cabinet. The drum is light. Just put it on the floor and strip off the old rear seal which is glued on. It too is fabric. Clean up the drum a little and fit the new seal on the drum. Once the seal is on the drum you can lift the edge of the fabric seal and glue the fabric flange to the drum. This becomes pretty obvious once you have the seal on the drum. If you put the glue on the drum first you will make a mess. Put the seal on properly and the lift the edge to apply the adhesive all the way around. The adhesive sets enough in a hour or so. Put the drum back in and replace the front panel. Don't forget the drive belt. It goes around the drive motor that is located on the bottom of the dryer on the right, around or over an idler pulley (my older model does not have a idler wheel but rather a bracket with a "slide" that the belt runs over that keeps sufficient tension on the belt to drive the drum. If your belt falls off the motor and the idler pulley falls out it may be confusing how the belt goes in. My idler bracket is held in slots on the bottom of the cabinet merely by the tension of the belt - no screws or anything. I suggest that you put the belt around the drum first, then the drive motor. You will have slack in the belt and it becomes a little more obvious how the idler pulley (which is mounted on spring steel) goes in and takes up that slack and keeps modest tension on the belt. The rubber side of the belt goes against the drum, the leathery side is the outside.
Once the front is off you'll see the bearing/seal on the inside of the front panel and it will be obvious how to remove the old one and place the new one. There are three pegs on the front panel that receive the three holes in the fabric bearing/seal. The seal will stay in place while you remove the shoe box and put the front cover back on. The drum fits over the seal like a lid on a jar and just slides on the fabric when the drum rotates. Low tech but the drums slides easily on the bearing material and seems to last a long time.
I also did the rear dryer seal. This is similar to the front. To do this you follow the procedure above but to get to the real seal you will have to remove the drum. It will fall out on its own if the front panel is removed. The drive belt goes around the drum. It is about 3/8th of and wide and just wraps around the drum without any teeth or channels or anything. Let the belt fall to the bottom as you lift the drum forward and out of the cabinet. The drum is light. Just put it on the floor and strip off the old rear seal which is glued on. It too is fabric. Clean up the drum a little and fit the new seal on the drum. Once the seal is on the drum you can lift the edge of the fabric seal and glue the fabric flange to the drum. This becomes pretty obvious once you have the seal on the drum. If you put the glue on the drum first you will make a mess. Put the seal on properly and the lift the edge to apply the adhesive all the way around. The adhesive sets enough in a hour or so. Put the drum back in and replace the front panel. Don't forget the drive belt. It goes around the drive motor that is located on the bottom of the dryer on the right, around or over an idler pulley (my older model does not have a idler wheel but rather a bracket with a "slide" that the belt runs over that keeps sufficient tension on the belt to drive the drum. If your belt falls off the motor and the idler pulley falls out it may be confusing how the belt goes in. My idler bracket is held in slots on the bottom of the cabinet merely by the tension of the belt - no screws or anything. I suggest that you put the belt around the drum first, then the drive motor. You will have slack in the belt and it becomes a little more obvious how the idler pulley (which is mounted on spring steel) goes in and takes up that slack and keeps modest tension on the belt. The rubber side of the belt goes against the drum, the leathery side is the outside.
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- Customer:
- charles from waukesha, WI
- Parts Used:
- WP3392519
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver
the dryer only blew cold air
actually i found your site before i even looked at the dryer,thats how i knew to check for the thermal fuse.
I ordered the part and it was on my door in 36
hours,pulled the two wires off the old fuse and installed the new,put the back cover on and it has been working ever since,thanks ( your in my bookmarks)
I ordered the part and it was on my door in 36
hours,pulled the two wires off the old fuse and installed the new,put the back cover on and it has been working ever since,thanks ( your in my bookmarks)
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- Customer:
- John from Bluffton, SC
- Parts Used:
- WP3392519
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Wrench set
Dryer motor would not turn on
After looking at the schematic to see what was in line with the motor, I found the fuse as the first item. I pulled the fuse out and used a multimeter to ohm out the fuse. Upon using the meter I found that the fuse was bad. I typed into Google my part number that was on the fuse and the PartSelect Website came up as one of the choices to pick from. When the part arrived approx. two days later I installed the fuse by first unplugging the dryer and then removing the bottom panel and removing the fuse from the exhaust by using a small 1/4 inch wrench and pulling out the old fuse. I installed the wires on the new fuse and re-installed and put the 1/4 inch screw back in. I started the dryer after plugging it back in and it worked like it should have. Thank you for the part and I have recommended your website to other people already.
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- Customer:
- Nick from Brandon, FL
- Parts Used:
- WP3392519
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver
No power
My 14 year old son did it as I supervised! Pulled the dryer out on a dolly, unpluged the dyer, removed 9 hex head screws to remove the back cover, removed and replaced the thermal fuse, located next to the exhust outlet, set the cover back on, moved the dryer back in with the dolly. I had the thermal fuse over nighted to me for a total price of $35, figured I saved at least $150 on a service call by Whirpool.
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- Customer:
- Jesus E from Palm Bay, FL
- Parts Used:
- 4392065
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers
dryer makes a lot of noice, bad rolleres
super fast shipping, got the part in two days, and had it done in 15-20 min, remove the front pannel, remove the belt and tenssioner,took the drum out , took the old rollers , lubed the shafts,replaced the old rollers with the new ones, intalled the drum back, the tenssioner and the new belt, reinstalled the front pannel, and done...easy and fast job, like new dryer, works nice...save some money...the new one will do the same..just dry the clothes.
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- Customer:
- Clifford from Mastic, NY
- Parts Used:
- 4392065
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Wrench set
Dryer stopped tumbling
Pryed the top off the dryer, unplugged the door switch, took the screws out of the front panel, then lifted the drum out. Placed the new belt around the drum and while my wife held it in place and steadied it, I reached underneath and looped the belt through (as per instructions), reassembled and back in business! Reaching under the drum was not that easy....VERY tight space to work in and there was no way I could get both hands through, I almost gave up, but one last try and a couple of good grunts, and it popped into place. Getting the wires back on the door switch was a bit of an ordeal too. Took about 30 mins. but still worth it. I'm sure I saved at least a $100 repair.
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- Customer:
- Robert from GOODRICH, TX
- Parts Used:
- WPW10314173
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
A high pitched squeal when drum was rolling.
First my son and I moved the dryer to the garage as we believed there would be a lot of lint possible during disassembly. Used a flat head screwdriver to pop the top from dryer housing. Then removing 2 nuts to facilitate the removal of the front of the dryer. The drum was able to be removed to diagnose the offending drum roller wheel. The drum roller wheel has experienced a failure as it had melted off of the metal spacer. Removing it and replacing with the new one was pretty easy. We then used a shop vac and an air hose to clean out all the lint, coins, paper clips and lost jewelry. Surprisingly there was not a single sock in there. Put it all back together in reverse order and plugged it in and now spins like a dream.
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- Customer:
- Shawn from Akron, OH
- Parts Used:
- 4392065
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Dyer drum doesnt turn
It was really quite esy remove the screws from the back and pop the top off . then remove 2 top inside screws from the front , lift the front off the sides , support the drum and lift out , you will then see the idler wheels, replace them with the new ones ,replce the tensioner , wrap the belt around the drum, need help putting the drum back in the case, have someone hold the drum in place while you lay on the ground and put the belt around the motor pulley and the tensioner on the bottom.you then put the front panel back into place and secure with the 2 inside screws, then put the rest back together in reverse oder. ... hope this helps someone
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- Customer:
- charles from parker, CO
- Parts Used:
- 279827
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers
had to replace the motor
Follow the advice given in the partsselect website. However, while removing the blower, my hand slipped into the housing and cut my thumb. Connected the wires to the junction box on the motor but didn't realize that the contacts would hit the drum when reinstalled. The original junction box was at a 90 degree rotation relative to the new box. When trying to test the breaker tripped. Using the multitester I found out that I burned out the thermal fuse, and froze the door switch. I replace both those parts and started the dryer and could hear a grinding sound. Inspection revealed that the housing of the motor was rubbing against the drum. Removing the drum yet again, I rotated the housing and replaced the drum. The dryer was finally working well.
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- Customer:
- Jim from Tucson, AZ
- Parts Used:
- WP8577274
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers, Socket set
Unit would shut down in the middle of cycle and flash E1 trouble code
Had to remove the back of unit to access the area of subject part by removeing 12 to 14 screws also the gas line had to be removed. Two screws held the part in place. Unit now runs normal.Saved alot on repair costs!!!!!
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- Customer:
- Charles from Gray, TN
- Parts Used:
- 4392065
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
Drayer Was Making Squeaking Sound
Took off the top and front panel. Found that the belt tensioner was worn out. Decided to pull drum out,and replace the belt and drum rollers also. Put it back together, and it works fine.
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- Customer:
- Jeff from Mesa, AZ
- Parts Used:
- WPW10314173
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable), Wrench set
noisy drum
the job would have gone faster if the right parts had been sent in the first place. I would have never paid for two day shipping. In the repair, I removed the rear panel, clipped the plastic triangle holding the bearing, installed the new bearing and new clip.
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- Customer:
- Michael from Maricopa, AZ
- Parts Used:
- WP3406107
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Broken door switch
Followed your online video for disassembly and it was not only educational but actually quite simple. I would recommend that you start the video with," make sure the power cord is disconnected from the power source". I have worked on numerous pieces of large electrical equipment and would strongly suggest this be added. Some people think if it's, "off", it's safe. Your phone staff when ordering was great. We will do business again.
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- Customer:
- Ernest from Beaumont, TX
- Parts Used:
- 279827
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
Dryer would quit before the end of the cycle
My wife reported that the dryer was not working. I checked it and it seemed to work fine. This went on for about a month or two. Every time I checked it, it started just fine.
Well, she threatened to go buy a new dryer, I took her more seriously. I thought perhaps a thermal protection was the cause. But when I dug into it, I learned that when those trip out, they are permanent (have to be replaced).
I finally noticed loud humming sound the motor made at start-up, when it failed to start turning on one occasion and eventually tripped out the motors thermal protection.
I ordered the new drive motor form PartSelect.com.
Replacing the motor was fairly easy if you like to take stuff apart. One thing that I had not anticipated was that the two foam gaskets on the exhaust duct were dry rotted. I went to my local part supplier to get them. They did not have them in stock. :( While I was there, I asked how much the motor was, they wanted $50 more than PartSelect.com :D
I put it back together without the new gaskets, and it runs like new. I ordered the gaskets from PartSelect and will add them when they arrive.
My wife is happy again, she can bust out the laundry in one day; it had been taking here all weekend.
I learned to take her at her word.
Well, she threatened to go buy a new dryer, I took her more seriously. I thought perhaps a thermal protection was the cause. But when I dug into it, I learned that when those trip out, they are permanent (have to be replaced).
I finally noticed loud humming sound the motor made at start-up, when it failed to start turning on one occasion and eventually tripped out the motors thermal protection.
I ordered the new drive motor form PartSelect.com.
Replacing the motor was fairly easy if you like to take stuff apart. One thing that I had not anticipated was that the two foam gaskets on the exhaust duct were dry rotted. I went to my local part supplier to get them. They did not have them in stock. :( While I was there, I asked how much the motor was, they wanted $50 more than PartSelect.com :D
I put it back together without the new gaskets, and it runs like new. I ordered the gaskets from PartSelect and will add them when they arrive.
My wife is happy again, she can bust out the laundry in one day; it had been taking here all weekend.
I learned to take her at her word.
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- Customer:
- Dixon from Santa Fe, NM
- Parts Used:
- WP8577274
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver
Dryer turns off after 1-2 minutes
I tried to follow directions followed by others on this site after diagnosing the problem via suggestions provided by users. I have a Whirlpool Duet dryer from 2002. We've had problems since moving about 3 years ago. I removed the front panel (lower) by unscrewing the two bottom screws (1/4" sheet metal screws). Then I took out the lint screen and the metal tube/contraption immediately beneath to get access to the area where thermistor is located. See the drawing/chart to help you locate this. It's really easier than it seems. Make sure you have the chart/drawing for your model - it makes difference! The thermistor came out pretty easily with a nutdriver that has a swivel offset shaft. Ask your hardware store tool dept. about that one. Put everything back in reverse order of course and test either with/without the front panel re-attached. In my case it fixed at least part of the problem. I was able to get clothes almost dry with most settings but I have yet to install the moisture sensor to see if that helps in addition to the internal-bias thermistor. I am the kind of person that does one thing at a time so at least I now know the thermistor was bad. Good luck and hang in there with your own repair. It's a lot cheaper even if it takes you longer to do than a pro.
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