YWED9290FC0 Whirlpool Dryer - Instructions
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- Customer:
- Julian from San Antonio, TX
- Parts Used:
- 4392067
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers
Noisy/Rattleing Tumbler
First i did some research on the internet approx.1yr ago.Just in case any problems like this or any other kind of problems should arise which it did.The whole thing is Easy all you have to have is some basic knoledge of how things work.All of this came "OFF" in (4) sections.After installing everything back it was as "Quiet"as the day we purchased it.Good for another 5yrs.Retired welder & "J.O.A.T.Julian San Antonio,Texas
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- Customer:
- Jack from Gilbertsville, PA
- Parts Used:
- WP8577274
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Socket set
Dryer shutting down two to five min. into cycle E- 1
Removed the front lower skirt with two 1/4"hex screws. Vaccumed all inner parts exposed. Removed three 1/4" screws holding the blower housing.Memoved the bias thermister again two 1/4" screws. Make sure all inner exaust pipes and rear chimney gas or electric are clean and lint free. Re assemble and test the unit. Install the skirt and make sure the dryer is level Jack, Pa.
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- Customer:
- Lynn from Huntsville, AL
- Parts Used:
- WP8577274
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
no heat in dryer
diognostic suggested thermal fuse or thermistor. Thermistor tested low resistance (<2K olms). Replaced thermistor and dryer heat returned.
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- Customer:
- Beth from Valley Springs, CA
- Parts Used:
- 49621
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers
Washer overflowed
Once I watched a YouTube video showing me how to do the job I ordered the part from you. Am so impressed with your fast shipping and best prices via the Internet. Thank you SO much! The water level switch was easy to install, it ws getting the cover on the washer back on that was hard for me since I am 68 yrs old and have a bad knee. Its why it took me two hours to do what most people could do in 20 minutes.
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Noisy dryer
follow the video NOTE the felt seal was about 1.75 inches short. carefully stretch it by standing on it and pulling up on it, gradually increasing force and rotating the seal after holding a stretch for a count of 10. once it's stretched, glue it on pretty quick, it will shrink back again. this was the only surprise I encountered. my dryer runs like new now.
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Grinding and squeaky noise coming from dryer
Found a YouTube video with step by step instructions for disassembling a Whirlpool Duet dryer. Though not the same model as mine it was close enough. The hardest part of this repair was figuring out how to pry apart the elctrical connectors but it's pretty simple once you get the hang of it. You also might want a little help taking off the door. It's not mandatory ( I'm a big guy and I managed it by myself) but having an extra pair of hands makes things easier. If you can take out screws and remember the order you took them out you should not have any problems. The actual pully assembly was held in my one bolt, easily replaced once you get access to it. If you don't want to change out the belt, removing the door is not necessary as you can get to the pully from the back side of the machine. But since you have it halfway disassembled already, you might as well go for it and not have to make a return visit. Total time including vacumning out all the lint from inside the dryer was three hours. Took my time and saved myself a few hundred dollars for sure.
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- Customer:
- MARK from LEWISVILLE, TX
- Parts Used:
- 4392067
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
screetching noises and rubbing noises
The tear down on the dryer was more difficult than the instructions and internet showed due to different models used. The kit was not identical to the original parts but close enough to work (I think). The biggest issue we had was getting the drum back in and placed on the wheels where it would turn easily. Overall the repair came together but it was a bit more involved and we anticipated going into the project. The actual noises were caused by the disintegration of the tensioner wheel which broke and was wobbling on the axel.
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