7MWGD1900EW0 Whirlpool Dryer - Instructions
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- Customer:
- Richard from Davie, FL
- Parts Used:
- 341241
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver
Drum stopped turning, fan continued to blow
Disconnected supply. Lifted top (hinges on rear). removed two 1/4 hex head screws retaining front panel. Disconnected door switch wires. Removed front panel, lifting off from bottom tabs. Lifted out drum and discarded broken belt. Spent 30 minutes+ cleaning interior, drum skid area, dryer exit tube, motor pulley, belt tensioner, etc, etc. Checked wiring harness for possible damage (no damage found). Repositioned drum skid pads, which had become dislodged from their intended position. Reinstalled the drum with new belt, ensuring both belt & tensioner were correctly positioned, and drum rollers and felt seals were also correctly positioned. Reinstalled front panel, tightening the two 1/4 hex head retaining screws. Reconnected power. Checked functionality. Closed top cover.
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- Customer:
- Arron from El Reno, OK
- Parts Used:
- 279769
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Dryer motor runs,drum turns but no heat.
Removed the back of the dryer. Used a multimeter set to read Ohms to check each Thermal cut-off switch. Each one read with continuity and some resistance. The one that was bad read open. So i replaced this one and the other one that came in the kit since i already paid for both.Then i replaced the back ran the dryer and it worked great.
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- Customer:
- J. from Oakdale, NY
- Parts Used:
- 341241
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Dryer belt snapped
There are a total of six screws that have to be removed to do this job.
Take the lint tray out and remove the first two screws.
Secondly, remove the lower panel in the front of the dryer. You do this by inserting a screwdriver at the top portion and pry it off. Next, loosen the two screws under the top panel in the front of the dryer.
Now take your screwdriver and pry up the top lid of the dryer. The last two screws are in the inside of the front panel. They hold together the front and side panels. Remove them and be sure you have a support for under the dryer drum. (once you remove the front panel, the drum no longer has a way to stay suspended)
(Make sure you disconnect the wires attached to the front door, making note of which wire goes where.)
At this point, You can follow the easy instructions that come with your new belt.
If you have a little mechanical aptitude, this is a very easy project.
Take the lint tray out and remove the first two screws.
Secondly, remove the lower panel in the front of the dryer. You do this by inserting a screwdriver at the top portion and pry it off. Next, loosen the two screws under the top panel in the front of the dryer.
Now take your screwdriver and pry up the top lid of the dryer. The last two screws are in the inside of the front panel. They hold together the front and side panels. Remove them and be sure you have a support for under the dryer drum. (once you remove the front panel, the drum no longer has a way to stay suspended)
(Make sure you disconnect the wires attached to the front door, making note of which wire goes where.)
At this point, You can follow the easy instructions that come with your new belt.
If you have a little mechanical aptitude, this is a very easy project.
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- Customer:
- tony from prineville, OR
- Parts Used:
- WP3389441
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Top door catch assembly had broken
It was so easy, that my wife did it the day we got the part before I got home from work. She wedged it out with a flat head screw driver and then pushed the new door catch assembly in with her thumb. Pretty simple, thanks for having parts like this available to the public!
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- Customer:
- Bill from Houston, TX
- Parts Used:
- 279570
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Dryer door catch broke
The old catch on my dryer door was gone and I was keeping the door closed using tape. I ordered the part and it arrived with no hassles in about 5 days. The repair was too easy. I just popped the new catch in place. It took all of about 30 seconds to complete using no tools. I wish all home repairs were this easy.
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- Customer:
- rex from streator, IL
- Parts Used:
- 279311
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Wrench (Adjustable)
no heat
the ignitor did not glow red checked thermal fuse by exhaust duct. fuse open replaced thermal fuse
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- Customer:
- Chris from Morgan City, LA
- Parts Used:
- W11778253
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
old lint screen -torn at wire mesh
Local stores did not have any in supply. Went to Partselect and located lint screen, ordered, received in 3 days. replaced screen, Wife now happy again...
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- Customer:
- Billy from Maryville, TN
- Parts Used:
- 49572A
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Wrench set
cocverting natural gas to propane gas
removed burner installed propane orfice and kit as per instruction sheet.
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- Customer:
- Shawn from Akron, OH
- Parts Used:
- 4392065
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Dyer drum doesnt turn
It was really quite esy remove the screws from the back and pop the top off . then remove 2 top inside screws from the front , lift the front off the sides , support the drum and lift out , you will then see the idler wheels, replace them with the new ones ,replce the tensioner , wrap the belt around the drum, need help putting the drum back in the case, have someone hold the drum in place while you lay on the ground and put the belt around the motor pulley and the tensioner on the bottom.you then put the front panel back into place and secure with the 2 inside screws, then put the rest back together in reverse oder. ... hope this helps someone
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- Customer:
- charles from parker, CO
- Parts Used:
- 279827
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers
had to replace the motor
Follow the advice given in the partsselect website. However, while removing the blower, my hand slipped into the housing and cut my thumb. Connected the wires to the junction box on the motor but didn't realize that the contacts would hit the drum when reinstalled. The original junction box was at a 90 degree rotation relative to the new box. When trying to test the breaker tripped. Using the multitester I found out that I burned out the thermal fuse, and froze the door switch. I replace both those parts and started the dryer and could hear a grinding sound. Inspection revealed that the housing of the motor was rubbing against the drum. Removing the drum yet again, I rotated the housing and replaced the drum. The dryer was finally working well.
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The dryer belt broke. During the effort to replace the belt it was noted that the lint trap housing seals were in need of replacement.
With the dryer taken apart to replace the broken belt it was obvious that the lint seals had not been working properly due to the excessive amount of lint covering all of the inside surfaces of the dryer. The belt idler pully had also moved from its normal mounting position and was laying at the bottom of the dryer. Because the lint had covered the bottom before the belt broke it was obvious to determine where the idler pully attached to the bottom.
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
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- Customer:
- Charles from Gray, TN
- Parts Used:
- 4392065
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
Drayer Was Making Squeaking Sound
Took off the top and front panel. Found that the belt tensioner was worn out. Decided to pull drum out,and replace the belt and drum rollers also. Put it back together, and it works fine.
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- Customer:
- Roger from Bonners Ferry, ID
- Parts Used:
- WP338906
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Screw drivers
Dryer would not heat up.
I unplugged the dryer,removed the two small screws on the front of the dryer and pulled the bottom forward. The two wires connected to the door do not have to be removed. With an electrical tester using the Ohm setting I tested the Radiant sensor and the Gas Valve coils. The two terminal coil was DOA. The dryer can be operated with the front open as long as the door wires are connected. Symptons: The igniter would heat up and not release gas. My repair was successfull due to this awesome website and the super fast shipping service. AAAA++++
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Dryer would not tumble.
I wasn't sure if the problem was the belt (probable) or the idler pulley assembly (less likely) but the total for both parts was about $26 plus shipping. So why not replace both to be sure?
As it turns out, my original idler pulley assembly does not turn. Rather, it has a concave semi-circular piece that is fixed in place. The belt ran in a groove in that piece.
The replacement part has a nylon wheel that turns. As a result of replacing the idler pulley assembly (which I don't think was necessary to fix my tumbling problem) the dryer runs much quieter. (We used to get a fair amount of squeaking when the belt rubbed).
As for the actual repair (I would rate myself as above average on tackling household repairs), it was about the simplest repair I've ever done. I followed the video provided on this site (excellent video) and it took less than 20 minutes -- cleaning up all of the lint/odds and ends under the washer and dryer took longer than the actual repair.
My only issue (minor) was disconnecting the electric harness. It did not slide as easily as in the video. I had to coax mine a bit with a small screwdriver (make sure your dryer is unplugged!!). I suspect it was simply a function of the harness never being unplugged -- the dryer is 9 years old.
I also felt great because I'm sure I saved a $125 service call (for only $26 in parts and 20 minutes of my life).
Good luck!
As it turns out, my original idler pulley assembly does not turn. Rather, it has a concave semi-circular piece that is fixed in place. The belt ran in a groove in that piece.
The replacement part has a nylon wheel that turns. As a result of replacing the idler pulley assembly (which I don't think was necessary to fix my tumbling problem) the dryer runs much quieter. (We used to get a fair amount of squeaking when the belt rubbed).
As for the actual repair (I would rate myself as above average on tackling household repairs), it was about the simplest repair I've ever done. I followed the video provided on this site (excellent video) and it took less than 20 minutes -- cleaning up all of the lint/odds and ends under the washer and dryer took longer than the actual repair.
My only issue (minor) was disconnecting the electric harness. It did not slide as easily as in the video. I had to coax mine a bit with a small screwdriver (make sure your dryer is unplugged!!). I suspect it was simply a function of the harness never being unplugged -- the dryer is 9 years old.
I also felt great because I'm sure I saved a $125 service call (for only $26 in parts and 20 minutes of my life).
Good luck!
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- Customer:
- Leonard from Lemitar, NM
- Parts Used:
- 49572A
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Socket set
Convert gas dryer to Propane
Received conversion kit. Removed front dryer panel,2 screws. Removed burner tube, 2 screws then removed natural gas orfice.
Installed propane orfice and repalced burner tube.
Removed regulater plug and replaced with new plug from kit using 90 degree ratchet screw driver. Approximately 20 minutes. Dryer working great.
Installed propane orfice and repalced burner tube.
Removed regulater plug and replaced with new plug from kit using 90 degree ratchet screw driver. Approximately 20 minutes. Dryer working great.
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