3LGR5436EQ0 Whirlpool Dryer - Instructions
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flame fadedout after unit got hot; problem turned out to be the solenoid coils
removed frt & rear panels & drum and lint chute for seal replacement replaced these components, problem didn't go away, ordered & replaced both gas valve coils (m series coil kit) problem solved
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- Customer:
- Douglas from Fernley, NV
- Parts Used:
- WP338906
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Socket set
Dryer got hot then heat would shut off
Sensor is in the front lower left. Gas off, electicity off. Removed two screws for the filter, pry/lifted the top up and taped it too the overhead cabinet, removed two screws inside top of front panel, lifted pandel with door closed staight off. Two screws to remove the flame sensor braket. unplug the old sensor install the new one and reverse everything. With others suggestions I purchased temperature switches etc. but the radiant flame sensor was the problem. I now have some spare switches for future. Excellent company and very quick service. Oh, Sears wanted 200.00 just for the service call, I live rural.
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- Customer:
- David from Fort Myers, FL
- Parts Used:
- WP3406105
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers
Dryer on/off door switch broke and needed replaced.
Took the dryer top off and removed the bad part. Looked it up online and found a replacement by looking for whirlpool parts. They didn't have one at the local parts stores so I ordered the part online and had it mailed within three days. I replaced it quite easily. It worked and I put everything back together and my wife took over the tricky part of drying the laundry! The repair was quite easy for a non mechanical person like me.
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Dryer was screeching and squealing when running
I removed the top panel, then the front panel.
Removed the belt and the drum.
Saw what I needed to replace. Ordered the parts then put back together. It was a really easy job.
Removed the belt and the drum.
Saw what I needed to replace. Ordered the parts then put back together. It was a really easy job.
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- Customer:
- MONTE from CHESAPEAKE, VA
- Parts Used:
- WP18776
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Dryer Top Panel is Loose
1) Unplug power cable from dryer.
2) Remove the 2 screws that secure the chute for lint filter screen with
Phillips head screwdriver.
3) Remove the lint filter screen.
4) Depress plastic locking clip on each side with putty knife to release
tension and lift up top panel to clear the locking clips. Each locking
clip is located 2-1/2 inches from the front edge of side panel.
5) Lift the top panel and lean against the wall for support. If dryer top
panel cannot be raised all the way due to cabinet(s) above, tape
the dryer top panel to cabinet above or have somebody hold the
top panel for temporary support.
6) Install the new metal locking clips. Ensure that the elongated tab
of the metal locking clip is towards the front of dryer. Compress
locking clip lightly with pliers and push down into the hole.
7) Lower the dryer top panel and press it down in place over the metal
locking clips for a tight fit.
8) Reinstall the 2 screws to secure the lint filter chute.
9) Reinstall lint filter screen.
10) Reconnect power cable for dryer.
11) Turn on dryer and inspect that all dryer panels (top, sides and
front) are tight and secured.
Repair Duration: 5 minutes
2) Remove the 2 screws that secure the chute for lint filter screen with
Phillips head screwdriver.
3) Remove the lint filter screen.
4) Depress plastic locking clip on each side with putty knife to release
tension and lift up top panel to clear the locking clips. Each locking
clip is located 2-1/2 inches from the front edge of side panel.
5) Lift the top panel and lean against the wall for support. If dryer top
panel cannot be raised all the way due to cabinet(s) above, tape
the dryer top panel to cabinet above or have somebody hold the
top panel for temporary support.
6) Install the new metal locking clips. Ensure that the elongated tab
of the metal locking clip is towards the front of dryer. Compress
locking clip lightly with pliers and push down into the hole.
7) Lower the dryer top panel and press it down in place over the metal
locking clips for a tight fit.
8) Reinstall the 2 screws to secure the lint filter chute.
9) Reinstall lint filter screen.
10) Reconnect power cable for dryer.
11) Turn on dryer and inspect that all dryer panels (top, sides and
front) are tight and secured.
Repair Duration: 5 minutes
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Dryer stopping during dry cycle.
First I pulled the dryer away from the wall and unplugged it. Next I removed the dryer vent hose and threw it away and replaced it with a more rigid metal vent hose. Next, I used a socket wrench to removed the screws holding on the back cover of the dryer. Once the back cover was off it was just a matter of using the socket wrench to removed the bolt holding the sensor in place. After the part was removed I made sure the replacement was orientated in the same way as the original part and then I unplugged the wires from the bad sensor and placed them in the same order on the new part and then I bolted the new sensor back in place. Since the new part has been installed the dryer is working flawlessly and is not turning off mid-cycle like it was. ***Oh, and an important reminder. When you have the back cover pulled off the dryer use a shop vacuum to suck out any dirt and lint in the back of the dryer and make sure you unbolt the metal chute that the dryer lint screen goes into and clean inside the area near the exhaust blower. This is a VERY IMPORTANT part of servicing your dryer and should be done every few months to help avoid the risk of a fire.****
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Dryer had no heat at all. This is an older gas dryer.
Cleaned out years of fuzz behind lower access panel and noticed where the igniter sits there is a metal tube about 1 inch in diameter. It had rust on the end and was starting to flake away. Found some helpful hints about how to test the igniter. Very easy, just used an ohmeter. Unplugged the 2 pin wire connector and checked for continuity. 1 lead on 1 pin and the other on the other pin., igniter side not the harness side from the dryer. A good igniter should read less than 5 ohms. I don't know the spec. exacttly, but it should not read open or infinite resistance. My meter read an open circuit. Removed the tube and igniter assembly, mine only 2 small bolts. I found the igniter element cracked. Ordered and installed igniter and tube assembly. This was a very easy install. 20 year old dryer works great and it's better than spending $500.00+ on a new one.
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- Customer:
- Michael from CLIFTON HTS, PA
- Parts Used:
- WP694089
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
Motor was bad
I have not received the parts yet waiting on the motor, can’t put the blower fan in without the motor, ordered it , Jan 23rd, still no motor, have to go to laundry mat, have you ever had to do that with 7kids, and you and your wife’s laundry, probably not, because you would have had your motor by now. Maybe you can help me with the part so I can redo a testimonial here for you. 19 days and still waiting
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- Customer:
- anthony from Port Arthur, TX
- Parts Used:
- 279311
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
No heat, would not light because igniter burnt out
Unplug dryer. Remove the front bottom panel of dryer 2 screws, then unplug wire connector to the old igniter then unscrew one screw holding ignitor then wiggle out. Open new igniter wiggle back in place insert screw tighten, (getting this screw back in is a little hard) replug wire connector to new igniter replace front panel with two screws. Plug in dryer and there you go drying clothes again. Wife all happy again.
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Poor drying and took excessive amount of time to complete partially dried loads
Took back cover off. Cleaned out the lint that had built up inside the dryer. Replaced the lint trap housing and lint chute seals. Also replaced the drying vent hose. Works great now.
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Loud squeeking.
I ordered the belt idler pully and drum support rollers and after watching the video on Parts Select web page, changed the parts. It could be done by one person, however having a second person to help with the drum installation worked great. I discovered the motor bearing on the front side of the motor was the source of the squeek. I disassembled the dryer again and removed the motor. After ordering a motor the installation and reassembly went smoothly. The parts came in two days of placing the orders and virtually new parts in the dryer makes it seem like a new machine.
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Making loud squealing noises
Removed the Lint filter, then lifted top panel and rested the panel against the wall.
Disconnected connector attached to the door panel.
removed screws, from both side of door panel and lifted door panel up and out.
Moved Idler pulley to the right taking tension off the drum belt, lift the drum out with the drum belt.
removed old drum felt seal and removed old residual glue, reglued and installed new Rear Drum Felt Seal.
Installed new Idler pulley Assembly and reassembled in reverse order.
Disconnected connector attached to the door panel.
removed screws, from both side of door panel and lifted door panel up and out.
Moved Idler pulley to the right taking tension off the drum belt, lift the drum out with the drum belt.
removed old drum felt seal and removed old residual glue, reglued and installed new Rear Drum Felt Seal.
Installed new Idler pulley Assembly and reassembled in reverse order.
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- Customer:
- Steven from Oxnard, CA
- Parts Used:
- WPW10512946, 349241T, WPW10359270, WPW10359269
- Difficulty Level:
- Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable)
The dryer was squeaking and would not heat at all.
The first thing I did was call my friend Donnie who manages some apartment buildings and who is always complaining about fixing things and getting the right parts to fix things. He told me what to order from PartsSelect and when the parts got here I called him up and he did the repair work.
He was reluctant to do the work at first but after he found out I had ordered the parts from PartsSelect he was happy to do the work. "Their parts are always right and they always work," was what he said after he had my dryer working just like new. So if you know nothing about fixing things and buying parts just call PartsSelect and you will be fine. Just ask my friend Donnie!!!
He was reluctant to do the work at first but after he found out I had ordered the parts from PartsSelect he was happy to do the work. "Their parts are always right and they always work," was what he said after he had my dryer working just like new. So if you know nothing about fixing things and buying parts just call PartsSelect and you will be fine. Just ask my friend Donnie!!!
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Front seal was ripped.
Step one: UNPLUG THE 220V LINE!
Removed the 2 screws on top under the lint door then flipped up the top. Next I unclipped the wire harness at the front and disconnected the 2 wires to the door switch and flipped the harness out of the way. Then I popped off the kick panel. Next, I removed the (4) 9mm screws holding the front panel on. The 2 lower screws only need to be loosened and the panel lifted off. Note the location of the door springs at the bottom. These springs can be reinstalled easily through the kick panel after you reinstall the front panel.
Next I removed the remnants of the old seal from the front panel but left the 3 plastic clips in place. The seal wraps around the perimeter of the panel and is held in place by the lip of the opening. The extra flap is then folded back so that the folded edge is toward the dryer drum and away from the front of the panel. The sketch in the instructions is not helpful!
Next, reinstall the front panel. As you set it onto the lower screws, you may need to lift the drum slightly to fit the panel into the drum opening. Tighten the 4 screws then reattach the 2 door springs. Test the operation by turning the drum counterclockwise by hand. Check to make sure the rear seal has not been displaced or damaged. That seal is actually glued into place. If it turns smoothly, snap the kick panel back on and reinstall the wire harness. Flip down the top and reinstall the 2 screws at the lint tray on top. Plug it in and give it a spin!.
Note, While you have it open, you'll want to use your shop vac and clean all the lint and pocket change out of the machine. You might as well take off the back panel and clean up in there and in the vent pipe too.
I didn't know if I needed a new belt but ordered one anyway. The old one turned out to be pretty well shot. After I had the front panel removed, replacing the belt is very simple. There is an idler pulley underneath that is under tension. Just push on the idler until the belt is loose. Switch the new one into place and you are done.
Removed the 2 screws on top under the lint door then flipped up the top. Next I unclipped the wire harness at the front and disconnected the 2 wires to the door switch and flipped the harness out of the way. Then I popped off the kick panel. Next, I removed the (4) 9mm screws holding the front panel on. The 2 lower screws only need to be loosened and the panel lifted off. Note the location of the door springs at the bottom. These springs can be reinstalled easily through the kick panel after you reinstall the front panel.
Next I removed the remnants of the old seal from the front panel but left the 3 plastic clips in place. The seal wraps around the perimeter of the panel and is held in place by the lip of the opening. The extra flap is then folded back so that the folded edge is toward the dryer drum and away from the front of the panel. The sketch in the instructions is not helpful!
Next, reinstall the front panel. As you set it onto the lower screws, you may need to lift the drum slightly to fit the panel into the drum opening. Tighten the 4 screws then reattach the 2 door springs. Test the operation by turning the drum counterclockwise by hand. Check to make sure the rear seal has not been displaced or damaged. That seal is actually glued into place. If it turns smoothly, snap the kick panel back on and reinstall the wire harness. Flip down the top and reinstall the 2 screws at the lint tray on top. Plug it in and give it a spin!.
Note, While you have it open, you'll want to use your shop vac and clean all the lint and pocket change out of the machine. You might as well take off the back panel and clean up in there and in the vent pipe too.
I didn't know if I needed a new belt but ordered one anyway. The old one turned out to be pretty well shot. After I had the front panel removed, replacing the belt is very simple. There is an idler pulley underneath that is under tension. Just push on the idler until the belt is loose. Switch the new one into place and you are done.
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- Customer:
- Gay from Apple Valley, CA
- Parts Used:
- W10820036
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Drum would not spin to drain water
Removed two screws and lifted the control console then tilted forward the shell. Removed two screws holding the latch cover and assembly then disconnected two wires. I played with the assembly until I discoved the element was toast. Ordered the part but when I got it I was confused because it had three prongs (two on one side and one on the other) when the burnt one had only one and one and I only had 2 disconnect wires. I thought I had gotten the wrong part but figured it out. Actually putting the assembly together was the easy part, trying to get the outer shell back together was a little tough. Between taking it a part, figuring out what was wrong and ordering and receiving the part was about three weeks. So when putting it all together took awhile but I did it and it works great.
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