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MEDB855DC2 Maytag Dryer - Instructions

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All Instructions for the MEDB855DC2
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Customer:
GREGORY from Wilsonville, OR
Parts Used:
279640
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers, Screw drivers
Very Loud Squeaking Noise
1) Disconnected power cord from wall. 2) Disconnected vent hose from back of dryer. 3)Removed dryer rear panel. 4)Disengaged tension spring on idle wheel arm. 5) Removed worn idle wheel. 6)Installed new Idler wheel assembly. 7) Vacuumed dust from rear of dryer (optional, recommended). 8) Reinstalled rear cover, vent hose and power cord. Easy repair 15-30
60 of 71 people found this instruction helpful.
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Customer:
Michelle from Richardson, TX
Parts Used:
72017
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Scratches in Surface
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.
64 of 125 people found this instruction helpful.
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Customer:
John from Tucson, AZ
Parts Used:
WPW10314173, WPW10359272, W11236646, WPW10512946
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Nutdriver, Screw drivers, Wrench (Adjustable)
worn out part
The repair was fairly easy. The most timely part of the repair was removing the twelve screws from the back panel to expose the repair.
41 of 60 people found this instruction helpful.
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Customer:
Robert from Princeton, WV
Parts Used:
279640
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Nutdriver, Screw drivers
TOb stopped turning after a week or so of high pitched "squeals" coming from inside the dryer.
I recommend you order the idler pulley as soon as you start to hear the unusual noise indicating metal against metal. Replace the idler pulley before it fails and possibly causes more damage to the drive system. Simply removed the power cord at the back of the dryer and then the multiple screws holding the back panel in place as well as the clip holding the exhaust vent in place. You may need to remove the top panel to access a few of these screws. A diagram of the belt routing is in the paperwork I found behind the front lower panel of the dryer. This too is easily removed with just a few screws.
29 of 33 people found this instruction helpful.
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Customer:
Jim from Tucson, AZ
Parts Used:
WP8577274
Difficulty Level:
A Bit Difficult
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Screw drivers, Socket set
Unit would shut down in the middle of cycle and flash E1 trouble code
Had to remove the back of unit to access the area of subject part by removeing 12 to 14 screws also the gas line had to be removed. Two screws held the part in place. Unit now runs normal.Saved alot on repair costs!!!!!
30 of 40 people found this instruction helpful.
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Customer:
joe from cheswick, PA
Parts Used:
WP697772
Difficulty Level:
A Bit Difficult
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
craked blower motor
somthing fell down in the blower motor compartment and busted up the bloewr motor fan,and was making noise and out of balance.i changed the blower motor and runs like a charme
63 of 142 people found this instruction helpful.
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Customer:
Keith from Richmond, VA
Parts Used:
279640
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Socket set
Idler Pulley broke
I disconnect the power, then the vent pipe. I removed the back panel of the dryer to access the pulley and removed the belt. Replaced the back and put everything back together.
21 of 26 people found this instruction helpful.
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Customer:
Dixon from Santa Fe, NM
Parts Used:
WP8577274
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver
Dryer turns off after 1-2 minutes
I tried to follow directions followed by others on this site after diagnosing the problem via suggestions provided by users. I have a Whirlpool Duet dryer from 2002. We've had problems since moving about 3 years ago. I removed the front panel (lower) by unscrewing the two bottom screws (1/4" sheet metal screws). Then I took out the lint screen and the metal tube/contraption immediately beneath to get access to the area where thermistor is located. See the drawing/chart to help you locate this. It's really easier than it seems. Make sure you have the chart/drawing for your model - it makes difference! The thermistor came out pretty easily with a nutdriver that has a swivel offset shaft. Ask your hardware store tool dept. about that one. Put everything back in reverse order of course and test either with/without the front panel re-attached. In my case it fixed at least part of the problem. I was able to get clothes almost dry with most settings but I have yet to install the moisture sensor to see if that helps in addition to the internal-bias thermistor. I am the kind of person that does one thing at a time so at least I now know the thermistor was bad. Good luck and hang in there with your own repair. It's a lot cheaper even if it takes you longer to do than a pro.
19 of 21 people found this instruction helpful.
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Customer:
Jeff from Mesa, AZ
Parts Used:
WPW10314173
Difficulty Level:
A Bit Difficult
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers, Wrench (Adjustable), Wrench set
noisy drum
the job would have gone faster if the right parts had been sent in the first place. I would have never paid for two day shipping. In the repair, I removed the rear panel, clipped the plastic triangle holding the bearing, installed the new bearing and new clip.
20 of 26 people found this instruction helpful.
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Customer:
Jerry Duty from Fort Walton Beach, FL
Parts Used:
279640
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
idler pully sqwieling
once the back is off remove belt from tentioner and remove v clip. smooth shaft with wd-40 and scotch brite , then install new idler replace v clip
and your done !!!
19 of 24 people found this instruction helpful.
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Customer:
Victor from HOUSTON, TX
Parts Used:
W10837240, 279640
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Screw drivers
Dryer starts with loud squeak initially. Eventually there was a loud clank and dryer stopped.
Rather than remove the front panels, door, control panel and drum, I noticed 1/4" metal screws on the back panel. There were approximately 6 holding the back panel in place. I did have to remove the top panel as well before removing the back. Once removed I had complete access to the broken idler pulley assembly. I immediately saw the broken pulley. I installed the new one with very little effort. Reset the belt according to instructions from the video. Reassembled, plugged in, hit start and enjoyed the sweet sounds of success. All told it took me about 20 minutes from start to finish.
15 of 16 people found this instruction helpful.
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Customer:
Kim K from Hurst, TX
Parts Used:
279640
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Wrench (Adjustable)
Dryer would not turn
My dryer starter squeaking in December 09 and the repairman told me that it would cost between $200-$500. I did not let him fix it as this machine is only 3 years old. When the part finally broke in April 10, I was ready to junk this and just buy a used dryer. My husband went on line and quickly figured out the part he would need to do the repairs. It cost under $20.00. Now my dryer is fixed and running and there are no squeaks. Thank you
15 of 18 people found this instruction helpful.
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Customer:
John from Cedar Rapids, IA
Parts Used:
279973
Difficulty Level:
A Bit Difficult
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Pliers, Screw drivers
Flashing E1 code for a bad thermistor
I replaced the thermistor earlier, but the code was still flashing. I noticed the heater terminals were charred and pretty well covered in carbon. So, I replaced the heater, the thermostat and thermal fuse and replaced the 3/8" spade terminals on the heater wires. (These are hard to find - most electrical spades terminals are .250. Also, I crimped and soldered these for a connection with the lowest resistance possible). After all that, the code still flashed! I let the explatives fly, calmed down, and ran the control board test. (This is done by pressing "more time" "less time" "more time" "less time" in succession.) The control board was passing all the tests, but the thermistor test, and the only thing is in this circuit is the thermistor, the wires, the connector to the control board, and some circuit on the control board that involves a few resistors and the "brain" chip. So, I checked the terminals at the thermistor, the wires up to the control board and the connector at the board. The control board connector was fairly dust encrusted, so I unplugged it, cleaned the control board terminals and sucked away all the lint and dust. Finally, I carefully removed earch crimp terminal from the Molex connector (the white female connector) and cleaned and bent them to yield a better connection to the terminals on the control board. I put it all back together, and thus far it is working fine.
17 of 25 people found this instruction helpful.
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Customer:
Joyce from Holbrook, NY
Parts Used:
WP8577274
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers
When using the dryer the cycle would stop and display E1 as the reason
Unscrewed the bottom panelof the dryer and located the thermistor through the schematic for my machine. Removed the old one and put the new one in the same way. No more E1 problems and all cycles now complete themselves.
12 of 17 people found this instruction helpful.
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Customer:
Michael from ENOLA, PA
Parts Used:
W10837240, 279640
Difficulty Level:
Very Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Socket set
Dryer squeeching very loud
Took off back of dryer Undid belt from belt adjuster pulled and took off adjuster put new one on redid belt and put back on dryer. Done
9 of 9 people found this instruction helpful.
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All Instructions for the MEDB855DC2
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