Models > MLG19PDDGW > Instructions

MLG19PDDGW Maytag Dryer - Instructions

Jump to:

All Instructions for the MLG19PDDGW
61 - 75 of 873
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
Customer:
Thomas from Olathe, KS
Parts Used:
12002022
Difficulty Level:
Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
Failed bearings cause by a failed lip seal
First of all, let me say that the Lip Seal Kit was delivered the next day after my order and that I was encourged to attempt the repair by the owners repair procedure response. The lip seal in my machine must have failed along time ago as I have been living with noisy bearings for at least the last twelve months. Disassembly of the machine was straight forward following the Part Select instructions. The lip seal was so disintegrated it hard to tell what originally looked like. Lots of rust and gunk in lip seal area. After removing the snap ring behind the rear bearing I was able to drive out the rear bearing using a brass 3/4" drift pin and a two# hammer. I than attemped to remove the front bearing using a 1 1/2" steel pipe that matched up to the inner race of the front bearing and my trusty hammer. Nothing I did could budge that bearing. Since the outer tube is suspended by springs and struts I decided that lot of hammer energy is absored by springs and my best solution was to remove the outer tub. I then used a couple pieces of U channel steel(this could be steel pipe or some 2X4's) that were longer than the depth of the tub and positioned them to contact metal bearing tub insert. These supports were mounted in small Workmate vise setting on the garage floor and using the 1 1/2" steel pipe I drove the inside bearing out. After some general clean up I picked up some bearings at the local distributor for $42.00. Re-assembly takes a little planning as you need to hold the steel insert betwwen the bearings and keep it lined up in the bore. I think the best way is to install the rear bearing first and install the snap ring. I then put the steel ring in place and held it with cardboard insert from a paper towel roll. The cardboard roll was cut about 2 1/2" long and cut lenght wise to insert though the rear bearing and held in place with tape. The front bearing was then tapped into place followed by the lip seal. Note that if you install the front bearing first and seat it all the way in, the rear bearing will contact the steel insert and not allow enough room to get the snap ring in place. When I was done I didn't have any parts leftover and thru six washing machine loads peace and quiet has returned to my house. Hope it last. Note: If you elect to remove the outer tub you might want to take some pictures so you can see how it all is supposed to look before you close the hood.
12 of 15 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Robert from Milford, OH
Parts Used:
WP33002032, WP33001755
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Screw drivers
One of the Baffles came loose.
I took out screws holding top to dryer & raised the top & proped it up to gain access to inside of the dryeeer drum. I then inatalled the new baffle & secured it with 2 screws. It would have been better if the part came with new screws.It was hard to determine which was the right screws for this application.
12 of 16 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Douglas from Marion, IN
Parts Used:
12001788
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Drive belt sqeaked and contiued to roll off the drum.
Removed washer back panel (after unplugging unit). Installed new belt. Reinstalled back panel. Belt wAs very tight getting it to roll onto the drum.
13 of 19 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Scott from Palm Bay, FL
Parts Used:
306436
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Dryer door latch broken, using duct tape every time to dry clothes.
Piece of cake. Used flat screwdriver to pry out female part on cabinet side, same with the male part on door. Every new replacement part was tight and operated like new. Thanks Part Select, you'll be forever on my list of online parts buying.
10 of 11 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Jim from Foothill Ranch, CA
Parts Used:
279834
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers
Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
10 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Roger from Westminster, SC
Parts Used:
279834, 279834
Difficulty Level:
Very Difficult
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Screw drivers
Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.

The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.

I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
12 of 18 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
tommy from madisonville, KY
Parts Used:
12002022
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers, Socket set
High Pitch Noise During Spin Cycle The Seal Failed Causing The Bearing To Fail Also
First I removed front and rear covers and the dispenser screws. If you are carefull you can fold the front cover back and lay it on top of the washer so that you do not have to unplug all the wires. Remove the clips on the front of the outer drum with a small flat blade screwdriver and set aside. Go to the back and roll the belt off the pulley. Remove bolt and snap ring and the pulley should pull toward you off of the shaft. This is plastic be carefull. The inner drum will now pull out thru the front of the machine. Now read the directions again and again about the seal because you have to replace exactly what you take out. This is my only complaint with the directions there needs to be a picture and not an illustration of the placement of the sael and the spacer in my case.
9 of 10 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Carl from Livermore, CA
Parts Used:
WP33001761
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Broken door strike
Removed one screw and took out old broken door strike, replaced with new door strke and put screw back in. Only took two three days to get the part. The dryer is as good as new!
10 of 13 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Wade from Lovell, WY
Parts Used:
WP33001755
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Socket set
Short Baffle in dryer drum was broke off
This was fairly easy, I have had the dryer front off before. Unplug dryer from electrical outlet. Pull dryer away from wall. Remove the dryer door, open dryer door there are 2 phillips screws on dryer door hing, remove these crews then lift gently and remove door, across from these screws, where dryer door closes into face cover of dryer remove 2 more phillips screws. From top of face cover, pull out front of face cover and lift to remove face cover of dryer. On each side of dryer on the front, after removing the front cover is a 5/16 bolt, remove these and pull off retaining bracket with a twisting motion. You now can lift the top of the dryer up. You can now see the barrel drum. Rotate barrel by hand so the broken baffle is on top. Remove two 5/16 bolts, and replace new baffle in place. Reassemble in reverse order of disassemble.
8 of 8 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Noah from Maiden, NC
Parts Used:
WP694674
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Wrench (Adjustable)
No heat in dryer
Took off the lower front panel, removed duct piece from filter to blower fan, removed two screws and two wires to thermostat in exhaust ducting, then replaced thermostat with new one. Very easy job and everything worked like new when I reassembled it.
10 of 14 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
TJ from WARWICK, NY
Parts Used:
WP22004477, WP22003074
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Screw drivers, Socket set
mold on door boot, replace door boot
followed the approach on fixya.com. when installing new boot and cable loop, found it easier to remove drum cover from machine (held on with simple clips). Then you can install boot onto the cover and the door frame. Putting everything back in machine and re-attaching the various braces took only a couple of minutes.
8 of 9 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
john from st helen, MI
Parts Used:
22004465
Difficulty Level:
Really Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers, Socket set
water leaking on the floor.
I opened the door on the washer,and pushed on inner tub upward.it moved about 1 inch and the I knew tub bearings where shot .So I removed all components and repaced the outer tub with new bearing pack.. NOTE... Not an easy repair..but when i finished i had no probems with water leakage.ALL GOOD.
8 of 9 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
John from Palmdale, CA
Parts Used:
WP33002535, WP6-3705180, WP6-3700340
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Screw drivers, Socket set
Squeaking sound then Barrel stoped turning
Unplugged the unit
Removed door and two clips that hold front panel on (6 Philip crews)
Then removed front panel by hand hold each side of the panel at the top
Of the “U” shape and pulling out ward until it frees it self from the two
Bottom clips.
You can now see a belt that is no longer tight around the drum
When I tried to put the belt back on I noticed the idler pulley was flopping around and I would need to replace it .That where you guys saved me.
Your exploded model and parts list made it easy to see exactly what parts I
Needed to order.
The rest gets a little tricky there is another plate that supports the barrel
A couple of clips that hold the top cover in place all of this must be removed
Note the top cover only need to be lifted up an inch or two at the front where the
Two steel clips where and doses not need to be removed to get this panel off that
Supports the barrel.
There are some wires attached to it also I only had to unplug the three that go to
The door safety switch then I was able to rotate it off to the side out of the way
And now the barrel can be lifted out. You can now remove the idler pulley assembly
I used pliers to remove the spring and a crocket wrench to remove a bolt that holds
The bracket that also should be replaced due to ware at the idler pulley barring pin
The tricky part is putting it all back together again. To explain this I would need to Wright a book. It takes a lot of good common sense. I was proud of how I reached
Around from each side of the motor and by feel alone and get the belt around
The motor pulley and the idler pulley that keeps the belt tight around the barrel
Makes me think I should have been a repairman.
8 of 9 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
NICHOLAS from PARMA, OH
Parts Used:
WP338906
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers, Wrench set
No Heat
I suspected a faulty igniter and disconnected the cable to the igniter and measured the resistance of the igniter and found it to be 70 ohms then I checked the voltage at the same cable towards the power source and found it to be 25 volts ac which should be 120 volts ac. Next I checked the radiant flame sensor and found it to be open (it should be a closed circuit when cold). I removed the flame sensor (with the power off) using a small box wrench and found a broken lead. Replacing the flame sensor solved the problem.
9 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Customer:
Philip from La Palma, CA
Parts Used:
WP338906
Difficulty Level:
Really Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers, Wrench set
No heat
Took everything apart, replaced the igniter flint, and still didn't get heat. Then found out the thermal sensor wasn't running a electrical current through it with voltmeter and just replaced that, now it we have heat again!
9 of 13 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
All Instructions for the MLG19PDDGW
61 - 75 of 873