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YMEDZ600TB2 Maytag Dryer - Instructions

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All Instructions for the YMEDZ600TB2
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Customer:
mike from jensen beach, FL
Parts Used:
WP3391914, WP3387747
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Screw drivers, Socket set
dryer will not dry the cloths
1st. i removed the two screws that holds the cover.
2nd. -vacumn (most time used)around to find the screws that hold the metal heat tube and shield.
3 rd. removing the screws tip the front of the tube up and pull out from the back.my element was clipped in place. I then pulled the element out and replaced the thermostat (tip: replace all t'stats around the heat element). it is as simple as reading the repair stories
23 of 27 people found this instruction helpful.
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Customer:
Mark from San Diego, CA
Parts Used:
W10470674
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Screw drivers, Wrench (Adjustable)
Needed to change rear exhaust to the side to fit dryer into my closet.
First, I opened up the front of the dryer and then unscrewed the entire back piece. I assembled the new exhaust piece from the kit. Next, I took out the old straight rear exhaust and then replaced it with the elbow shaped left eshaust from the kit. Lastly, reattache the back and front pieces of the dryer.
44 of 91 people found this instruction helpful.
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Customer:
John from Madison, WI
Parts Used:
W10120998
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Poorly designed lint filter/ gasket falls off
Replaced
25 of 34 people found this instruction helpful.
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Customer:
Paul from Bradford, MA
Parts Used:
WP3387747
Difficulty Level:
Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Pliers
Dryer runs with no heat
It was easier to remove the blower manifold cover, (3 screws) to get at the heater element. Remove the heat shield, disconnect the two wires from the element. There is another screw on the side holding the element in the housing. Remove it and slide the element torward you. I used pliers as it was a snug fit. Replace. Good time to vacuum the whole area.
23 of 29 people found this instruction helpful.
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Customer:
JEFF from LEBANON, TN
Parts Used:
WP3387747, 279973
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Socket set
dryer wouldnt heat
First i tested each part for continuity and found out that the thermal fuse was bad. So ordered the part and went ahead and got thermostat and element to ensure no problems in the future since I already was in there.
24 of 35 people found this instruction helpful.
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Customer:
Keith from Richmond, VA
Parts Used:
279640
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Socket set
Idler Pulley broke
I disconnect the power, then the vent pipe. I removed the back panel of the dryer to access the pulley and removed the belt. Replaced the back and put everything back together.
21 of 26 people found this instruction helpful.
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Customer:
john from OLYMPIA, WA
Parts Used:
4392067
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Screw drivers
Noisy sound from dryer
Just like video except there were two screws in back to take control head off. Be prepared to have shop vacation ready. Clean dryer duct too. Have bandaids ready. Plastic triangles are not easy to take off, video makes it look easy.
20 of 23 people found this instruction helpful.
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Customer:
sandra*broadnax from BRISTOW, VA
Parts Used:
W11086603, WP3387223
Difficulty Level:
Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
The sensor would not slide into grill
Initially, i watched the how to do it instruction in the fix website to determine the complexity of repairs. The instruction built up my confidence. I ordered and recieved the grill amd the two new sensors. I placed the two new sensors into the new grill sensor slots. Then removed the old grill by unscrewing three screws. Connected the two sensors positioned the grill and screwed in the three screws put the lent stray in the grill and closed the dyer door. I have been a happy camper ever since. I saved the $75 home insurance fee plus maintenence installment. Thanks
18 of 18 people found this instruction helpful.
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Customer:
Jack from JONESBORO, AR
Parts Used:
WP3387223
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Pliers, Screw drivers
Moisture sensors need replacement
Inside the dryer tub, remove the filter housing by removing two phillips head screws. Unplug the sensor wires, note when replacing wires, black wire goes on upper sensor.
Separate filter grill from housing. Using the pliers, compress the tabs on the sensor plugs and push it thru the grill. The small blade screwdriver may come in handy here to pry up on sensor to assist in pulling the plug end through the grill. Replace the sensors by hooking short end into grill and pushing the long end through the grill. When replacing the housing to the dryer, the most difficult thing is getting the screwdriver onto the recessed screws. Be sure to put the tab on top of the housing under the dryer frame when rotating the assembly into place.
20 of 24 people found this instruction helpful.
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Customer:
Michelle from Richardson, TX
Parts Used:
72017
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Scratches in Surface
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.
80 of 206 people found this instruction helpful.
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Customer:
Jerry Duty from Fort Walton Beach, FL
Parts Used:
279640
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
idler pully sqwieling
once the back is off remove belt from tentioner and remove v clip. smooth shaft with wd-40 and scotch brite , then install new idler replace v clip
and your done !!!
19 of 24 people found this instruction helpful.
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Customer:
Rebecca from Laredo, TX
Parts Used:
W10120998
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
The felt strip on the filter had come undone.
Took the old filter out and inserted the new one- works great!!
21 of 31 people found this instruction helpful.
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Customer:
Victor from HOUSTON, TX
Parts Used:
W10837240, 279640
Difficulty Level:
Really Easy
Total Repair Time:
15 - 30 mins
Tools:
Nutdriver, Screw drivers
Dryer starts with loud squeak initially. Eventually there was a loud clank and dryer stopped.
Rather than remove the front panels, door, control panel and drum, I noticed 1/4" metal screws on the back panel. There were approximately 6 holding the back panel in place. I did have to remove the top panel as well before removing the back. Once removed I had complete access to the broken idler pulley assembly. I immediately saw the broken pulley. I installed the new one with very little effort. Reset the belt according to instructions from the video. Reassembled, plugged in, hit start and enjoyed the sweet sounds of success. All told it took me about 20 minutes from start to finish.
16 of 17 people found this instruction helpful.
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Customer:
rodney from Mad River, CA
Parts Used:
WPW10512946, WPW10359272, WPW10359271, WPW10314173
Difficulty Level:
Very Difficult
Total Repair Time:
More than 2 hours
parts took more than two months to get here.
I'm still waiting on my idler pulley. It arrived at Fed EX depot in Tracy CA on December 14th and has still not been shipped. So it is pretty fucking hard for me to install it! Maybe if you had customer service that would answer their phones or reply to my Emails would be helpful
16 of 18 people found this instruction helpful.
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Customer:
John from Cedar Rapids, IA
Parts Used:
279973
Difficulty Level:
A Bit Difficult
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Pliers, Screw drivers
Flashing E1 code for a bad thermistor
I replaced the thermistor earlier, but the code was still flashing. I noticed the heater terminals were charred and pretty well covered in carbon. So, I replaced the heater, the thermostat and thermal fuse and replaced the 3/8" spade terminals on the heater wires. (These are hard to find - most electrical spades terminals are .250. Also, I crimped and soldered these for a connection with the lowest resistance possible). After all that, the code still flashed! I let the explatives fly, calmed down, and ran the control board test. (This is done by pressing "more time" "less time" "more time" "less time" in succession.) The control board was passing all the tests, but the thermistor test, and the only thing is in this circuit is the thermistor, the wires, the connector to the control board, and some circuit on the control board that involves a few resistors and the "brain" chip. So, I checked the terminals at the thermistor, the wires up to the control board and the connector at the board. The control board connector was fairly dust encrusted, so I unplugged it, cleaned the control board terminals and sucked away all the lint and dust. Finally, I carefully removed earch crimp terminal from the Molex connector (the white female connector) and cleaned and bent them to yield a better connection to the terminals on the control board. I put it all back together, and thus far it is working fine.
19 of 28 people found this instruction helpful.
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All Instructions for the YMEDZ600TB2
31 - 45 of 499