1107080299 Kenmore Dryer - Instructions
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- Customer:
- Richard from Fairfax, VA
- Parts Used:
- W11778253
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Needed lint filter for my old Kenmore dryer that was no longer manufactured by Sears.
Lint filter supplied by Parts Select was an exact replacement by an aftermarket manufacturer. I put the old one and the new one side by side and they were identical (of course, the handle wasn't broken off on the new one!). I coulnd't be happier. It arrived at my house 2 days after I ordered it. I highly recommend Parts Select.
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Dryer sounded like it had rocks in it when running
Following the instructions that came with the parts, I removed the top off of the dryer, which was very easy, two more 5/16" screws and I had the drum out. I confess, this was my second time at this repair. 1st time I neglected to replace the rear drum seal which I strongly recommend you do while you have it open. I only replaced the 2 wheels last time and it failed very soon afterwards.
Lesson Learned: Always replace the rear drum seal when you replace the support wheels!!!
Lesson Learned: Always replace the rear drum seal when you replace the support wheels!!!
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- Customer:
- Richard from Davie, FL
- Parts Used:
- 341241
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver
Drum stopped turning, fan continued to blow
Disconnected supply. Lifted top (hinges on rear). removed two 1/4 hex head screws retaining front panel. Disconnected door switch wires. Removed front panel, lifting off from bottom tabs. Lifted out drum and discarded broken belt. Spent 30 minutes+ cleaning interior, drum skid area, dryer exit tube, motor pulley, belt tensioner, etc, etc. Checked wiring harness for possible damage (no damage found). Repositioned drum skid pads, which had become dislodged from their intended position. Reinstalled the drum with new belt, ensuring both belt & tensioner were correctly positioned, and drum rollers and felt seals were also correctly positioned. Reinstalled front panel, tightening the two 1/4 hex head retaining screws. Reconnected power. Checked functionality. Closed top cover.
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- Customer:
- David from Bedford, IN
- Parts Used:
- 279834
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Wrench (Adjustable)
Dryer would start and heat, but after 1st cycle the burner would not fire and a buzzing sound was coming from the gas valve solenoid area. Igniter and other functions worked fine.
Removed front of dryer, unplugged each coil to determine where buzzing was coming from.....determined it was the boosting coil....ordered part and replaced. Dryer works great....we think it had be going bad over time because drying times have noticeable decreased.
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- Customer:
- Ryan from Livonia, MI
- Parts Used:
- 279834
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
dryer would not continuously heat, and took several cycles to dry clothes. The flame would ignite and heat the dryer at first, but then would ignite and go out quickly for the rest of the cycle. I tried the thermostats first with no luck.
I first ordered the coils from a different web site and they sent the wrong ones. The job would have been much eaiser if i had just returned and ordered from here. Instead i cut wires and tried the others but since they were worng, it did not work. I didn't label the wires so it was a puzzle to put it back together. Once i had the wires connected properly it was a simple fix. You just open the top and take the front pannel off, remove the drum and it is right there at the bottom. Two screws take the cover off of the coils and they slide off the gas valve. Slide the new ones on and replace the cover. Put the front pannel back on, close the top and its good to go. I first tried the highlimit thermostat, and termostat with no luck. The flame would light when it was cold, but once warmed up, the flame would ignite and immediatly go out. The coils did the trick.
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- Customer:
- J. from Oakdale, NY
- Parts Used:
- 341241
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Dryer belt snapped
There are a total of six screws that have to be removed to do this job.
Take the lint tray out and remove the first two screws.
Secondly, remove the lower panel in the front of the dryer. You do this by inserting a screwdriver at the top portion and pry it off. Next, loosen the two screws under the top panel in the front of the dryer.
Now take your screwdriver and pry up the top lid of the dryer. The last two screws are in the inside of the front panel. They hold together the front and side panels. Remove them and be sure you have a support for under the dryer drum. (once you remove the front panel, the drum no longer has a way to stay suspended)
(Make sure you disconnect the wires attached to the front door, making note of which wire goes where.)
At this point, You can follow the easy instructions that come with your new belt.
If you have a little mechanical aptitude, this is a very easy project.
Take the lint tray out and remove the first two screws.
Secondly, remove the lower panel in the front of the dryer. You do this by inserting a screwdriver at the top portion and pry it off. Next, loosen the two screws under the top panel in the front of the dryer.
Now take your screwdriver and pry up the top lid of the dryer. The last two screws are in the inside of the front panel. They hold together the front and side panels. Remove them and be sure you have a support for under the dryer drum. (once you remove the front panel, the drum no longer has a way to stay suspended)
(Make sure you disconnect the wires attached to the front door, making note of which wire goes where.)
At this point, You can follow the easy instructions that come with your new belt.
If you have a little mechanical aptitude, this is a very easy project.
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- Customer:
- Bill from Houston, TX
- Parts Used:
- 279570
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Dryer door catch broke
The old catch on my dryer door was gone and I was keeping the door closed using tape. I ordered the part and it arrived with no hassles in about 5 days. The repair was too easy. I just popped the new catch in place. It took all of about 30 seconds to complete using no tools. I wish all home repairs were this easy.
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- Customer:
- tony from prineville, OR
- Parts Used:
- WP3389441
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Top door catch assembly had broken
It was so easy, that my wife did it the day we got the part before I got home from work. She wedged it out with a flat head screw driver and then pushed the new door catch assembly in with her thumb. Pretty simple, thanks for having parts like this available to the public!
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- Customer:
- Monique from Mission Viejo, CA
- Parts Used:
- 279834
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Socket set
My dryer only heats up at the beginning of cycle so my clothes will not dry.
I remove the front control panel and to get to the bottom front dryer door off. Using my volt meter i checked all the sensors and thermal. I surf the internet for hint and some one mention to replace the coil since some time you could have one goes out and the other working still. After i replaced the coil kit it works like a champ.
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- Customer:
- Billy from Maryville, TN
- Parts Used:
- 49572A
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Wrench set
cocverting natural gas to propane gas
removed burner installed propane orfice and kit as per instruction sheet.
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- Customer:
- Chris from Morgan City, LA
- Parts Used:
- W11778253
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
old lint screen -torn at wire mesh
Local stores did not have any in supply. Went to Partselect and located lint screen, ordered, received in 3 days. replaced screen, Wife now happy again...
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- Customer:
- rex from streator, IL
- Parts Used:
- 279311
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Wrench (Adjustable)
no heat
the ignitor did not glow red checked thermal fuse by exhaust duct. fuse open replaced thermal fuse
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dryer drum not turning and no air circulating
replaced motor and drum rear seal as well as idler wheels, the old rear drum seal was completly worn out, since I had it all apart, I replaced lint chute and trap seals and belt and tensioner. I spent less money on parts than if I would have bought a new dryer. The motor was the main problem as the bearings were shot.
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The dryer belt broke. During the effort to replace the belt it was noted that the lint trap housing seals were in need of replacement.
With the dryer taken apart to replace the broken belt it was obvious that the lint seals had not been working properly due to the excessive amount of lint covering all of the inside surfaces of the dryer. The belt idler pully had also moved from its normal mounting position and was laying at the bottom of the dryer. Because the lint had covered the bottom before the belt broke it was obvious to determine where the idler pully attached to the bottom.
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
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Dryer would dry for 5-10 minuets then no heat
I tested the dryer coils and found that they were getting a voltage but would not open the gas valve. Coils were not bad but weak. After they warmed up they would not open the gas valve. It took 10 min to repace both coils and the heat sensor.
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