11096272600 Kenmore Dryer - Instructions
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- Customer:
- Douglas from Greensburg, PA
- Parts Used:
- 279769
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver
Dryer would not generate heat
My dad was ready to spend $2000 on a new washer/dryer (he has to have a matching set!). Anyway, his dryer would not generate heat. A google search turned up partselect.com, which walked me through the procedure to see what we needed.
It turned out to be a simple to replace $25.00 part! The dryer is drying as if it was brand new. Saved $1,975. Hehe.
Thanks, partselect!
It turned out to be a simple to replace $25.00 part! The dryer is drying as if it was brand new. Saved $1,975. Hehe.
Thanks, partselect!
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- Customer:
- David from Fleetwood, PA
- Parts Used:
- WPW10512946, 349241T
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Wrench (Adjustable)
One of the drum support rollers was worn out
I lifted the top of the dryer and removed the front panel. I removed the drum exposing the drum rollers. I replaced the rollers and reassembled the dryer. The exploded views on the web site made it easy to see what to do.
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Dryer would not heat during cycle.
I followed the video offered by your website and it was very informative and right to the point. Was very brief and easy to follow. I ordered the parts before 10:00am and received the parts the next day with the regular shipping.Very good website others need to benchmark you. I will use your service for future repairs and refer you to others.
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Badly worn idler pulley and rollers.
Braced dryer drum with a block. Removed the two rollers one at a time by using a screwdriver to pop off the triangular clip. Slid on new rollers. Would have been easier to remove the drum out the front instead of bracing it. Installed new idler pulley and belt. Dryer is 25 years old and sounds like a new one now when running.
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- Customer:
- Mark from Huntington Station, NY
- Parts Used:
- WP18776
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
broken clip on top panel hold down
pressed clip into hole on top of front panel. first remove two philip screws that hold filter so you can lift top up.
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- Customer:
- John from Brookings,, OR
- Parts Used:
- 279769
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Socket set, Wrench set
Dryer runs heats up, will run for a short period and then shuts down, after a minute or two it will come back on and will resume drying.
Replaced the thermastat first, then the cutoff switch, still the same, I then replaced the thermister, and still have the problem.
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- Customer:
- Dawn from Chesapeake City, MD
- Parts Used:
- 279570
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
my teenage son was messing around and got into the dryer and broke the door catch and bent the door.
removed the catch and the pin and replaced it. We were sent a couple different sizes so we tested the one that looked like the closest match. I think the pin was made with different thicknesses of metal. Worked great and saved us from having to get a new dryer!
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- Customer:
- Ronald from Oakdale, CT
- Parts Used:
- 341241
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers
Dryer belt broke- drum would not turn
This was so much easier than I though it was going to be. Pulled up on the top part of the dryer and folded it over to the back. Removed 2 screws for the front panel and disconnected some wires. Laying down I fed the new belt on and made sure the tensioner was put back into the right spot, because when the belt broke the tensioner sprung to the other end of its travel. Put everything back together. This was made super easy because you guys had the parts and the shipping was super fast. Alot of the local shops in the area didnt even carry the belt or were not helpful..
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- Customer:
- John from Midland, TX
- Parts Used:
- 279827
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Old motor was making noise and tripping after a few minutes
I disassembled the dryer once to clean the motor and compartment. After reasembly, the problem persistes. I ordered the motor and the second diasasssembly was accomplished in 10 minutes and the entire job took 45 minutes and the dryer was running like new. Tip- Leave the motor secured while removing the blower fan.
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- Customer:
- Eric from West Chester, PA
- Parts Used:
- W10820036
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Washer stopped working mid cycle restarts after resetting lid
Repair went well, but my switch only had one contact on the non common end. The new switch had two contacts. One is for operation with lid open and one for lid closed. Make sure to connect to the lid closed contact and the common on the other end and leave the lid open contact unused.
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- Customer:
- Ed from Greensboro, NC
- Parts Used:
- W11607443
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
replace lint filter
with both hands
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- Customer:
- Marcia from CAmden, NY
- Parts Used:
- 349241T
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers, Wrench set
Loud rumble noise while drum was turning
First I pulled out lint catcher, you will see two screws ,removed two the screws on top ,( philips head screw driver) I than took a putty knife and pushed in the front of the dryer under the lid and lifted the top up, I than removed a self tapping screw on each side with a 5/16 wrench and lifted the front panel out. I than pulled out the drum and this exposed the two rollers, I than pulled of the nut locks with athe pliers , took off the plastic triangle snaps and pullled off the old rollers , replaceing them with the new ones,put the triangle locks on and that the lock nuts on , I than put the drum back in, than the front panel, replaceing the two self tapping screws , snapped down the top,replaced the other two screws again on top and replaced the lint catcher, I was done.
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- Customer:
- Michael from Brownstown, PA
- Parts Used:
- WP4391960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver
Heating Element went bad
Took the back cover off and WA-LA, a bad element. Went online to PartSelect.Com and ordered the part and my Mom was drying clothes again in lees than a week. Now, I am her favorite son again.
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Broken dryer belt
Prop up the hood of the dryer with flat bar. Take out 2 screws holding dryer front end and 2 switch screws for dryer light inside dryer door. Secure dryer drum with bungee cord. Lift front end and remove. Remove broken belt. Route new belt over drum and pass underneatch idler pulley at botttom of dryer. Apply pressure to idler pulley w/one hand while securing belt around motor with the other. Make sure drum seals are snug between front and back of dryer while putting everything back together.
Have confidence. This is a very easy fix.
Have confidence. This is a very easy fix.
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Dryer had quit turning
I first disconnected the power cord and the vent hose. I removed the screws on the top of the back side to raise the top of the unit. There are also 2 screws holding the lint filter shoot which were also removed to allow the top to be lifted up. Its not necessary to remove the top since this would require disconnecting the wiring harness etc.
Next I removed the 2 screws located on the top-inside surface, which connect the front panel to the unit. After these were removed, the front panel lifts up and off--there are two clips which slid free on the bottom of the unit. The shut off switch on the door has to be disconnected to remove the panel.
With the front panel removed, the drum can be removed. I vacuumed out the interior and retrieved the idle pulley which had popped loose when the belt broke.
I removed the old rear drum seal and cleaned the edge with some brake cleaner solvent and steel wool. I then wiped the edge with paper towel and more brake cleaner to remove any oily residues. Before applying the glue, I test fit the seal which turned out to be a bit tight, so I stretched it a bit around the drum until it would fit on easily.
I used a disposible glue brush to spread a thin layer of the contact cement along the edge of the drum. By the time I finished one round, the glue was dry where I had started and so I did a second thin coat.
I then oriented the seal as per the directions and began fitting onto the edge trying to keep the free felt surface from getting into the glue. By the time I had reach the opposite side, the belt was pretty tight and so I had to stretch it a bit to get it to go on. I then worked my way around the edge a final time insuring that the seal was positioned correctly all the way around and the glue was pressed tight. I let the glue set for several hours before reassembling.
After the glue was dry, I put the drum back into the unit and worked the seal up onto the circular back panel until the groove on the drum was correctly positioned on the rear rollers. I propped the front edge of the drum on two 2 in rolls of duck tape so that I could rotate the drum freely several times. I checked the outside and inside to be sure that the seal was not turned under any place.
Finally, I slipped the new belt over the drum and past my 2 rolls of tape and positioned it groove side in over the drum. I then reinserted the tensioning pulling back into the slot just in front of the motor. The pulley goes just to the left of the motor pulley, the end of the tap on the base inserts in a slot and then 2 pins rest in a second slot to the right of the first. A loop of the belt then passes through underneath the pulley and then over the motor pulley. This requires pulling the tensioning pulling pulley towards the motor to get enough slack. I then rotated the drum several times and made sure that the belt was not twisted and the groove side was towards the drum.
To help hold the drum up while I was fitting the front panel. I supported the drum with a piece of 2 in tape run from the top/front edge of the drum to the back panel of the unit. I removed my two rolls of tape from under the unit, slipped the front panel back onto the two bottom clips, and then worked the front open of the drum over the front seal by opening the door and pushing from the inside and rotating the drum. I replugged the door switch and made sure the wire clips were secure.
I then replaced the 2 screws to hold the front panel. I put the top back down and resecured the screws on the back before reattaching the hose and replugging the unit. I test ran the unit for several minutes empty, listening for weird noises that would indicate something didn't go together correctly.
Next I removed the 2 screws located on the top-inside surface, which connect the front panel to the unit. After these were removed, the front panel lifts up and off--there are two clips which slid free on the bottom of the unit. The shut off switch on the door has to be disconnected to remove the panel.
With the front panel removed, the drum can be removed. I vacuumed out the interior and retrieved the idle pulley which had popped loose when the belt broke.
I removed the old rear drum seal and cleaned the edge with some brake cleaner solvent and steel wool. I then wiped the edge with paper towel and more brake cleaner to remove any oily residues. Before applying the glue, I test fit the seal which turned out to be a bit tight, so I stretched it a bit around the drum until it would fit on easily.
I used a disposible glue brush to spread a thin layer of the contact cement along the edge of the drum. By the time I finished one round, the glue was dry where I had started and so I did a second thin coat.
I then oriented the seal as per the directions and began fitting onto the edge trying to keep the free felt surface from getting into the glue. By the time I had reach the opposite side, the belt was pretty tight and so I had to stretch it a bit to get it to go on. I then worked my way around the edge a final time insuring that the seal was positioned correctly all the way around and the glue was pressed tight. I let the glue set for several hours before reassembling.
After the glue was dry, I put the drum back into the unit and worked the seal up onto the circular back panel until the groove on the drum was correctly positioned on the rear rollers. I propped the front edge of the drum on two 2 in rolls of duck tape so that I could rotate the drum freely several times. I checked the outside and inside to be sure that the seal was not turned under any place.
Finally, I slipped the new belt over the drum and past my 2 rolls of tape and positioned it groove side in over the drum. I then reinserted the tensioning pulling back into the slot just in front of the motor. The pulley goes just to the left of the motor pulley, the end of the tap on the base inserts in a slot and then 2 pins rest in a second slot to the right of the first. A loop of the belt then passes through underneath the pulley and then over the motor pulley. This requires pulling the tensioning pulling pulley towards the motor to get enough slack. I then rotated the drum several times and made sure that the belt was not twisted and the groove side was towards the drum.
To help hold the drum up while I was fitting the front panel. I supported the drum with a piece of 2 in tape run from the top/front edge of the drum to the back panel of the unit. I removed my two rolls of tape from under the unit, slipped the front panel back onto the two bottom clips, and then worked the front open of the drum over the front seal by opening the door and pushing from the inside and rotating the drum. I replugged the door switch and made sure the wire clips were secure.
I then replaced the 2 screws to hold the front panel. I put the top back down and resecured the screws on the back before reattaching the hose and replugging the unit. I test ran the unit for several minutes empty, listening for weird noises that would indicate something didn't go together correctly.
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