IP82000 Inglis Dryer - Instructions
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- Customer:
- David from Joppa, MD
- Parts Used:
- 279816
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
The dryer would run i.e. the drum would turn, but there was no heat so the clothes didn’t dry.
I took a ¼ inch nut driver and removed the rear cover from the unit, and then used a continuity tester to determine which safety device was open. According to the schematic there was one non-resettable safety device in the heating circuit, and that was open. The kit that I ordered came with thermal cutoff and a thermostat. I replaced both parts and the unit now operates normally. While I had the dryer open I thoroughly cleaned the dust and lint from the unit and also the 4 inch vent pipe. I ordered this part on Friday morning and received it early Saturday afternoon.
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- Customer:
- Richard from Davie, FL
- Parts Used:
- 341241
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver
Drum stopped turning, fan continued to blow
Disconnected supply. Lifted top (hinges on rear). removed two 1/4 hex head screws retaining front panel. Disconnected door switch wires. Removed front panel, lifting off from bottom tabs. Lifted out drum and discarded broken belt. Spent 30 minutes+ cleaning interior, drum skid area, dryer exit tube, motor pulley, belt tensioner, etc, etc. Checked wiring harness for possible damage (no damage found). Repositioned drum skid pads, which had become dislodged from their intended position. Reinstalled the drum with new belt, ensuring both belt & tensioner were correctly positioned, and drum rollers and felt seals were also correctly positioned. Reinstalled front panel, tightening the two 1/4 hex head retaining screws. Reconnected power. Checked functionality. Closed top cover.
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- Customer:
- J. from Oakdale, NY
- Parts Used:
- 341241
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Dryer belt snapped
There are a total of six screws that have to be removed to do this job.
Take the lint tray out and remove the first two screws.
Secondly, remove the lower panel in the front of the dryer. You do this by inserting a screwdriver at the top portion and pry it off. Next, loosen the two screws under the top panel in the front of the dryer.
Now take your screwdriver and pry up the top lid of the dryer. The last two screws are in the inside of the front panel. They hold together the front and side panels. Remove them and be sure you have a support for under the dryer drum. (once you remove the front panel, the drum no longer has a way to stay suspended)
(Make sure you disconnect the wires attached to the front door, making note of which wire goes where.)
At this point, You can follow the easy instructions that come with your new belt.
If you have a little mechanical aptitude, this is a very easy project.
Take the lint tray out and remove the first two screws.
Secondly, remove the lower panel in the front of the dryer. You do this by inserting a screwdriver at the top portion and pry it off. Next, loosen the two screws under the top panel in the front of the dryer.
Now take your screwdriver and pry up the top lid of the dryer. The last two screws are in the inside of the front panel. They hold together the front and side panels. Remove them and be sure you have a support for under the dryer drum. (once you remove the front panel, the drum no longer has a way to stay suspended)
(Make sure you disconnect the wires attached to the front door, making note of which wire goes where.)
At this point, You can follow the easy instructions that come with your new belt.
If you have a little mechanical aptitude, this is a very easy project.
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Dryer had heat intermittently and would take 3 cycles to dry a load of clothes
First, remove the back panel of dryer which is about 10 screws. Then remove the 2 thermal switches, one is above the heating element and the other is where the hot air comes out. They are both really easy to get to and the pictures on Part Select.com are identical, so you can order the part first and then just "match them up" if you are not sure what to replace. Oops, the first step is to unplug the dryer.
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- Customer:
- Leon from Jasper, AL
- Parts Used:
- 279838
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver
dryer would not heat
I removed the four screws holding the
heating element, then I pulled the element out
and then put the new element in and hucked
the wires from the old element after I disconnected
them to the new element..no problem......
heating element, then I pulled the element out
and then put the new element in and hucked
the wires from the old element after I disconnected
them to the new element..no problem......
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- Customer:
- Bill from Houston, TX
- Parts Used:
- 279570
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Dryer door catch broke
The old catch on my dryer door was gone and I was keeping the door closed using tape. I ordered the part and it arrived with no hassles in about 5 days. The repair was too easy. I just popped the new catch in place. It took all of about 30 seconds to complete using no tools. I wish all home repairs were this easy.
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- Customer:
- Michael from Plano, TX
- Parts Used:
- 279838
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Socket set
The Dryer had no heat
I ordered up a new heating coil. It was plug and play, real easy to do. Make sure to turn on the dryer with the before you put it back together to make sure the heating coils heat up. Be careful though, it will get real hot, so run for a second or two. Also, you may see a little smoke as the coil burns in, that should be fine. Once it is tested and works, let it cool off, then reattach it, put on the backplate and you are done!
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- Customer:
- David from Bend, OR
- Parts Used:
- 279838
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver
dryer wouldn't dry at all
1. UNPLUG 2.Undo 8 screws @ back of dryer. Locate heating element midway down on right about 6"x10" has three thermostat wires connected to it undo the 2 screws & 3 wires either order. You will need to pry up GENTLY on the thermostat on the old element. Replace themostat to new element and make a test run to make sure its running and HOTand repeat steps in reverse order...
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- Customer:
- lori from windsor, MO
- Parts Used:
- 279838
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
No dryer heat
Took the back off with a cordless drill with an apex holder. I unplugged the old wires from the old heating element and plugged them into the new heating element. Put the back back on after testing it to make sure it worked and that was it. Since this element was in a housing it was really simple to reinstall the new one.
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- Customer:
- Chris from Morgan City, LA
- Parts Used:
- W11778253
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
old lint screen -torn at wire mesh
Local stores did not have any in supply. Went to Partselect and located lint screen, ordered, received in 3 days. replaced screen, Wife now happy again...
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dryer did not heat anymore
My husband removed the old (2) thermostats..then installed the new ones...he said the only thing he needed was his battery run screwdriver, and it was really needed!
we are happy with the ordering, delivery, and the ease of replacement of our new parts. Thanks.
we are happy with the ordering, delivery, and the ease of replacement of our new parts. Thanks.
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- Customer:
- Shawn from Akron, OH
- Parts Used:
- 4392065
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Dyer drum doesnt turn
It was really quite esy remove the screws from the back and pop the top off . then remove 2 top inside screws from the front , lift the front off the sides , support the drum and lift out , you will then see the idler wheels, replace them with the new ones ,replce the tensioner , wrap the belt around the drum, need help putting the drum back in the case, have someone hold the drum in place while you lay on the ground and put the belt around the motor pulley and the tensioner on the bottom.you then put the front panel back into place and secure with the 2 inside screws, then put the rest back together in reverse oder. ... hope this helps someone
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dryer drum not turning and no air circulating
replaced motor and drum rear seal as well as idler wheels, the old rear drum seal was completly worn out, since I had it all apart, I replaced lint chute and trap seals and belt and tensioner. I spent less money on parts than if I would have bought a new dryer. The motor was the main problem as the bearings were shot.
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The dryer belt broke. During the effort to replace the belt it was noted that the lint trap housing seals were in need of replacement.
With the dryer taken apart to replace the broken belt it was obvious that the lint seals had not been working properly due to the excessive amount of lint covering all of the inside surfaces of the dryer. The belt idler pully had also moved from its normal mounting position and was laying at the bottom of the dryer. Because the lint had covered the bottom before the belt broke it was obvious to determine where the idler pully attached to the bottom.
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
Before cleaning I marked the exact location where the idler pully mounted to the bottom of the dryer.
While waiting for the replacement parts to be delivered a vacuum cleaner was used to remove lint from the inside surfaces of the dryer as well as the old fragments of the lint trap housing seals were removed and surfaces where the new seals would attach were cleaned.
Assembling the dryer with the new belt was a challenge due to the lack of support for the drum while getting the new belt in place, lined up properly, threaded through the idler pully and attached to the motor drive shaft. This is how I installed the new belt:
I used a piece of wood wider than the sides of the dryer, drilled holes that allowed for a piece of cloths line rope to be looped through and used to support the door opening end of the drum.
The drum was set on the seal and rollers at the back of the dryer.
The temporary wood /rope hanger was placed at the front end of the dryer resting on the sides with the top of the dryer raised.
The rope was adjusted until the drum rested on the back rollers and the rope like it would be positioned normally.
The new belt was then gently installed under the temporary support rope and around the drum.
The new belt had many kinks from shipping and was difficult to align with the location on the drum where it needs to ride so small strips of tape were temporarily used to hold the new belt in position until it could be fed through the idler pully and on to the drive shaft.
Several small pieces of a cardboard box were used to shim under the idler pully to hold it in its proper location as well as to make the belt attachment to the drive shaft easier.
With the belt attached, the temporary cardboard shims were removed from under the idler pully.
The front of the dryer was attached .
The temporary board and rope hanger was removed.
The tape that had been placed over the new belt to hold it in proper alignment was removed as the drum was rotated slowly by hand to ensure that all tape was removed prior to closing the top of the dryer.
The seals as well as the remainder of the dryer assembly was completed without any problems.
The dryer ran well for its initial trial spin and has dried several loads of laundry since.
Great parts and support Thankyou
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- Customer:
- charles from parker, CO
- Parts Used:
- 279827
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers
had to replace the motor
Follow the advice given in the partsselect website. However, while removing the blower, my hand slipped into the housing and cut my thumb. Connected the wires to the junction box on the motor but didn't realize that the contacts would hit the drum when reinstalled. The original junction box was at a 90 degree rotation relative to the new box. When trying to test the breaker tripped. Using the multitester I found out that I burned out the thermal fuse, and froze the door switch. I replace both those parts and started the dryer and could hear a grinding sound. Inspection revealed that the housing of the motor was rubbing against the drum. Removing the drum yet again, I rotated the housing and replaced the drum. The dryer was finally working well.
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