DLB1550BRL Hotpoint Dryer - Instructions
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- Customer:
- Stephen from Kendall Park, NJ
- Parts Used:
- WE25M40, WE12X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
Drum not turning, machine 20 years old
I read all the reviews first, and decided on the best method, which is, disconnect utilities, remove four phillips screws under front of top,swing top open like a box lid, pull the two spade connectors off of the door switch, loosen the two hex head screws under the front of the front panel,remove the 2 hex head screws near the top of the front panel, and free the wire harness along right side of machine, this will allow you to swing the entire front panel to the right side,now remove the three torx screws inside the drum,this will allow the drum to be removed, exposing the bearing assembly at the rear of the drum. My machine is 20 years old, and when ordering parts, my machine #s were not listed, but they looked identical, but my bearing's shaft had a circlip retaining it in the bearing receiver, which had to be removed,( the newer shaft just inserts into the receiver, which is screwed into the back of the machine). Make sure to install the ground strap like the one you removed.My best advice for someone thinking about this repair, take it apart first and survey the parts needed before making the decision to repair your old machine, my drum's old bearing allowed the machine to function, and the shaft wore through the bottom of the receiver, allowing the defector, a round disc of thin sheet metal at the back of the drum (a $128 part), to make contact with it's housing, severely damaging both parts, making further investment in this machine unwise,even if I replaced the disc, the cut in the back, would allow really hot gases to escape into the dryer's interior, a scary scenario. I cut my losses and bought a new dryer last week. Anybody want to buy a brand new rear bearing assembly & belt for a GE dryer?. If you only have to replace the bearing, the job is a snap, but prepare to do a lot of dust removal!. Steve
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- Customer:
- BJ from WHEAT RIDGE, CO
- Parts Used:
- WE25M40
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Screw drivers, Socket set
Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
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- Customer:
- John from Perry, FL
- Parts Used:
- WE12X10014
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Screw drivers
broken belt
Took the top and front off. DO NOT TAKE DRUM OFF!! Lifted drum slightly and worked belt around drum. Replaced front and top. Took off rear panel at bottom near vent pipe. Put belt around motor and then tension pulley. Buttoned everything up and that was it!
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- Customer:
- Robert from Concord, MA
- Parts Used:
- WE18X26
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Lint filter showing signs of wear. Can it be replaced?
I wanted to be sure a replacement would be available when the need arose. The dryer might be 30+ years old. Within a very few minutes I found the filter and placed an order. It arrived in 2 days. Now I won't have to worry about it in this aging lifetime.
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- Customer:
- GERI from ROCHESTER, NY
- Parts Used:
- WE18X26
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
My lint filter had broken sections in the screen
Just took it out and installed the new one--thanks so much
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- Customer:
- Matthew from Alma, WI
- Parts Used:
- WE12X10014
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Dryer Don't turn
I removed the 2 screws and lock assemblies from both sides on the back. Then i removed 4 screws (two from each side) on the control panel and lifted that up as i tipped the cover forward to disconnect the wires from the door switch. I found the wiring diagram inside the control panel cover, which included a belt routing diagram (very helpful, being the belt was laying in the bottom. I then removed 3 torx srews holding the drum to the bearing, and removed the drum. Let the fun begin! i proceded to put the belt onto the motor pulley and around the tensioner. i needed some help from my wife to set the drum back in as i held the belt up around it. once the drum was back in, i found the beld had fallen away from the tensioner. I lifted the front of the drum up just enough to get both arms below it and move the tensioner back to slip the belt over it correctly. With the new belt on i started to put the screws back in the drum. This got very frustrating, as you have to correctly line up all the holes again, while holding the drum in the correct angle to start the screws. this was the hardest part, not physically, but wears on a person's nerves quickly! Once all the screws were in and tight, i took a deep sigh of relief before i tipped the front cover up just enought to get the wires hooked back up for the door. I turned the unit on to verify the repair before re-assembly. Yep! works again, for well under $20.00! Thanks PartSelect!
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- Customer:
- James from Marco Island, FL
- Parts Used:
- WE12X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
Broken dryer belt on 30-year-old dryer
Found excellent instructions and diagrams online by searching under the model number. Best of all was the service from PartSelect. Belt arrived 24 hours after ordering. It was the right part, it was easy to install, and the dryer is running beautifully.
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- Customer:
- Joseph from Freeland, MI
- Parts Used:
- WE25M40
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers, Socket set
loud noise when ran for 5 min.
Replaced the rear drum bearing. Not doing it before ,it took about 1 1/2 hrs. Problem was fixed.
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- Customer:
- TOM from ATHENS, GA
- Parts Used:
- WE12X10014, WE4X600, WE3X75
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
Dryer Wasnt Drying ;Motor Sometimes Not Starting
Disassembled;(mainly just taking screws out) blew/vacuumed 50 pounds of lint from chassis/motor area ; replaced thermostat, and while I had it apart replaced belt and bearing. Runs/dries like new
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- Customer:
- PRESTON from CINCINNATI, OH
- Parts Used:
- WE12X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
Drum Would Not Turn
Remove the bottom cover of dryer to look at the motor, see belt hanging remove broken belt. Remove screws from the top and front, slide belt over drum put small piece of tape to hole belt in place replace screws go back to the rear pull belt over the motor pulley close back panel
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- Customer:
- George from Dassel, MN
- Parts Used:
- WE25M40
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers, Socket set, Wrench set
Dryer squeaked when running
Took the dryer apart to get to the rear bearing. Took the bearing assembly out, kept the e-ring from the old bearing shaft, replaced the bearing kit, took the o-ring off the new shaft and replaced it with the e-ring, then reassembled the unit. Make sure to place a nail or long screw into into the rear of the drum, so that you can realign bearing on the drum. It is easier with two people when reassembling.
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- Customer:
- David from EASTON, CT
- Parts Used:
- WE12X83
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers, Socket set, Wrench set
Replace broken drum belt and belt idler pully wheel.
Watched video instruction, paying attention to what it showed in machine. Several virsions of similar designs over the years, look over yours and note access points, take pictures as you go! Just pay attention, it is very logical. Spread the side panels to get the drum in and out, and pay attention to drum axel in back and the bushing it rides in. Be patient, be firm but gentle, no real forcing needed if you are alligned. Be sure the grooves of belt are on the drum, drive wheel on motor, no twists. Reverse order to reassemble. There are several internet videos of models with same basic setup, so look at others if one doesn't show the detail you need to see, or clear some uncertainty. Your local hardware to sorce push fastening for the idler wheel to shaft if you mash it up, they are cheep and several styles will work.
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- Customer:
- Barbara from Sugar Valley, GA
- Parts Used:
- WE25M40
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
dryer had a loud sqeaking noise
removed top, 2 hex screws, removed front 2 hex screws & 2 star screws. removed belt, slid drum out. Removed old bearing and replaced with new bearing kit. assembled in reverse.
It would help to have another person assist you.
It would help to have another person assist you.
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- Customer:
- Timothy from Rochester, NY
- Parts Used:
- WE25M40
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Pliers, Screw drivers, Wrench set
Drum was squeaking and making a lot of noise!
Took apart the dryer housing fairly quickly, pulled out the drum, and installed the kit. Was fairly simple. Then reassembled. The hardest part was trying to get the belt on properly and reconnect to the motor. Believe it or not, I wasted most of my time on the belt. Should've watched the video better and listened to my wife and her suggestions.
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- Customer:
- Edward from CAMP VERDE, AZ
- Parts Used:
- WE25X60
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Socket set
Squeak when running
Moved the dryer so I had room to work. Took off front of dryer with torx socket. Took off drum belt then able to take out the drum. The glides were worn replaced with two new glides (held in with 5/16 screws). While apart replaced the heater assembly and replacement of the drum belt. Went very well and smooth.
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