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HDS600SBLWH General Electric Dryer - Instructions

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All Instructions for the HDS600SBLWH
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Customer:
Charles from POINT HARBOR, NC
Parts Used:
WE12X10014
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
Dryer motor was running, but the drum stopped turning. The drive belt was broken.
I followed the instructions in your detailed online video. Fortunately on my model there was a removable panel on the back of the dryer which provided easy access to install the drive belt on the motor pulley and the idler pulley. Great video and very easy repair.
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Customer:
E J from S HAMILTON, MA
Parts Used:
WE4X584
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
Only heating on 'high' setting
Per suggestion of "Parts Select", I replaced the "high limit thermostat"....very simple task on the dryer: 1 - unplug from power source; 2 - remove screws securing top to front (open door, screws located beneath lip of unit); 3 - tilt top up allowing access to everything; 4 - remove connections to 'thermostat' (note which wires go where); 5 - loosen screws securing thermostat to unit and remove thermostat; 6 - vacuum any and all lint while unit is apart; 7 - install new thermostat and put everything back together; 8 - test dryer to see if repairs worked!
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Customer:
David from Dublin, OH
Parts Used:
WE12X10014
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers
Drum was not turning
This is the third time for a belt on this 28 year old dryer. Not too much to it. Unplug the dryer. Open the door. Remove the screws holding on the front panel and loosen the screw at the bottom. Disconnect the wires to the door switch and lift off the front panel and start up the shop vac to clean out the lint - there is a lot to be found in various places. Slide the new belt over the front of the drum and make sure there are no twists. You can now reverse the order to mounte the front panel but don't close the top so you have light to see inside. Go around to the back panel and remove the machine bolts holding on the access panel at the back. This allows access to the motor and belt tensioner. Get the shop vac out here and get to some more lint. Google the model number to find a diagram on how to route the belt. Put the belt on the motor shaft and around the tensioner as depicted. Occaisionally the plastic idler pully is worn and this can be the cause of the brokent belt. If the idler wheel does not spin freely, squeads or is cracked it should be replaced or you will be right back replacing the belt again. If all is fine it is time for a test run. CAUTION - you can plug the dryer in but keep your hands out of the cabinet as there are live exposed 220 volt terminals exposed. This allows you to observe that all is working and not binding during a test run with NO heat. If all is fine, unplug the dryer and put the covers back on. Reconnect the exhaust hose (now is a good time to clean that and the vent to outdoors as well).
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Customer:
Stephen from Kendall Park, NJ
Parts Used:
WE25M40, WE12X10014
Difficulty Level:
Easy
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Screw drivers, Socket set
Drum not turning, machine 20 years old
I read all the reviews first, and decided on the best method, which is, disconnect utilities, remove four phillips screws under front of top,swing top open like a box lid, pull the two spade connectors off of the door switch, loosen the two hex head screws under the front of the front panel,remove the 2 hex head screws near the top of the front panel, and free the wire harness along right side of machine, this will allow you to swing the entire front panel to the right side,now remove the three torx screws inside the drum,this will allow the drum to be removed, exposing the bearing assembly at the rear of the drum. My machine is 20 years old, and when ordering parts, my machine #s were not listed, but they looked identical, but my bearing's shaft had a circlip retaining it in the bearing receiver, which had to be removed,( the newer shaft just inserts into the receiver, which is screwed into the back of the machine). Make sure to install the ground strap like the one you removed.My best advice for someone thinking about this repair, take it apart first and survey the parts needed before making the decision to repair your old machine, my drum's old bearing allowed the machine to function, and the shaft wore through the bottom of the receiver, allowing the defector, a round disc of thin sheet metal at the back of the drum (a $128 part), to make contact with it's housing, severely damaging both parts, making further investment in this machine unwise,even if I replaced the disc, the cut in the back, would allow really hot gases to escape into the dryer's interior, a scary scenario. I cut my losses and bought a new dryer last week. Anybody want to buy a brand new rear bearing assembly & belt for a GE dryer?. If you only have to replace the bearing, the job is a snap, but prepare to do a lot of dust removal!. Steve
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Customer:
BJ from WHEAT RIDGE, CO
Parts Used:
WE25M40
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Screw drivers, Socket set
Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
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Customer:
John from Dushore, PA
Parts Used:
WE12X10014
Difficulty Level:
A Bit Difficult
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers
Belt broke, tumbler did not turn.
After identifying the issue, the biggest issue was trying to identify how to get the belt around the drum tumbler. After looking through the back hatch, I figured the best way was through the top. I removed the top just enough to work the belt in between the drum and the front sheet metal. Then I turned it on its side and worked the belt from the back hatch. I pulled the pulley back on the tensioner and slipped the belt under neath. Put it back together, been working great.
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Customer:
Mark from Teaneck, NJ
Parts Used:
WE18X54
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
My GE Hotpoint dryer would not completely dry clothes due to rusty and clogged flint filter.
I just pulled out the old white frame by hand and replaced it with a new one ordered online. No tools were needed. Simply easily, anyone can do with no required skills.

This saved the appliance from possible damage due to poor ventilation and also save the cost of a handyman to fix the problem.
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Customer:
richard from pleasant grove, AL
Parts Used:
WE01X20419
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Plastic Door Handle Cracked
Old handle popped out by pulling back and out. Inserted new handle by pushing in and forward. Easy!
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Customer:
Rick from Nora Springs, IA
Parts Used:
WE01X20419
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Bottom part of handle was loose
Opened up the package and took off existing door handle. The new one snapped right into place. This took all of 10 seconds!
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Customer:
Dan from Erie, PA
Parts Used:
WE18X54
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
The lint filter was cracked/ screen came off
Very simple. Took the old 1 out and placed new filter in.
The impressive thing was I ordered the part on a Saturday and received it on the following Wednesday. Thank you! I will for sure recommend your site to my family/friends.
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Customer:
Bud from RCH CUCAMONGA, CA
Parts Used:
WE01X20419
Difficulty Level:
Very Easy
Total Repair Time:
Less than 15 mins
Broken door handle
Snapped right into place , less than a minute, if that
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Customer:
Steve from West Bloomfield, MI
Parts Used:
WE01X20419
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Plastic handle in dryer broke off.
All I neede to do was buy the new part and snap it into place on the door. The hardest part was making the door usable while waiting for a new handle. The solution was good old duct tape. I just taped the old broken handle in place until the new one showed up.
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Customer:
William from San Juan, TX
Parts Used:
WE25M40
Difficulty Level:
Difficult
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Wrench set
Very loud squeak with drum rotation
Key starting point is to remove top cover by removing two long screws located at the front of the cover
Remove control panel and it's bottom and side supports.
Remove short vent pipe by bending retainer tab.
Support the drum at the top using piece of rope.
Remove main rear cover (leave bottom attached).
Remove electric heating unit and install new bearing carrier from kit.
Reinstall the the heating unit
Remove three screws (inside the drum)to release the inner drum cover and release the bearing carrier.
Install new bearing carrier. Note: the three holes in the bearing carrier are not tapped, I suggest that the screws be installed (threads cut) into the bearing cover before attempting to install the bearing carrier.
Install the new bearing carrier. Note: pilot one of the holes using a small nail etc. then go on to install screws in the other two holes remove the pilot device and install the third screw.
Reassemble in reverse order.
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Customer:
mountain ridge pet from nashua, NH
Parts Used:
WE3X75
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
squeaking noise then drum stopped turning
The repair in retrospect was very easy. Not knowing alot about the dryer I made one mistake. I put the bearing in backwards and broke the rubber gasket. After ordering a new gasket and paying close attention to what I was doing it worked out fine. Saved me about $200 for a repairman.
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Customer:
janet from martinsville, IN
Parts Used:
WE1X1192
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
dryer did not latch
easy to fix took less than 10 minutes
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All Instructions for the HDS600SBLWH
76 - 90 of 291