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DBLR333GT1WW General Electric Dryer - Instructions

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All Instructions for the DBLR333GT1WW
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Customer:
Stephen from Kendall Park, NJ
Parts Used:
WE25M40, WE12X10014
Difficulty Level:
Easy
Total Repair Time:
More than 2 hours
Tools:
Nutdriver, Screw drivers, Socket set
Drum not turning, machine 20 years old
I read all the reviews first, and decided on the best method, which is, disconnect utilities, remove four phillips screws under front of top,swing top open like a box lid, pull the two spade connectors off of the door switch, loosen the two hex head screws under the front of the front panel,remove the 2 hex head screws near the top of the front panel, and free the wire harness along right side of machine, this will allow you to swing the entire front panel to the right side,now remove the three torx screws inside the drum,this will allow the drum to be removed, exposing the bearing assembly at the rear of the drum. My machine is 20 years old, and when ordering parts, my machine #s were not listed, but they looked identical, but my bearing's shaft had a circlip retaining it in the bearing receiver, which had to be removed,( the newer shaft just inserts into the receiver, which is screwed into the back of the machine). Make sure to install the ground strap like the one you removed.My best advice for someone thinking about this repair, take it apart first and survey the parts needed before making the decision to repair your old machine, my drum's old bearing allowed the machine to function, and the shaft wore through the bottom of the receiver, allowing the defector, a round disc of thin sheet metal at the back of the drum (a $128 part), to make contact with it's housing, severely damaging both parts, making further investment in this machine unwise,even if I replaced the disc, the cut in the back, would allow really hot gases to escape into the dryer's interior, a scary scenario. I cut my losses and bought a new dryer last week. Anybody want to buy a brand new rear bearing assembly & belt for a GE dryer?. If you only have to replace the bearing, the job is a snap, but prepare to do a lot of dust removal!. Steve
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Customer:
Dan from Erie, PA
Parts Used:
WE18X54
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
The lint filter was cracked/ screen came off
Very simple. Took the old 1 out and placed new filter in.
The impressive thing was I ordered the part on a Saturday and received it on the following Wednesday. Thank you! I will for sure recommend your site to my family/friends.
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Customer:
richard from pleasant grove, AL
Parts Used:
WE01X20419
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Plastic Door Handle Cracked
Old handle popped out by pulling back and out. Inserted new handle by pushing in and forward. Easy!
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Customer:
Steve from West Bloomfield, MI
Parts Used:
WE01X20419
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Plastic handle in dryer broke off.
All I neede to do was buy the new part and snap it into place on the door. The hardest part was making the door usable while waiting for a new handle. The solution was good old duct tape. I just taped the old broken handle in place until the new one showed up.
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Customer:
Mark from Teaneck, NJ
Parts Used:
WE18X54
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
My GE Hotpoint dryer would not completely dry clothes due to rusty and clogged flint filter.
I just pulled out the old white frame by hand and replaced it with a new one ordered online. No tools were needed. Simply easily, anyone can do with no required skills.

This saved the appliance from possible damage due to poor ventilation and also save the cost of a handyman to fix the problem.
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Customer:
Rob from Valencia, CA
Parts Used:
WE12X10014
Difficulty Level:
Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Screw drivers
Dryer shut down completely, wouldn't start
Removed 3 torx screws on the control panel. Removed two more regular screws from the dryer opening. This allows removal of the top. Removed some panels from the back to access where belt feeds through the motor. Found the belt snapped in two inside.

Now that I knew what the problem was I found partselect.com on Google. Ordered the part friday morning with ground. The belt arrived SATURDAY MORNING! I didn't even know fedex would deliver ground shipments on Saturday. Less than 24 hours later I had it. AWESOME.

Removed the front panel by removing two hex bolts to allow me to drape the belt over the drum. Not having seen how the belt was originally around the tensioner and the bad diagrams included with the dryer, it took some figuring to get it back on right. But we did it and we're back in business. I will absolutely buy from PartSelect.com again!
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Customer:
William from San Juan, TX
Parts Used:
WE25M40
Difficulty Level:
Difficult
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Wrench set
Very loud squeak with drum rotation
Key starting point is to remove top cover by removing two long screws located at the front of the cover
Remove control panel and it's bottom and side supports.
Remove short vent pipe by bending retainer tab.
Support the drum at the top using piece of rope.
Remove main rear cover (leave bottom attached).
Remove electric heating unit and install new bearing carrier from kit.
Reinstall the the heating unit
Remove three screws (inside the drum)to release the inner drum cover and release the bearing carrier.
Install new bearing carrier. Note: the three holes in the bearing carrier are not tapped, I suggest that the screws be installed (threads cut) into the bearing cover before attempting to install the bearing carrier.
Install the new bearing carrier. Note: pilot one of the holes using a small nail etc. then go on to install screws in the other two holes remove the pilot device and install the third screw.
Reassemble in reverse order.
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Customer:
mountain ridge pet from nashua, NH
Parts Used:
WE3X75
Difficulty Level:
Easy
Total Repair Time:
1- 2 hours
Tools:
Nutdriver, Pliers, Screw drivers, Socket set
squeaking noise then drum stopped turning
The repair in retrospect was very easy. Not knowing alot about the dryer I made one mistake. I put the bearing in backwards and broke the rubber gasket. After ordering a new gasket and paying close attention to what I was doing it worked out fine. Saved me about $200 for a repairman.
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Customer:
Ruth from Frederick, MD
Parts Used:
WE9X1090
Difficulty Level:
A Bit Difficult
Total Repair Time:
30 - 60 mins
Tools:
Pliers
Tabs on gasket were not spaced as on door
Had to skip holes for tabs on corners. could not stretch gasket to fit the holes. Cut off the unused tabs in order to close door. Used pliers to push tabs in holes. New gasket fit sufficently and is better than old cracked gasket.
3 of 5 people found this instruction helpful.
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Customer:
Linda from Clermont, FL
Parts Used:
WH1X2721
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Selector knob broke off
I ordered a selector knob and it was delivered in a short amount of time. I wasn't sure if it was the right one when I ordered it, but my husband just put it right on the dryer. He said it was perfect. Thank you PartSelect!
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Customer:
Edward from Garrison, NY
Parts Used:
WE4X881
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Pliers, Screw drivers
there was no problem
installation exactly how your directions told me on the computer
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Customer:
BJ from WHEAT RIDGE, CO
Parts Used:
WE25M40
Difficulty Level:
A Bit Difficult
Total Repair Time:
More than 2 hours
Tools:
Screw drivers, Socket set
Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
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Customer:
James from NAPLES, FL
Parts Used:
WE1X1263
Difficulty Level:
Very Easy
Total Repair Time:
Less than 15 mins
Timer knob was stripped
Popped the timer knob on and it was a perfect fit. Works great!
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Customer:
DERALD from Burleson, TX
Parts Used:
WE4X881
Difficulty Level:
Really Easy
Total Repair Time:
Less than 15 mins
Tools:
Screw drivers
Switch was either stuck in start position or had to rotate full turn to start
Removed four allen head screws to expose inside of panel. Used flat blade screwdriver to raise spring retainer and turned switch counter clockwise to remove.
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Customer:
Richard from LORDSBURG, NM
Parts Used:
WB1X500D
Difficulty Level:
Really Easy
Total Repair Time:
30 - 60 mins
Tools:
Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable)
No Spin Cycle
Lid Switch.
Rewiring connection.
Function is satisfactory.
Fan belt ordered is saved.
A 1970 Clothes Washer.
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All Instructions for the DBLR333GT1WW
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