861-4730-090 General Electric Dryer - Instructions
Jump to:
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
- Customer:
- Thomas from Terre Haute, IN
- Parts Used:
- WE12X10014, WE12X81
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers, Socket set
Dryer drum would not turn
After opening the front door there are screws that are holding the top to the door. Take those screws out using a Phillips screwdriver. The top should lift up and rest at a near 90 degree angle.
The door has two screws at the bottom that need to be taken out. Once those are out there are two screws on both sides at the top holding it to the frame. Remove those as well.
Before you remove the front you should document the wiring for the door light switch. I took these off to give the door a little extra room so I could rest it on a toolbox without taking all the wires completely off.
Once the door is free, on the back there is a metal plate with two screws in it roughly in the middle of the unit. Unscrew the top completely but leave the bottom screw in and just slightly loosen it. This will allow it to swing down out of the way without the need to completely remove it and have one more part to put back together in the end.
What this plate is covering is the center of the drum. There is a small metal tab that you can push on and it will push the drum out so it can be removed. Gripping the drum, you can lift it out by guiding it through the notches on each side where the drum protrudes.
With the drum removed you'll see the motor and idle pulley. On my model the pulley was attached to a metal rod that was spring loaded. The pulley is held on by a small tension washer that was easily removed with pliers. Installation was somewhat more difficult but mostly just getting it lined up and started. Once on the rod it was easy to push it into place.
With the new pulley installed it's time to install the new belt. To do this first put the belt over the drop and then replace the drum back into the frame. Once the drum is pushed back into the hole it will support itself.
Now you need to remove the panel on the back to get access to the motor and pulley. This panel has a lot of screws. Once that's off you can then guide the belt over the motor and get the idle pulley to put tension on the belt.
Once that is complete just replace all the screws you removed, plug it back in and watch as your new belt moves the drum once again.
The door has two screws at the bottom that need to be taken out. Once those are out there are two screws on both sides at the top holding it to the frame. Remove those as well.
Before you remove the front you should document the wiring for the door light switch. I took these off to give the door a little extra room so I could rest it on a toolbox without taking all the wires completely off.
Once the door is free, on the back there is a metal plate with two screws in it roughly in the middle of the unit. Unscrew the top completely but leave the bottom screw in and just slightly loosen it. This will allow it to swing down out of the way without the need to completely remove it and have one more part to put back together in the end.
What this plate is covering is the center of the drum. There is a small metal tab that you can push on and it will push the drum out so it can be removed. Gripping the drum, you can lift it out by guiding it through the notches on each side where the drum protrudes.
With the drum removed you'll see the motor and idle pulley. On my model the pulley was attached to a metal rod that was spring loaded. The pulley is held on by a small tension washer that was easily removed with pliers. Installation was somewhat more difficult but mostly just getting it lined up and started. Once on the rod it was easy to push it into place.
With the new pulley installed it's time to install the new belt. To do this first put the belt over the drop and then replace the drum back into the frame. Once the drum is pushed back into the hole it will support itself.
Now you need to remove the panel on the back to get access to the motor and pulley. This panel has a lot of screws. Once that's off you can then guide the belt over the motor and get the idle pulley to put tension on the belt.
Once that is complete just replace all the screws you removed, plug it back in and watch as your new belt moves the drum once again.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Vernon from BALTIMORE, MD
- Parts Used:
- WE12X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set
Replaced dyer belt
First unplug dryer... very important. You have to identify the appropriate size socket wrench and locate all necessary screws to remove top panel of dryer and front panel. Locate belt drive. Remove old belt , replacing it with new belt attaching belt to dryer drum . Remove back panel of dryer to better reach and adjust belt onto tension wheels. Put dyer back together. YouTube gives you an idea of how to properly change a belt on dryer
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Michael from lexington, NC
- Parts Used:
- WE12X10014
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
dryer would not rotate clothes to dry
first I removed the screws with the nutdriver at the bottom of the dryer at the back..then I could see the belt was broken...next I took off the 2 nuts at the back that hold the top on ..then opened the dryer front door and unscrewd the 4 screws holding the top on....then I lifted the top up and to the side...then all I had to do was take out 2 screws one on each side of dryer front and the the front was open enough that I could slide the new belt on dryer..then screwed the front back on...then placed the top on and went to the back of dryer and put belt on pulley using the diagram I found in the instructions inside the dryer top...really a lot easier than it sounds...easy fix saved me from buying another dryer
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Robert J from Egg Harbor City,, NJ
- Parts Used:
- WE3X75
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Socket set
Dryer was producing a screeching noise while running
I removed the front panel and the top of the dryer, pulled the drum forward and removed the old rear drum bearing then inserted the new rear drum bearing. I didn't replace the washers or the retaining ring in the back. Put the drum shaft into the new rear drum bearing. Put the front panel and the top in place and started using the dryer again.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Philip from Fairfax City, VA
- Parts Used:
- WE11X260
- Difficulty Level:
- Very Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
heater coils burnt out
Took apart the entire dryer. Cleaned and vacuumed all parts.
Removed drum assembly and threaded new coils in insulators.
Connected new heater coils to supply terminals and then reassembled dryer. Key to proper assembly was having threaded keys to properly allign the dryer drum during assembly. Dryer was tested and it works like a new dryer now. Old dryers have higher quality motors than newer dryers.
Removed drum assembly and threaded new coils in insulators.
Connected new heater coils to supply terminals and then reassembled dryer. Key to proper assembly was having threaded keys to properly allign the dryer drum during assembly. Dryer was tested and it works like a new dryer now. Old dryers have higher quality motors than newer dryers.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Neil from Royal Oak, MI
- Parts Used:
- WE25M40, WE12X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
bad drum bearing caused motor pulley to burn through belt
Top is hinged in back, removing the 4 screws over the door under the top allowed the top to open. Removing the 2 screws near the top of the door panel allowed it's removal. Marked and disconnected wiring. Lifted drum through top. New bearing housing required 3 mounting holes to be tapped to 10-24. Installed bearing and backing shims with old hardened allen head mounting screws inside drum while wife held bearing in back of drum. Furnished 3- 10-24 lock nuts to lock mounting screws in place from their back side. Reinserted drum through dryer top with belt on drum. Hardest part was getting the belt on motor pulley while holding the idler in it's correct position due to small access holes at the very bottom in rear panel. Works just fine again.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Stephen from Kendall Park, NJ
- Parts Used:
- WE25M40, WE12X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Screw drivers, Socket set
Drum not turning, machine 20 years old
I read all the reviews first, and decided on the best method, which is, disconnect utilities, remove four phillips screws under front of top,swing top open like a box lid, pull the two spade connectors off of the door switch, loosen the two hex head screws under the front of the front panel,remove the 2 hex head screws near the top of the front panel, and free the wire harness along right side of machine, this will allow you to swing the entire front panel to the right side,now remove the three torx screws inside the drum,this will allow the drum to be removed, exposing the bearing assembly at the rear of the drum. My machine is 20 years old, and when ordering parts, my machine #s were not listed, but they looked identical, but my bearing's shaft had a circlip retaining it in the bearing receiver, which had to be removed,( the newer shaft just inserts into the receiver, which is screwed into the back of the machine). Make sure to install the ground strap like the one you removed.My best advice for someone thinking about this repair, take it apart first and survey the parts needed before making the decision to repair your old machine, my drum's old bearing allowed the machine to function, and the shaft wore through the bottom of the receiver, allowing the defector, a round disc of thin sheet metal at the back of the drum (a $128 part), to make contact with it's housing, severely damaging both parts, making further investment in this machine unwise,even if I replaced the disc, the cut in the back, would allow really hot gases to escape into the dryer's interior, a scary scenario. I cut my losses and bought a new dryer last week. Anybody want to buy a brand new rear bearing assembly & belt for a GE dryer?. If you only have to replace the bearing, the job is a snap, but prepare to do a lot of dust removal!. Steve
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- John from Dushore, PA
- Parts Used:
- WE12X10014
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Belt broke, tumbler did not turn.
After identifying the issue, the biggest issue was trying to identify how to get the belt around the drum tumbler. After looking through the back hatch, I figured the best way was through the top. I removed the top just enough to work the belt in between the drum and the front sheet metal. Then I turned it on its side and worked the belt from the back hatch. I pulled the pulley back on the tensioner and slipped the belt under neath. Put it back together, been working great.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- BJ from WHEAT RIDGE, CO
- Parts Used:
- WE25M40
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Screw drivers, Socket set
Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Rob from Valencia, CA
- Parts Used:
- WE12X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Dryer shut down completely, wouldn't start
Removed 3 torx screws on the control panel. Removed two more regular screws from the dryer opening. This allows removal of the top. Removed some panels from the back to access where belt feeds through the motor. Found the belt snapped in two inside.
Now that I knew what the problem was I found partselect.com on Google. Ordered the part friday morning with ground. The belt arrived SATURDAY MORNING! I didn't even know fedex would deliver ground shipments on Saturday. Less than 24 hours later I had it. AWESOME.
Removed the front panel by removing two hex bolts to allow me to drape the belt over the drum. Not having seen how the belt was originally around the tensioner and the bad diagrams included with the dryer, it took some figuring to get it back on right. But we did it and we're back in business. I will absolutely buy from PartSelect.com again!
Now that I knew what the problem was I found partselect.com on Google. Ordered the part friday morning with ground. The belt arrived SATURDAY MORNING! I didn't even know fedex would deliver ground shipments on Saturday. Less than 24 hours later I had it. AWESOME.
Removed the front panel by removing two hex bolts to allow me to drape the belt over the drum. Not having seen how the belt was originally around the tensioner and the bad diagrams included with the dryer, it took some figuring to get it back on right. But we did it and we're back in business. I will absolutely buy from PartSelect.com again!
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- E. Thomas from REDONDO BEACH, CA
- Parts Used:
- WE12X10014, WE25X60
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Screw drivers
Dryer leaving marks on clothes. Clothes were getting caught between drum and outside ring. Worn slides.
Remove top panel and front panel. 12 Screws. Be sure to vacuum entire inside of cabinet free of lint.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- David from Dublin, OH
- Parts Used:
- WE12X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Drum was not turning
This is the third time for a belt on this 28 year old dryer. Not too much to it. Unplug the dryer. Open the door. Remove the screws holding on the front panel and loosen the screw at the bottom. Disconnect the wires to the door switch and lift off the front panel and start up the shop vac to clean out the lint - there is a lot to be found in various places. Slide the new belt over the front of the drum and make sure there are no twists. You can now reverse the order to mounte the front panel but don't close the top so you have light to see inside. Go around to the back panel and remove the machine bolts holding on the access panel at the back. This allows access to the motor and belt tensioner. Get the shop vac out here and get to some more lint. Google the model number to find a diagram on how to route the belt. Put the belt on the motor shaft and around the tensioner as depicted. Occaisionally the plastic idler pully is worn and this can be the cause of the brokent belt. If the idler wheel does not spin freely, squeads or is cracked it should be replaced or you will be right back replacing the belt again. If all is fine it is time for a test run. CAUTION - you can plug the dryer in but keep your hands out of the cabinet as there are live exposed 220 volt terminals exposed. This allows you to observe that all is working and not binding during a test run with NO heat. If all is fine, unplug the dryer and put the covers back on. Reconnect the exhaust hose (now is a good time to clean that and the vent to outdoors as well).
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Charles from POINT HARBOR, NC
- Parts Used:
- WE12X10014
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
Dryer motor was running, but the drum stopped turning. The drive belt was broken.
I followed the instructions in your detailed online video. Fortunately on my model there was a removable panel on the back of the dryer which provided easy access to install the drive belt on the motor pulley and the idler pulley. Great video and very easy repair.
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Dennis from Brilliant, AL
- Parts Used:
- WE18X26
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
Temperature Switch failed. Lint Filter warped from over-heat.
Removed filter as for cleaning. Replaced with new filter. NO TOOLS REQUIRED!
Was this instruction helpful to you?
Thank you for voting!
- Customer:
- Michael from Edmond, OK
- Parts Used:
- WE25M40
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers, Socket set
Rythmical Squeaking
The instructions that came with the bearing were limited and the illustrations were too dark to see. However, after reading the reports of others on this website, the repair was very easy.
Prior to disassembly, remove theaccess panel on the rear of the dryer. Pull the belt drive pulley arm up and the belt will easily slide off of the motor pulley. The belt can be left on the drum.
Then, remove two screws at the inside top of the dryer door. The top of the dryer will then lift up at the front and slide forward to remove. This will allow you access to two bolt head screws on each side of the front panel. Remove these two screws and then lift the panel slightly up and forward. The front panel will then be free and the dryer drum will slide forward and out. Remove the four bolt head screws (behind the electric elements) from the heater element on the inside back of the dryer box.
You can now exchange the bearing on the drum and the bearing insert on the dryer heating element simply by removing the old and reinstalling the new just as the old was removed - four screws for each.
You will need an assistant to re-install the bearing. Someone needs to hold the three pieces behind the drum as you insert the three screws. You'll also need a star wrench set for this.
The drum is easily reinserted - just be careful to get the front of the drum placed into the front bearing surface when reinstalling the front panel. One word of caution, My wife tried to remove the felt bearing on the bottom of the front panel thinking that it was lint.
I found that the inside of my ten year old dryer was unbelievably full of lint. I'm sure that the efficiency improvements by cleaning the air passages will be substantial and I've just saved $400 on the price of a similar dryer ($900 if my wife and I decided to upgrade to the "new" model that we wanted but really didn't need.
Prior to disassembly, remove theaccess panel on the rear of the dryer. Pull the belt drive pulley arm up and the belt will easily slide off of the motor pulley. The belt can be left on the drum.
Then, remove two screws at the inside top of the dryer door. The top of the dryer will then lift up at the front and slide forward to remove. This will allow you access to two bolt head screws on each side of the front panel. Remove these two screws and then lift the panel slightly up and forward. The front panel will then be free and the dryer drum will slide forward and out. Remove the four bolt head screws (behind the electric elements) from the heater element on the inside back of the dryer box.
You can now exchange the bearing on the drum and the bearing insert on the dryer heating element simply by removing the old and reinstalling the new just as the old was removed - four screws for each.
You will need an assistant to re-install the bearing. Someone needs to hold the three pieces behind the drum as you insert the three screws. You'll also need a star wrench set for this.
The drum is easily reinserted - just be careful to get the front of the drum placed into the front bearing surface when reinstalling the front panel. One word of caution, My wife tried to remove the felt bearing on the bottom of the front panel thinking that it was lint.
I found that the inside of my ten year old dryer was unbelievably full of lint. I'm sure that the efficiency improvements by cleaning the air passages will be substantial and I've just saved $400 on the price of a similar dryer ($900 if my wife and I decided to upgrade to the "new" model that we wanted but really didn't need.
Was this instruction helpful to you?
Thank you for voting!