7308-87C Frigidaire Dryer - Instructions
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- Customer:
- Luann from Huntersville, NC
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Lint screen had torn
For me it wasn't even a repair, but rather, open the package, take out and discard the old lint tray and pop the new one in! Done. I didn't have to replace the frame. I would like to comment on how easy ordering was from partselect.com and how quickly the part arrived. Very satisfied customer! Thank you!
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- Customer:
- Joyce from North Dighton, MA
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
The lint screen had tears on it which could cause a serious problem, possibly a fire.
I unscrewed the old the lint screen FRAME and easily removed it, replacing it with the new one. The new lint -- SCREEN -- just needed to be squeezed here and there, and molded into a better shape. The screen itself, arrived flattened on the bottom, causing it to be too wide and difficult to remove from the frame. I easily molded it with my hands into the shape of the previous one and it slipped right into place. ( Shaped like an oval, flexible sack.) VERY easy!
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- Customer:
- Michael from MAPLE GROVE, MN
- Parts Used:
- 5303281154, 5303281153, 5303212849
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- More than 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers, Socket set
VERY NOISY!!!
Have done this before - dissembled, cleaned everything, re-assembled with new parts - rear bearing, idler, and belt. Hardest part is getting the spring back on the idler pulley.
You take the top lid off, remove the front panel and then the drum. remove the access panel on the back to release the spring tension on the idler pulley, then remove the drum. Vacuum clean everything, then reassemble with new stem and bearing, new belt, and idler pulley. Test spin drum by hand - if belt comes off it's likely twisted. Put belt back on and try again. Try operating with air mode to spin drum. If belt stays on, complete re-assembling and make sure you have no screws left over!
You take the top lid off, remove the front panel and then the drum. remove the access panel on the back to release the spring tension on the idler pulley, then remove the drum. Vacuum clean everything, then reassemble with new stem and bearing, new belt, and idler pulley. Test spin drum by hand - if belt comes off it's likely twisted. Put belt back on and try again. Try operating with air mode to spin drum. If belt stays on, complete re-assembling and make sure you have no screws left over!
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- Customer:
- Michel from CHICAGO, IL
- Parts Used:
- 5303281153, 5303281153, 131825900, 5303281153
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers
The drier was "screeching"
First of all, the folks at Part Select have been terrific. I balled up my address and they were great in correcting my error and getting the parts promptly to me. They provide directions with the parts. And You Tube, is a wealth of information too. The process is to remove the drum and replace the nylon busihing that supports the drum at the back of the machine. Getting it out was no sweat. Getting the drum back in was a bit more challenging single handed. If I was going to make any suggestion it would be this is a good project for two sets of hands with the second set needed for about ten minutes. The You Tube video I watched said putting the front cover with the drum attached to the back of the unit would be the challenge and they were right. Otherwise, super easy and the results are it's back to "new" condition. Thanks again to Part Select!
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- Customer:
- Gordon from Canton, PA
- Parts Used:
- 5303281049
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers
Small burn marks on light clothing
First I unpluged the machine, then opened the top with a flat head screw driver. Then I removed the two screws inside, unpluged the door sensor. (makes it stop when opened) Removed old gasket, cleaned with emery cloth, cleaned the residue and applied the glue provided. Waited about 1 min. and applied the new gasket leaving about 1/8'' of it hanging over the door facing the drum.
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- Customer:
- Doug from ODESSA, TX
- Parts Used:
- 5303281153, 5303281153, 131825900, 5303281153
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
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- Customer:
- Harriett from Leesburg, FL
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Needed new lint screen for dryer
Removed 2 screws and dropped new screen holder in with lint screen in it and replaced screws. Really easy
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- Customer:
- Reveice E from Arcadia, FL
- Parts Used:
- 5303281154
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Dryer wouldn't spin, belt broken
Popped the top of the dryer off. Removed 3 screws from lower front panel. Removed front panel slide belt over drum, remove 2 bolts from rear panel and installed belt over motor and around idler tensioner. Reinstalled front panel and top of dryer . Also greased idler pulley to shaft , beings tensioner was okay. Plugged in and tested dryer, it was okay.
We went to PartSelect. com and order the belt and it was fast shipping. We couldn't find the belt anywhere else. Thanks for PartSelect.
We went to PartSelect. com and order the belt and it was fast shipping. We couldn't find the belt anywhere else. Thanks for PartSelect.
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- Customer:
- Steve from COVINGTON, KY
- Parts Used:
- 134120900
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Dryer not heating
UNPLUG DRYER (this is key) Removed the top of dryer. used screwdriver and pliers to remove two screws and electrical connections then reinstalled new part stick the magnet behind the part to the back of the dryer to help control the small screws.
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- Customer:
- Ben from Weaverville, NC
- Parts Used:
- 5303281154, 5303212849
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Dryer drum would not turn
I first removed a vent cover in the back where the idler is located. With pliers I removed the tension off the spring. Next I simply slide the idler off the post. I pulled up on the top panel which opened like a clam shell. I used a flat blade screw driver to separate the front panel from the dryer so I could slide the new belt around the drum. I reversed the steps. All in all it was easy. It took me about 30min including cleanup.
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- Customer:
- Timothy from CRANBURY, NJ
- Parts Used:
- 134120900
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
May not have to take out the whole drum to replace the limiter!
After lifting the dryer top and finding the location of the thermal limiter on the back of the dryer, where it is difficult to get at, I carefully cut through the dryer cabinet with the multimaster on three sides to form a 'flap' upon which the limiter was mounted. By prying this flap open from the back, the two wires and two screws are easily accessible to replace the limiter, without having to remove the whole drum. Afterwards, I just bent the flap back into place and taped the seams. If it ever blows again, the fix will take all of about two minutes.
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- Customer:
- Frank from Las Vegas, NV
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
dryer lint screen rplacement
removed two screws - replaced lint screen replacement, TIME TO REPLACE UNIT - ONE MINUTE. What made this project a snap was the pictures and graphs( parts replace) uses to ensure you are ordering the exact screen .
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- Customer:
- Bill from Shelby, MI
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Riped lint screen
This was easer than, well brushing my teeth. And it took less time than that too. Really, really easy, just like I read.
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- Customer:
- Paul from Dennis, MA
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
The lint screen was old, rusty, and torn.
This was the easiest and most inexpensive repair I ever had on a dryer. I did a search on the internet, found "PartSelect.com" searched their web site, found the part I needed (at a very reasonably low price) ordered it, received it within 2 days, opened the box, removed 2 screws from the old part, put the new part in, replaced the 2 screws, inserted the filter screen... and my wife was happy. Thank You PartSelect.com for perfect selection, ordering and service.
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- Customer:
- jeffrey from round lake heights, IL
- Parts Used:
- 5303281049
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers
The old drum seal top had torn off.
Opened the drayer top and then removed the front panel.
Removed the bottom seal from the acr as it was warn.
Carefully scarped off the remaining bits of felt from the arc.
Applied the supplied adhesive to the top half of the cleaned arc.
Placed the seal and held in place with small spring clamps.
Let it dry for an hour, then I repeated the process with the bottom seal.
I let it dry over night, overkill probably but I wanted it to stay.
Replaced the front with new seal and closed up the top.
It has been working well since. Thanks for stocking parts that help out homeowner's on tight budgets.
Removed the bottom seal from the acr as it was warn.
Carefully scarped off the remaining bits of felt from the arc.
Applied the supplied adhesive to the top half of the cleaned arc.
Placed the seal and held in place with small spring clamps.
Let it dry for an hour, then I repeated the process with the bottom seal.
I let it dry over night, overkill probably but I wanted it to stay.
Replaced the front with new seal and closed up the top.
It has been working well since. Thanks for stocking parts that help out homeowner's on tight budgets.
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