FDE216RBT0 Frigidaire Dryer - Instructions
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- Customer:
- Doug from ODESSA, TX
- Parts Used:
- 5303281153, 5303281153, 131825900, 5303281153
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
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- Customer:
- Harriett from Leesburg, FL
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Needed new lint screen for dryer
Removed 2 screws and dropped new screen holder in with lint screen in it and replaced screws. Really easy
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- Customer:
- Frank from Las Vegas, NV
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
dryer lint screen rplacement
removed two screws - replaced lint screen replacement, TIME TO REPLACE UNIT - ONE MINUTE. What made this project a snap was the pictures and graphs( parts replace) uses to ensure you are ordering the exact screen .
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- Customer:
- JOHN from NAUGATUCK, CT
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Wire Meshing Had Broken Away From The Rubber Framing Tha Was To Hold It Together And Lint Was Bypassing The Screen And Getting Into The Vent Tube.
Opened the dryer door unsrewed the two phillips holding the filter framework in place did a two second swap-out dropped the new unit into place the new unit and refastened it with the 2 screws that held the old one in place . And was drying a load of clothes within two minutes . . Thank you jg
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- Customer:
- charles from nantucket, MA
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
replace old screen
take out of box remove old screen drop in new screen
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- Customer:
- steve from scottsville, KY
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
screen fell out of lint screan frame
remove 2 screws,pull frame out. put new in. tighten 2 screws. put lint screen in
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- Customer:
- TJ from SCOTT DEPOT, WV
- Parts Used:
- 131658800
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
Door catch broken
Popped in the new door catch! Tightened the hinge screws( which work loose and allow the door to droop. The reason the catch broke!) Also put red Loctite on the screws in an attempt to keep them from backing out again! Working great so far!!!
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- Customer:
- Paul from Dennis, MA
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
The lint screen was old, rusty, and torn.
This was the easiest and most inexpensive repair I ever had on a dryer. I did a search on the internet, found "PartSelect.com" searched their web site, found the part I needed (at a very reasonably low price) ordered it, received it within 2 days, opened the box, removed 2 screws from the old part, put the new part in, replaced the 2 screws, inserted the filter screen... and my wife was happy. Thank You PartSelect.com for perfect selection, ordering and service.
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- Customer:
- Bill from Shelby, MI
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Riped lint screen
This was easer than, well brushing my teeth. And it took less time than that too. Really, really easy, just like I read.
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- Customer:
- William from Hudson Falls, NY
- Parts Used:
- 5303281153
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
Loud Squealing
Remove top panel with large flat screwdriver and 2 screws in back.Remove bottom panel with 2 screws.Release belt tensioner and remove belt.Remove 3 screws in center of drum inside.Remove drum. Remove rear bearing by pulling up on assembly.Replace all parts in reverse order.
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- Customer:
- STEPHEN from Nashville, TN
- Parts Used:
- 134120900
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
No Heat, Dryer Runs, But Right Side Of Timer Would Not Advance, Left Timer Would
I used the percentage scale on this website to try and determine the likely cause. After reading several sites, I couldn't make sense of the timer not working on just one type cycle. When I got the dryer drum off, I could plainly see that one of the heater coils was broken. They get heat stressed and break down over time and a hard shake probably finished this off. This unit is 5 plus years old. It was Saturday and I had no heater, so I actually found it at a local parts supplier. Also replaced the drum bearing and the bearing cup in the rear along with the heater. BTW, a new heater comes with a HIGH thermal switch attached to it so don't buy it extra. The bearing cone also comes with a new bushing in the pack. I DID use the Thermal Limiter that I order from the site because I was already in there. Everything works great now. I may have gotten most off my parts elsewhere but this site was the biggest help of them all. I will definitely be back here again.
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- Customer:
- Jeff from Reidsville, NC
- Parts Used:
- 5303937139, 5303281049
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers
Clothes where getting brown stripmarks on the fabric.
After removing the front door of the unit I removed the Drum seal felt and upper felt part. Then I cleaned the metal ring with acetone to remove dirt. We you install the new parts the glue sent with the Drum Glide is enough for the task with a little left over. Now its working great.
Thanks for good part Jeff
Thanks for good part Jeff
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- Customer:
- jeffrey from round lake heights, IL
- Parts Used:
- 5303281049
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers
The old drum seal top had torn off.
Opened the drayer top and then removed the front panel.
Removed the bottom seal from the acr as it was warn.
Carefully scarped off the remaining bits of felt from the arc.
Applied the supplied adhesive to the top half of the cleaned arc.
Placed the seal and held in place with small spring clamps.
Let it dry for an hour, then I repeated the process with the bottom seal.
I let it dry over night, overkill probably but I wanted it to stay.
Replaced the front with new seal and closed up the top.
It has been working well since. Thanks for stocking parts that help out homeowner's on tight budgets.
Removed the bottom seal from the acr as it was warn.
Carefully scarped off the remaining bits of felt from the arc.
Applied the supplied adhesive to the top half of the cleaned arc.
Placed the seal and held in place with small spring clamps.
Let it dry for an hour, then I repeated the process with the bottom seal.
I let it dry over night, overkill probably but I wanted it to stay.
Replaced the front with new seal and closed up the top.
It has been working well since. Thanks for stocking parts that help out homeowner's on tight budgets.
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- Customer:
- Shelia from Elizabethtown, IL
- Parts Used:
- 134503600
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Wrench set
replaced broken belt
Romoved front from dryer . Then loosened tub , slid belt on , reached in back and put belt on pulley , turned tub till belt went into place and reassembled dryer all with the help of a 3 year old and an8 year old,so in my oppinion it was one of the easiest fixes i've ever done!
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- Customer:
- Cherry from WATERVLIET, NY
- Parts Used:
- 134503600, 5303281153, 131825900
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Very noisy
Replaced rear drum bearing, drum support bearing & drum belt. Still very noisy. Will order new motor & see if that does the trick.
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