FDG847GCS0 Frigidaire Dryer - Instructions
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- Customer:
- Michel from CHICAGO, IL
- Parts Used:
- 5303281153, 5303281153, 131825900, 5303281153
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 1- 2 hours
- Tools:
- Pliers, Screw drivers
The drier was "screeching"
First of all, the folks at Part Select have been terrific. I balled up my address and they were great in correcting my error and getting the parts promptly to me. They provide directions with the parts. And You Tube, is a wealth of information too. The process is to remove the drum and replace the nylon busihing that supports the drum at the back of the machine. Getting it out was no sweat. Getting the drum back in was a bit more challenging single handed. If I was going to make any suggestion it would be this is a good project for two sets of hands with the second set needed for about ten minutes. The You Tube video I watched said putting the front cover with the drum attached to the back of the unit would be the challenge and they were right. Otherwise, super easy and the results are it's back to "new" condition. Thanks again to Part Select!
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- Customer:
- Gordon from Canton, PA
- Parts Used:
- 5303281049
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers
Small burn marks on light clothing
First I unpluged the machine, then opened the top with a flat head screw driver. Then I removed the two screws inside, unpluged the door sensor. (makes it stop when opened) Removed old gasket, cleaned with emery cloth, cleaned the residue and applied the glue provided. Waited about 1 min. and applied the new gasket leaving about 1/8'' of it hanging over the door facing the drum.
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- Customer:
- Matthew from JOLIET, IL
- Parts Used:
- 5303937186, 5303931775
- Difficulty Level:
- Very Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Wrench set
No heat
Raise the top and remove the front panel assembly. One philips screw, 24mm gas line coupler and 3 electrical connectors frees the burner assembly. Slid the old igniter out and the new one in.2 philips screws to remove the coil retainer and replace the coils.
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- Customer:
- Joyce from North Dighton, MA
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
The lint screen had tears on it which could cause a serious problem, possibly a fire.
I unscrewed the old the lint screen FRAME and easily removed it, replacing it with the new one. The new lint -- SCREEN -- just needed to be squeezed here and there, and molded into a better shape. The screen itself, arrived flattened on the bottom, causing it to be too wide and difficult to remove from the frame. I easily molded it with my hands into the shape of the previous one and it slipped right into place. ( Shaped like an oval, flexible sack.) VERY easy!
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- Customer:
- Luann from Huntersville, NC
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Lint screen had torn
For me it wasn't even a repair, but rather, open the package, take out and discard the old lint tray and pop the new one in! Done. I didn't have to replace the frame. I would like to comment on how easy ordering was from partselect.com and how quickly the part arrived. Very satisfied customer! Thank you!
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- Customer:
- Doug from ODESSA, TX
- Parts Used:
- 5303281153, 5303281153, 131825900, 5303281153
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
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- Customer:
- Harriett from Leesburg, FL
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Needed new lint screen for dryer
Removed 2 screws and dropped new screen holder in with lint screen in it and replaced screws. Really easy
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- Customer:
- Vincent from Fairfield, CA
- Parts Used:
- 5303931775
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
heat would initially come on then go off or sometimes not come on at all.
1. unpluged the dryer and turned off the gas.
2. pulled dryer out so i'd have ample room to work on it.
3. used large flat blade screwdriver in the front between the top lid and dryer face to gently pop-up the lid.
4. removed 4 screws from inside, that hold the face to the main box leaving the wires all intact.
Found the coils on the lower left, held in place by two screws and plate.
5. took a good look at thier orientation before unpluging old and installing new, I recommend one at a time.
6. Vacuumm any exceess lint and check foam seal between lint trap and exhuast duc, the glue came undone on mine causing extra lint dust that is potentially flamable.
6. screw dryer front back on to main box, make sure to check wiring harness and that all electrical blade connectors are still pluged in to their componants.
7. At this point plug in, turn on gas and do a test run.
8.if everything checks out good then lower top make sure flexable exhuast hose is still connected on hte back of the dryer.
9. Tell your wife or girlfriend or husband or boy friend they can now finish your laundry :)
2. pulled dryer out so i'd have ample room to work on it.
3. used large flat blade screwdriver in the front between the top lid and dryer face to gently pop-up the lid.
4. removed 4 screws from inside, that hold the face to the main box leaving the wires all intact.
Found the coils on the lower left, held in place by two screws and plate.
5. took a good look at thier orientation before unpluging old and installing new, I recommend one at a time.
6. Vacuumm any exceess lint and check foam seal between lint trap and exhuast duc, the glue came undone on mine causing extra lint dust that is potentially flamable.
6. screw dryer front back on to main box, make sure to check wiring harness and that all electrical blade connectors are still pluged in to their componants.
7. At this point plug in, turn on gas and do a test run.
8.if everything checks out good then lower top make sure flexable exhuast hose is still connected on hte back of the dryer.
9. Tell your wife or girlfriend or husband or boy friend they can now finish your laundry :)
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- Customer:
- Steven from San Francisco, CA
- Parts Used:
- 5303931775
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
No heat.
As others have described in more detail... I lifted the top, removed the 2 screws holding the front panel (one on each side, inside the control panel on either side - not the easiest to get at, but not too bad), popped the clips holding the front panel in place and removed it. With the front panel off, the location of the coils is obvious (lower left side). The only challenging aspect of this repair is that the 2 screws holding the coils in place are really torqued in so it was crucial to use the exactly correct size screwdriver and not let the screwdriver slip while unscrewing those screws. Actually swapping out the coils took seconds, of course they have to go in exactly the same way as the old ones. I did take a few minutes extra to vacuum out years of lint from the inside of the dryer. Overall, much easier and cheaper than I was expecting and now I know where everything is inside the cabinet.
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- Customer:
- Paul from Dennis, MA
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
The lint screen was old, rusty, and torn.
This was the easiest and most inexpensive repair I ever had on a dryer. I did a search on the internet, found "PartSelect.com" searched their web site, found the part I needed (at a very reasonably low price) ordered it, received it within 2 days, opened the box, removed 2 screws from the old part, put the new part in, replaced the 2 screws, inserted the filter screen... and my wife was happy. Thank You PartSelect.com for perfect selection, ordering and service.
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- Customer:
- Bill from Shelby, MI
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
Riped lint screen
This was easer than, well brushing my teeth. And it took less time than that too. Really, really easy, just like I read.
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- Customer:
- David from Petaluma, CA
- Parts Used:
- 5303931775
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set
Gas dryer wouldn't stay hot.
I definitely would not have tried to do this had it not been for the other testimonials written here. But it sounded so easy, I had to just try it (the repair man estimated that with parts and labor, we would be looking at somewhere between $250 and $300!).
The repair itself took less than 15 min, but I spend a good deal of time looking around the garage for a few screwdrivers and my socket set (me and tools don't meet too often). I could simply pry up the top cover on the dryer with my hands, then got it all the way up after removing two screws from the lint trap and undoing this really annoying wire connector thing. From there the front panel lifted off. To remove the drum, just had to release the tensonier on the belt, and it came right out. From this point it was really obvious where the replacement parts would be going. A few screws later, and I could swap the parts, and put humpty dumpty back together again.
It works!!!
The repair itself took less than 15 min, but I spend a good deal of time looking around the garage for a few screwdrivers and my socket set (me and tools don't meet too often). I could simply pry up the top cover on the dryer with my hands, then got it all the way up after removing two screws from the lint trap and undoing this really annoying wire connector thing. From there the front panel lifted off. To remove the drum, just had to release the tensonier on the belt, and it came right out. From this point it was really obvious where the replacement parts would be going. A few screws later, and I could swap the parts, and put humpty dumpty back together again.
It works!!!
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- Customer:
- Michael from Weston, FL
- Parts Used:
- 131858004
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Water temperature knob broke
I push the new knob onto the post that fit the knob
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- Customer:
- steve from scottsville, KY
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
screen fell out of lint screan frame
remove 2 screws,pull frame out. put new in. tighten 2 screws. put lint screen in
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- Customer:
- charles from nantucket, MA
- Parts Used:
- 131390300
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
replace old screen
take out of box remove old screen drop in new screen
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