DE271EDW4 Frigidaire Dryer - Instructions
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- Customer:
- Randall from New Roads, LA
- Parts Used:
- 131825900, 5303281153, 131724301
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers
bearing bad and shaft broken
replaced bearing and shaft new belt and everything works just fine
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- Customer:
- JOHNNY from ASHEVILLE, NC
- Parts Used:
- 5303281154
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver
Belt snapped after 13 yrs. maybe 15 yrs
I raised up the top then took 4 bolts out of the front and it came off and then I slipped the belt on. Now was the fun part. I tried to put belt around the tension spring from the front of the machine. Bad mistake. So I turned the machine around and took off little plate bottom left, back side reached in and WA-LA back in commision. I took a long brush and cleaned all I could reach and put it back together. Bingo, back in business.
And I'm 71 yrs. old.
And I'm 71 yrs. old.
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- Customer:
- SHARON from SUMMERVILLE, SC
- Parts Used:
- 5303281153
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Screw drivers, Socket set, Wrench set
Dryer making horrible squeaking sound when running
I am a "do-it-yourselfer" despite my husbands opposition. I followed instructions from one of the posts on the site and took apart the dryer. I found the location of the rear bearing and took it out and replaced it with the new one. Easy as that. Made sure the parts looked the same. Made sure I saw how everything went together. I used a magnet to hold the ball bearing in place on the rear mount and taped the metal bracket on the outside of the dryer. Screwed it right in. Reassembled in reverse and works like a charm. To all the women out there who don't think they can do this. It's easy. Give it a try.
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- Customer:
- Lewis from Thornton, CO
- Parts Used:
- 131825900
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
loud squeeling noise
After changing the drum support bearing, and the front felt ring, the noise continued. It turned out to be the tensioner pully. The harmonic vibration travels throughout the dryer box like an instrument so you can't tell where the sound is comming from. Before you do anything, spray a little wd40 between the bushing and the shaft on the belt tenioner pully. If the squeel goes away, you have found your smoking gun.
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- Customer:
- Joyce from PORTAL, GA
- Parts Used:
- 131658800
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
Our door catch got lost inside the dryer after the door was slammed to hard
I took the new door catch out of the packaging and just snapped it in place it was easy peasy and took less time than opening the package
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- Customer:
- chris from dallas, TX
- Parts Used:
- 131658800
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Latch on dryer no longer worked
So easy! I ordered the part on the website. Received it 24 hours later. And popped it in place. Good as new.
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- Customer:
- Lawrence K from Harrisonburg, VA
- Parts Used:
- 5303212849
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Socket set, Wrench (Adjustable)
New Belt slipped off pulley - drum won't rotate
Removed access door. Disengaged spring, removed old idler. Slipped belt around new idler and motor pulley. Difficulty is putting spring back and inserting idler pulley bracket back in place while there is a lot of tension from the belt. Finally used adjustable wrench as a mini hammer.
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- Customer:
- DOUGLAS from EAST LANSING, MI
- Parts Used:
- 5303212849
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers
Extremely noisy, grinding, old electric dryer.
Removed small panel at rear of dryer which allowed access to the Idler Pulley asembly. Easily removed, and replaced with new idler assembly. Fed belt onto new pulley and attached tension spring. Actually, this replacement idler pulley assembly is much better than the original. It has a shoulder to allow the belt to "track" better over drum and around motor pulley. Dryer is now extremely quiet, like a new machine. Hope to get another 29 (yes 29) years out of it. Extremely pleased. Doug East Lansing, Michigan
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- Customer:
- John from Temple City, CA
- Parts Used:
- 5303281154, 5303212849
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Nutdriver, Pliers, Socket set, Wrench (Adjustable)
broken belt and pulley
First of all, I've purchased a belt from local service center that cost me more than $21 (local tax is 8.5%). But, I can not find the idel pulley assembly so I searched on the Internet and ordered from PartSelect.com.
Surprisedly, my order came just one day - they must cross-ship from local distribution that it's even faster than to get those in local stores (driving .. and hope they have what I want ..).
I've replaced the belt 2 days ago - it's easy with 4 screws removed to pull out the front door. The back panel is opened with 2 screws remove, and very easy to replace the pulley.
It's a heavy duty gas dryer made in 1989 and this is the third time I changed the belt and the first time to change a new pulley. I would recommend to change the idle pulley because I may not need to change the belt if I have had replaced it last time. A broken or not functional idle pulley may damage the belt in a short time.
Appliance such as gas dryer like mine will last forever with replaceable belt and pulley. I'm really happy to see a working dryer (almost 20 years old) and my wife is asking a small component for her washer .. that I think I can easily fix that too .. with the help of PartSelect search.
Hope this will help.
John
Surprisedly, my order came just one day - they must cross-ship from local distribution that it's even faster than to get those in local stores (driving .. and hope they have what I want ..).
I've replaced the belt 2 days ago - it's easy with 4 screws removed to pull out the front door. The back panel is opened with 2 screws remove, and very easy to replace the pulley.
It's a heavy duty gas dryer made in 1989 and this is the third time I changed the belt and the first time to change a new pulley. I would recommend to change the idle pulley because I may not need to change the belt if I have had replaced it last time. A broken or not functional idle pulley may damage the belt in a short time.
Appliance such as gas dryer like mine will last forever with replaceable belt and pulley. I'm really happy to see a working dryer (almost 20 years old) and my wife is asking a small component for her washer .. that I think I can easily fix that too .. with the help of PartSelect search.
Hope this will help.
John
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- Customer:
- james from tahlequah, OK
- Parts Used:
- 5303281153
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
bearing went out
took apart and replaced parts easy to do but no one in my town can get me parts. thay want 100.00 gust to come out and look at it so found parts online and thats that
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- Customer:
- khalid from HILLSBOROUGH, NJ
- Parts Used:
- 5303212849
- Difficulty Level:
- Very Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Drum was not revolving
Open the back plate. Broken pulley was already out of place. Put the spring on the pulley and placed it. It took me less than 10 min
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- Customer:
- David from PORT CLINTON, OH
- Parts Used:
- 5303281153
- Difficulty Level:
- Very Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Squeaking
Watched Video Provided. Very Simple Repair. Asked my lovely wife to hold drum in place while replacing drive belt. She gladly complied and is back doing what she seems to love most. And no, I'm not kidding. Our washer and dryer seem to run 24/7/365. I've completed various repairs on both appliances over the last couple of years and saved 100's of dollars thanks to this site .
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- Customer:
- April from CARYVILLE, TN
- Parts Used:
- 5303281153
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Noisy
Took it apart and installed the parts. Then I threw the dryer in the trash and bought a new one.
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- Customer:
- Debra from BROOKLYN, NY
- Parts Used:
- 131658800
- Difficulty Level:
- Very Easy
- Total Repair Time:
- 15 - 30 mins
Just popped the part I ordered right in and it's was closing in no time !
Just opened package and popped the part right in!
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- Customer:
- Doug from ODESSA, TX
- Parts Used:
- 5303281153, 5303281153, 131825900, 5303281153
- Difficulty Level:
- Easy
- Total Repair Time:
- 1- 2 hours
- Tools:
- Nutdriver, Pliers, Screw drivers
Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
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