PDWT302V50II General Electric Dishwasher - Instructions
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- Customer:
- Edward from Granite Bay, CA
- Parts Used:
- WD08X10032
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
tear in the tub gasket
Pulled out the old gasket and replaced with the new gasket. Inserted the steel spring clip into the ends of the gasket. Repair complete.
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- Customer:
- Peter from Davenport, FL
- Parts Used:
- WD14X10009
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Hing arm broke
Removed dish washer from cabinet area and snapped new clip into cable and hook into support.. The time that took the longest was to removed the screws to pull the unit out of the cabinet area.. Very easy fix...
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- Customer:
- Pierangela from River Forest, IL
- Parts Used:
- WD12X10163
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
the soap dispenser door had broken off
Open the door and go along entire edge of door and use Philipps to unscrew the front panel of the door from the inside panel of the door. Once unscrewed open carefully. There are screws in the dispenser cup. Undo those and then there are two plugs to be undone. There is also the main black computer component that has to be unplugged from its cord. Just remove and screw everything back the way it was. This was my first time and I am a female age 58 years old. It was simple. If I had to do it again I could do it in less than half the time.
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- Customer:
- William from Sterling, VA
- Parts Used:
- WD15X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable)
Serious water leak into basement from around a kitchen sink pipe.
Removing two screws holding the bottom trim/sound baffle opened a view of water dripping from the water intake valve at the left front of my Monogram dishwasher. I then turned off the local (under my adjacent sink) separate feed valve for the washer, then opened the (dedicated) breaker for the machine at my breaker panel.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
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- Customer:
- Cono from Bethlehem, GA
- Parts Used:
- WD02X10169, WD01X10107
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers
Loud noise when running
Middle arm bearing used a pair of pliers to unscrew the screw and to re-screw with new bearing in place. NO did not have to disconnect the arm. Lower arm turn counter clockwise to remove (comes off very easy) stick needle nose straight down opening and remove bearing. Use needle nose to place new bearing.
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- Customer:
- Eric from Stephens City, VA
- Parts Used:
- WD12X10122
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Old rinse aid cap melted by heating element
Simply screwed in the new rinse aid cap to replace the old one
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- Customer:
- Judith from Ventura, CA
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Rusted and Wheels falling off
I received the part very quickly. I threw away the old rack and put the new one in it's place. No tools or instructions were necessary. The new rack had all of the wheels and combs included. I did not have to purchase them separately. This is a much better designed part than the original rack. The combs are spread differently to better support plates, and the wheels are combined and enclosed to better support the rack. Also, I feel that this was a good price. Thank you!
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- Customer:
- Vivian from Belfast, ME
- Parts Used:
- WD12X10163
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Jet Dry Rinse was not dispensing
Removed 8 screws from inside door cover. Opened the door and pulled off two wires from the detergent rinse dispenser with a pair of pliers and removed screws that held the dispenser in place. Removed the dispenser, placed new part in place and put screws back in and put wires back onto the dispenser. Closed cover and screwed back down. Easiest thing I've ever done.
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- Customer:
- Mary from Dana Point, CA
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
The rack assembly needed replacing
Just removed the prior rack and put the new one in. Much improved design on the wheels and rack seems of better material as well. The rack does not have as many holders as the prior rack dishes and pans do not fit as well.
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- Customer:
- Edith from Petaluma, CA
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
lower rack was rusting, and one wheel came off
I took the old rack out of the dishwasher, took the new one out of the box it was shipped in and slid it into place. Works great. Need top one soon, but will wait until there's some extra money to order it!!!! Thanks for everything!!
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- Customer:
- joseph from pittsburgh, PA
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
bottom rack was rusting away
opened the dishwasher .............removed the old and slid in the new ...then attached by dropping in the utensil compartment.....piece of cake
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- Customer:
- MICHELLE from CHESTERFIELD, NJ
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
The Wheel Was Stuck And It Was Hard To Rolled It
I just ordered another one of the wheel rack and it was that easy. No tool required.
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- Customer:
- Jack from Indio, CA
- Parts Used:
- WD28X24469
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
removed old silverware basket
installed new silverware basket
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- Customer:
- kathy from zionsville, IN
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Lower Carriage Wheels So Bent It Would Not Move.
Took old one out, put new one in in less than 20 seconds!
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- Customer:
- Calvin from Mankato, MN
- Parts Used:
- WD12X10122
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
aid cap melted
Twisted new one in place of old. Disappointed that there was a melting issue at all. Need to investigate problem.
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