PDWT100V00BB General Electric Dishwasher - Instructions
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- Customer:
- Donald from The Villages, FL
- Parts Used:
- WD26X10053
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver
Leak from motor output/pump input shaft
Cut power and water flow to the appliance. Laid appliance on its side, removed the electrical lead from the motor. Remove the mount from the back of the motor and loosened the two clamps- one to the sump and one to the discharge tube. Removed and replaced the pump/motor assy. with the new one, reinstalled the clamps, rear mount and electrical lead. Righted the unit and fired it up. Worked fine.
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- Customer:
- Calvin from Mankato, MN
- Parts Used:
- WD12X10122
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
aid cap melted
Twisted new one in place of old. Disappointed that there was a melting issue at all. Need to investigate problem.
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- Customer:
- Kenneth R from Marcellus, MI
- Parts Used:
- WD15X10014
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Wrench (Adjustable)
Fractured brass bezel on bottom of valve- Leaking
simply removed broken valve and replaced with new valve, easy peasy. shipping was GREAT, Overnight. all in all a easy fix.
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- Customer:
- Victoria from Shepherdstown, WV
- Parts Used:
- WD08X10032
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
Water leakage
I examined how the old gasket was attached before removing it. I then pushed in the new gasket needing no tools. There has been no water leakage since.
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- Customer:
- paul from petaluma, CA
- Parts Used:
- WD15X10014
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Wrench (Adjustable), Wrench set
water dripping near front left of dishwasher
look at neww part first then r&r
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- Customer:
- Frances from Goodyear, AZ
- Parts Used:
- WD08X10032
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
Our tub gasket was torn by leaning utensils (a definite design flaw.)
Just have a good look at how the original is installed before removing, then clean the area. The new one was a breeze to install, just line it up and pop it in.
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- Customer:
- William from Sterling, VA
- Parts Used:
- WD15X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable)
Serious water leak into basement from around a kitchen sink pipe.
Removing two screws holding the bottom trim/sound baffle opened a view of water dripping from the water intake valve at the left front of my Monogram dishwasher. I then turned off the local (under my adjacent sink) separate feed valve for the washer, then opened the (dedicated) breaker for the machine at my breaker panel.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
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- Customer:
- Lloyd from Mint Hill, NC
- Parts Used:
- WD12X10163
- Difficulty Level:
- Difficult
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Soap Dispenser not Opening
NOTE I have classified this is a DIFFICULT JOB, but NOT because of the mechanics involved [including the electrical connectors UN-plugging and re-plugging, BUT DUE to the ANALYSIS you need to do to determine whether the SOAP DISH PART or the CONTROLLER is at fault. And this ANALYSIS will probably require you to get into the DISHWASHER DOOR twice. Once to do the analysis and then again to replace whatever part you target. Being you will want to continue to use the DISHWASHER by manually dropping the soap door [or just soap] at the appropriate time in the cycle, while awaiting the new part, which means you have re-button up the door and take it apart again when the new part arrives. . Before starting, view PartSelect's VIDEO on replacing the SOAP DISPENSER, but ignore THE STEPS OF REMOVING AND REPLACING THE SOAP DISPENSER.PART, at this time. The analysis starts with MANUALLY trying to activate the mechanical soap door release on the back of the mounted SOAP DISPENSER, with the soap door closed. It should take only ounces of downward pressure [towards the door hinge] on the vertical plastic piece in a channel near the center of the dispenser, to release the soap door. Next if you have access to an OHM METER {or MULTIMETER} or a DC POWER SUPPLY [to test the the activation of the door release] pull the two connectors on the SOAP DISH SOLENOID [a set pointed pliers will be helpful, as outlined in the VIDEO]. If measuring the SOLENOID's resistance it should read roughly 1800 OHMS. If using a DC POWER SUPPLY, you will probably need at least 25 volts DC to trigger the SOLENOID [NOTE I do not have a variable DC POWER SUPPLY to check it out nor do I know the voltage that the DISHWASHER uses]. Do not bother to measure the resistance of CONTROLLER's driving circuitry [the two wires having connectors], as it will read INFINITY, regardless of whether GOOD or BAD, The CONTROLLER apparently uses a RELAY on this circuit, as opposed to some kind of solid state switch. Replug the SOLENOID connectors. Re-buttoned up the DISHWASHER as shown in the VIDEO, assuming you are going to continue using it If you determine no problems in the above tests, then consider it a CONTROLLER pro0blem and you will need to order one. Otherwise you should have found indications of a SOAP DISPENSER PROBLEM. . When the replacement part arrives and you ready to install it, refer again to PartSelect's VIDEO on replacing the Soap Dish Dispenser for a refresher Following the VIDEO completely, if you replacing the DISPENSER. If you are replacing the CONTROLLER, once inside the DOOR, you will need to remove around 6 individual electrical connectors [before doing ANYTHING REMOVE POWER from the DISHWASHER [as instructed in the VIDEO}. These connectors [all but any single wire connectors] are designed to be plugged only one specific way, so when re-plugging NEVER FORCE a connection, The best way to make sure you do not get confused, take a picture of all the connectors -OR- make notes on the looks and orientation of each multi-wire connector. There is one mounting screw on right side of the CONTROLLER. When installing the new CONTROLLER there are mounting EARS on the left side that are first engaged by having the CONTROLLER tilted up on the right side. Replace the mounting screw. Replugged all the connectors using whatever guide you made. Proceed to put the DOOR back together as outlined in the VIDEO.
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- Customer:
- Nugent P from Garner, NC
- Parts Used:
- WD15X10014
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Screw drivers, Socket set, Wrench set
dishes not getting clean, top rack not washing
remove front lower cover, 2 philips screws, turn off water supply under kitchen sink to dish washer, turn off power to dish washer, remove water supply line to valve, remove power to valve, clip ons, remove two 5/16" screws holding valve on, turn valve gently to access clip holding washer supply hose, push clip up hose and hold hose while pulling valve off. re-install in reverse order, a flash light helps.
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- Customer:
- ronald from culver city, CA
- Parts Used:
- WD18X10026
- Difficulty Level:
- A Bit Difficult
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers
water leak
Came home for lunch to discover the kitchen rug soaked and the dishes I had started when I left that morning unclean. Not sure what happened, pushed start again and immediately found water flowing out from under the machine. pulled the machine out and discovered that mice had chewed through the pliable vinyl sump tank. found the part number in my owners manual and google turned it up on Part Select. this was on Saturday and I had the part Tuesday. very satisfied
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- Customer:
- Bill from Monterey, CA
- Parts Used:
- WD15X10014
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
Water leaking on floor
Water was leaking from under refer next to installed under counter dishwasher. Once determined to be dishwasher not refer I removed dishwasher toe place was able to see dripping inlet solenoid valve. I had to disconnect 11V power, shut off inlet water, disconnect inlet water house and remove dishwasher from under counter. Once dishwasher was in center of kitchen I flipped it upside down and removed the electric solenoid inlet valve. Removing the valve took one wrench to remove inlet hose then two wrenches to remove 90 degree brass fitting and another to hold solenoid. I used a nut drive to remove two screws that released the solenoid from the dishwasher frame. I used teflon tape to reattached the 90 degree brass fitting and inlet hose.
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- Customer:
- Brett from Ocala, FL
- Parts Used:
- WD18X10010, WD12X10061
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable)
Water was leaking out of bottom and not filling washer. Mouse at through this piece
Shut off water, disconnect drain line from disposer. Remove dishwasher from wall and remove water feed line. Unplug or disconnect power to unit. Remove upper and lower dish racks as well as lower water sprayer bar, and filters. Lay dishwasher down on backside (make sure to catch water with bowl). Disconnect pump connector with nut driver and replace. Stand dishwasher back up and reverse removal process
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- Customer:
- Robert from Wantage, NJ
- Parts Used:
- WD15X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 30 - 60 mins
dishwasher was not filling with water
very happy with the product and fast shipping. removed kick plate from dishwasher, inlet valve was on the front left bottom slid out dishwasher removed two screws and disconnected water line,and installed new inlet valve,very simple job if your somewhat handy,make sure you use thred sealant on water line when re installing
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- Customer:
- kathy from zionsville, IN
- Parts Used:
- WD28X25960
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Lower Carriage Wheels So Bent It Would Not Move.
Took old one out, put new one in in less than 20 seconds!
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- Customer:
- James from Jefferson City, MO
- Parts Used:
- WD28X10128
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
Holes In Silverware Basket
Just pulled out the old basket and put in the new one. . Don't know the holes got into the basket. . .
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