GLD5600V00BB General Electric Dishwasher - Instructions
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- Customer:
- stephen from mashpee, MA
- Parts Used:
- WD35X21038
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
bottom basket of dishwasher kept following out
i needed new rollers and inserts to keep wheels on now its like new when i pull out bottom basket
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- Customer:
- julie from Saint Charles, MO
- Parts Used:
- WD12X10163
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
soap dispenser latch was broken & didnt shut
We had to replace the soap dispenser. My husband is not very handy & this was a snap. You take off the front panel (cover) of the sishwasher & simply unscrew the old one & screw in the new one. I probably could have done it myself.
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- Customer:
- R. Cecil from Norfolk, VA
- Parts Used:
- WD35X21038
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
wheel was distorted
Simply replace wheel
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- Customer:
- Vicki from Mooresville, NC
- Parts Used:
- WD12X10163
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Soap Dispenser latch broke
I removed six screws and unplugged the module and removed.
Replaced by the new module and plugged in and then replaced the six screws.
Very easy to fix.
Replaced by the new module and plugged in and then replaced the six screws.
Very easy to fix.
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- Customer:
- Erin K. from Las Vegas, NV
- Parts Used:
- WD12X10163
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
soap dispenser was not staying closed....
hubby had no prob replacing the new part!!YEA!!dishes are clean again!
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- Customer:
- Frank from Tinton Falls, NJ
- Parts Used:
- WD22X10029
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
The old plastic filter's corner were bent up allow food to get into the plumbing going to the articulation sprayers and clogging them.
Remove bottom articulating sprayer and water fittings. Remove and replace filter
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- Customer:
- ROY from CULPEPER, VA
- Parts Used:
- WD13X10045
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
broken door handle actuator
Parts were easy to find, easy to order and arrived prior to the advertised delivery date. Instructions for replacement were easy to understand and in about 10 minutes the old part was removed, and the new one installed. thanks for your prompt and efficient company.
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- Customer:
- Nicholas from Alexandria, VA
- Parts Used:
- WD35X21038, WD35X21038
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
lost wheel
just snapped the new part in. couldn't have been easier
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- Customer:
- william from sykesville, MD
- Parts Used:
- WD18X10010, WD18X10008
- Difficulty Level:
- Really Easy
- Total Repair Time:
- More than 2 hours
- Tools:
- Socket set
water leaking from sump
I had a slow leak from vicinity of sump. I replaced sump and pump connector as these were only likely sources of leak based on parts select history. Turns out plastic tub had a fine crack. The crack was directly under the heating element which had melted the plastic and over time created this small crack that was found by a repair guy immediately. I even suspected a tub leak and searched for one but being directly under the element made it invisible to me and in an area I did not suspect (front). Oh well - also learned GE charges $100. to come to my house, show me a crack, and leave (I repaired it with epoxy).
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- Customer:
- Russell from Rosharon, TX
- Parts Used:
- WD02X10169, WD02X10067
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
missing screw for Spray Arm
Remove top rack stops, slide out upper rack from rack railing, turn over upper rack and attach spray arm using spray arm bearing and screw. Reassemble in reverse order.
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- Customer:
- Christopher from St Augustine, FL
- Parts Used:
- WD24X10045, WD12X10061, WD01X10103
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Rate chewed drain hose up.
Removed screws that held dishwasher under cabinet...pulled out DW...removed old part...replaced with new....easier than falling off a stump.
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- Customer:
- Sara from Greenwood, IN
- Parts Used:
- WD12X10163
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
The detergetn dispenser door hinge was broken.
I unscrewed the screws in the door of the dishwasher. Then pulled the inside part of the door up and unscrewed the 6 screws that held the dispenser. I am not sure the correct name of the part but it is on the backside of the dispenser and is red and it is where the wires connect to it, that was probably the most difficult part, disconnecting the plastic covers from the old dispenser. I used a butter knife to pop it out and then was able to get a better grip to pull them off. I pushed the wires on the new red thing and then put the new dispenser in place. You have to make sure that the dispenser is in the right spot and the brace on the underside of the inside part of the door, is in the correct place, otherwise, you will have a leak. Which is what happened to me. I just unscrewed and opened it again and screwed the screws tighter and it was fine.
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- Customer:
- William from Sterling, VA
- Parts Used:
- WD15X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable)
Serious water leak into basement from around a kitchen sink pipe.
Removing two screws holding the bottom trim/sound baffle opened a view of water dripping from the water intake valve at the left front of my Monogram dishwasher. I then turned off the local (under my adjacent sink) separate feed valve for the washer, then opened the (dedicated) breaker for the machine at my breaker panel.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
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- Customer:
- Anthony from Silver Spring, MD
- Parts Used:
- WD12X10163
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Soap door would not stay closed
Removed the holding screws around the edges; removed and replaced the soap container; reconnected the electrical leads, and done... Very simple fix. But it does get a little tricky since the door is spring loaded. NOTE: THERE ARE SCREWS AT THE BOTTOM THAT IS NOT OBVIOUS.
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- Customer:
- Chris from Carleton, MI
- Parts Used:
- WD15X10014, WD21X10355
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Wrench (Adjustable), Wrench set
The Water inlet valve was leaking.
I disconnected the pipes to the inlet valve. I removed the bolts from the bracket holding the valve. I tried to use two wrenches to remove the brass angle pipe thingie off the bottom of the old valve. I then beat on it with a hammer, then I just threw it against the basement floor till it came off. I would recommend getting a new brass angle pipe thingie before you start.
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