CDWT980V05SS General Electric Dishwasher - Instructions
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- Customer:
- Richard from Venice, FL
- Parts Used:
- WD24X10045
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Recived used without drain hose
It was an install. My problem is that the drain tube is not standard to other dishwashers,so I could not get it at either of the local home improvement centers. The good news is that it is larger than the standard, and offers better discharge.
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- Customer:
- julie from Saint Charles, MO
- Parts Used:
- WD12X10163
- Difficulty Level:
- Easy
- Total Repair Time:
- Less than 15 mins
soap dispenser latch was broken & didnt shut
We had to replace the soap dispenser. My husband is not very handy & this was a snap. You take off the front panel (cover) of the sishwasher & simply unscrew the old one & screw in the new one. I probably could have done it myself.
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- Customer:
- Robert from Hampton, GA
- Parts Used:
- WD14X10009
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
Door had no resistance/no balance/would fall open
First, remove the bottom front covers (two parts four screws). Second, remove the two screws at the top that secure the dishwasher to the counter. Third, gently pull away the dishwasher from underneath the counter just far enough to see and be able to remove the door spring(s) - one on each side. Fourth, remove the existing hinge arm link(s) if not already broken off, replace with the new one(s). Note that the door hinge goes on the door (front) side of the spring and the other side fits into a groove on the door arm - the other end of the spring attaches to one of the 3 available holes on the frame at the bottom. It would be a good idea to replace the hinge arm links on both sides even if only one is broken. Make sure that the door has the right tension (each spring can be hooked in 1 of 3 holes to adjust the tension). Then gently push the dishwasher back under the counter. Finally, replace the screws under the counter and replace the covers on the bottom front. All of this should take no more than 15-20 minutes. This was an easy job!
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- Customer:
- Vicki from Mooresville, NC
- Parts Used:
- WD12X10163
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Screw drivers
Soap Dispenser latch broke
I removed six screws and unplugged the module and removed.
Replaced by the new module and plugged in and then replaced the six screws.
Very easy to fix.
Replaced by the new module and plugged in and then replaced the six screws.
Very easy to fix.
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- Customer:
- Donna from Arlington, TN
- Parts Used:
- WD15X10014
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Pliers, Screw drivers
Water leaking out from bottom of Dishwaser
Very easy! Removed 4 screws that was holding the valve to the bracket. Placed bracket over water inlet line. Attached copper threaded coupling with pliers.Screwed valved on to the coupling. Attached bracket to the valve with 4 screws. Reattached water line. Attached bracket to frame of dishwaser. Put kickplate back on and done!
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- Customer:
- Erin K. from Las Vegas, NV
- Parts Used:
- WD12X10163
- Difficulty Level:
- Really Easy
- Total Repair Time:
- Less than 15 mins
- Tools:
- Screw drivers
soap dispenser was not staying closed....
hubby had no prob replacing the new part!!YEA!!dishes are clean again!
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- Customer:
- Russell from Rosharon, TX
- Parts Used:
- WD02X10169, WD02X10067
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers
missing screw for Spray Arm
Remove top rack stops, slide out upper rack from rack railing, turn over upper rack and attach spray arm using spray arm bearing and screw. Reassemble in reverse order.
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- Customer:
- Christopher from St Augustine, FL
- Parts Used:
- WD24X10045, WD12X10061, WD01X10103
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Pliers, Screw drivers
Rate chewed drain hose up.
Removed screws that held dishwasher under cabinet...pulled out DW...removed old part...replaced with new....easier than falling off a stump.
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- Customer:
- Donald from The Villages, FL
- Parts Used:
- WD26X10053
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver
Leak from motor output/pump input shaft
Cut power and water flow to the appliance. Laid appliance on its side, removed the electrical lead from the motor. Remove the mount from the back of the motor and loosened the two clamps- one to the sump and one to the discharge tube. Removed and replaced the pump/motor assy. with the new one, reinstalled the clamps, rear mount and electrical lead. Righted the unit and fired it up. Worked fine.
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- Customer:
- Kenneth R from Marcellus, MI
- Parts Used:
- WD15X10014
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Screw drivers, Wrench (Adjustable)
Fractured brass bezel on bottom of valve- Leaking
simply removed broken valve and replaced with new valve, easy peasy. shipping was GREAT, Overnight. all in all a easy fix.
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- Customer:
- William from Sterling, VA
- Parts Used:
- WD15X10014
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers, Wrench (Adjustable)
Serious water leak into basement from around a kitchen sink pipe.
Removing two screws holding the bottom trim/sound baffle opened a view of water dripping from the water intake valve at the left front of my Monogram dishwasher. I then turned off the local (under my adjacent sink) separate feed valve for the washer, then opened the (dedicated) breaker for the machine at my breaker panel.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
The replacement valve was identical form and fit to the original. It included the replacement mounting bracket integrated with the valve.
Removing two additional screws holding a bigger sound baffle backed with foam gave good access to replace the valve. The foam was fitted to the power box and a few other obstructions, and apparently stuck to something near the top. I ran my hand up separating the foam from the panel and both then came out easily. I reattached the foam to the panel with clear silicon adhesive.
Removing two screws from the front edge of the bracket holding the valve allowed dropping it down for fairly easy access to the clamp holding the flexible house from the valve to the washer. There wasn’t much slack, so I reached the spring clip with a long plier-like device with cups on the working sold as automotive hose clip tool for that purpose. Regular pliers would likely work, with more skin loss from hands.
That action then allowed pulling the valve out from under the machine (feeding slack in the flexible feed I have installed years ago between that valve and the one under my sink. A small adjustable wrench then made easy work of disconnecting the hose brass coupling from the valve.
The right-angle adapter between the valve body and flexible feed hose is apparently specific to the installation, so it had to be removed and attached to the replacement valve. That was facilitated by placing the valves in a large bench vise, clamping the mounting bracket with the right angle adapter up, and using the adjustable wrench again. The old valve had residue from metal pipe thread sealer, so I used some new sealer on the adapter when installing it. Take care. Getting some inside the valve might be a serious problem. Turn the adapter with the adjustable wrench for a snug fit facing the same direction as the plastic nipple for the machine-side hose.
Installation proceeded easily in reverse of the removal process, using a bit of care to fit that foam back around the intended machine projections. I actually used identical thread lattes screws (wider flange) to hold the upper baffle because I misplaced one of the original screws and decided to originals were distorting the mounting slots because the flanges were too small.
I ran the machine through two cycles before replacing the bottom trim, just to assure there were no leaks. Mild panic when the intake valve didn’t operate as soon as I expected, but it must have been some out of phase control operation, because it eventually operated, then operated as expected during the second cycle.
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- Customer:
- Frances from Goodyear, AZ
- Parts Used:
- WD08X10032
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
Our tub gasket was torn by leaning utensils (a definite design flaw.)
Just have a good look at how the original is installed before removing, then clean the area. The new one was a breeze to install, just line it up and pop it in.
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- Customer:
- Victoria from Shepherdstown, WV
- Parts Used:
- WD08X10032
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
Water leakage
I examined how the old gasket was attached before removing it. I then pushed in the new gasket needing no tools. There has been no water leakage since.
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- Customer:
- Chris from Carleton, MI
- Parts Used:
- WD15X10014, WD21X10355
- Difficulty Level:
- Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Pliers, Wrench (Adjustable), Wrench set
The Water inlet valve was leaking.
I disconnected the pipes to the inlet valve. I removed the bolts from the bracket holding the valve. I tried to use two wrenches to remove the brass angle pipe thingie off the bottom of the old valve. I then beat on it with a hammer, then I just threw it against the basement floor till it came off. I would recommend getting a new brass angle pipe thingie before you start.
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- Customer:
- Anthony from Silver Spring, MD
- Parts Used:
- WD12X10163
- Difficulty Level:
- Really Easy
- Total Repair Time:
- 15 - 30 mins
- Tools:
- Nutdriver, Screw drivers
Soap door would not stay closed
Removed the holding screws around the edges; removed and replaced the soap container; reconnected the electrical leads, and done... Very simple fix. But it does get a little tricky since the door is spring loaded. NOTE: THERE ARE SCREWS AT THE BOTTOM THAT IS NOT OBVIOUS.
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